Event Notification Report for January 30, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/29/2001 - 01/30/2001 ** EVENT NUMBERS ** 37697 37698 37699 37700 37701 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37697 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 01/28/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 23:38[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 01/28/2001| +------------------------------------------------+EVENT TIME: 22:28[EST]| | NRC NOTIFIED BY: SANTINI |LAST UPDATE DATE: 01/29/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVEN DENNIS R1 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STEAM GENERATOR BLOWDOWN ISOLATED FOLLOWING ALARM RECEIVED ON RAD MONITOR | | R-49 | | | | An alarm was received for rad monitor R-49, Steam Generator radiation | | monitor, due to a spike. This resulted in automatic closure of the Steam | | Generator Blowdown isolation valves which is an ESF actuation. All other | | primary to secondary leakage parameters were normal. At the time of the | | spike, the Nuclear NPO was adjusting 24 S/G sample flow to obtain the | | required flow (as found: 35gph, required: 38-40gph). AOI 1.2(Steam | | Generator Tube Leak Procedure) was entered and supplemental monitoring was | | initiated. There are no indications of primary to secondary steam generator | | tube leakage. | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATED AT 1350 ON 1/29/01 BY GOETHCHIUS, RECEIVED BY WEAVER * * * | | | | Upon further review, the closure of these isolation valves is not reportable | | per 10 CFR 50.72. These containment isolation valves are limited to a | | single system and therefore, no reporting is required. Investigation of the | | issue will be in accordance with our corrective action process. This event | | is retracted The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37698 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 01/29/2001| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 05:36[EST]| | RXTYPE: [3] CE |EVENT DATE: 01/28/2001| +------------------------------------------------+EVENT TIME: 22:45[CST]| | NRC NOTIFIED BY: PELLEGRIN |LAST UPDATE DATE: 01/29/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DALE POWERS R4 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRESSURIZER STEAM SPACE SAMPLE ISOLATION VALVES FAILED TO CLOSE | | | | At 2245 on 1/28/01 it was discovered that PSL-303 and PSL-304, Pressurizer | | Steam Space Sample Inside and Outside Containment Isolation Valves would not | | close when their respective control switches at OP-8 in the Control Room | | were taken to the "Close" position. The valves had been open since 1455 | | that same day to perform degas of the Pressurizer. The Nuclear Plant | | Operator first took the switch for PSL-304 to the "Close" position and | | observed that the valve continued to indicate "Open". He then took the | | Switch for PSL-303 to the "Close" position, and observed that valve continue | | to indicate "Open". Technical Specification 3.6.3 was entered and a Nuclear | | Auxiliary Operator was dispatched to verify the position of PSL-304 locally. | | PSL-304 was found to be in the open position and the on-shift chemistry | | technician confirmed that there were still indications of flow through the | | sample line. Another attempt to close PSL-304 was made using the switch on | | CP-8 in the control room. The Nuclear Auxiliary Operator observed that the | | valve moved approximately one quarter-inch in the closed direction. At | | 2257 PSL-304 was closed using the manual gagging device. At 2310 PSL-304 | | was de-energized to comply with the action requirements of Technical | | Specification 3.6.3.b. At 0007 on 1/29/01, another attempt was made to | | close PSL-303 using the control switch at OP-8. This attempt was successful. | | The affected containment penetration is a one-half-inch line and is | | currently isolated. They are investigating the cause. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37699 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HADDAM NECK REGION: 1 |NOTIFICATION DATE: 01/29/2001| | UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 16:31[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 01/29/2001| +------------------------------------------------+EVENT TIME: 16:20[EST]| | NRC NOTIFIED BY: CHARLES REID |LAST UPDATE DATE: 01/29/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DANIEL HOLODY R1 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION | | | | The licensee reported a spill of mercury greater than one pound mass to the | | State of Connecticut Department of Environmental Protection. The spill was | | just over one pound mass and occurred in the primary auxiliary building. | | The spill has been contained and a contractor has been contacted to clean up | | the spill. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37700 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 01/29/2001| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 19:38[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/29/2001| +------------------------------------------------+EVENT TIME: 18:10[CST]| | NRC NOTIFIED BY: JEFF NADEN |LAST UPDATE DATE: 01/29/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FISH KILL | | | | Clinton Power Station personnel have been investigating the cause of a fish | | kill on Clinton Lake that was first discovered on January 24, 2001. After | | reviewing environmental data, CPS has sufficient evidence to conclude that | | the plant trip on December 18, 2000, following a Group 1 isolation was the | | cause of the fish kill. During this event, the main steam isolation valves | | closed and all decay heat was removed through the suppression pool instead | | of the main condenser and discharge flume to the lake. With the sudden loss | | of heat, input into the discharge flume and the lake in the vicinity of the | | flume discharge, a rapid drop in lake temperature shocked the fish in this | | area causing a kill of an estimated 7000 fish. The majority of these fish | | were carp and buffalo head. CPS has provided pertinent plant data to the | | Illinois Department of Natural Resources and the Illinois Environmental | | Protection Agency. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37701 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 01/30/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 01:34[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 01/30/2001| +------------------------------------------------+EVENT TIME: 00:15[CST]| | NRC NOTIFIED BY: TEMPOE |LAST UPDATE DATE: 01/30/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY RELIEF VALVES WERE DECLARED INOPERABLE | | | | A Technical Specification shutdown was initiated as required by T.S. 3.6.E.2 | | following the discovery that not all of Section XI requirements were met | | with respect to the safety relief valves. The safety relief valves were | | declared inoperable @ 1830 on 1/29/01. The reactor conditions shall be as | | follows within 24 hrs: reactor pressure <110 psig and reactor temperature | | <345�F. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021