Event Notification Report for January 25, 2001
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
01/24/2001 - 01/25/2001
** EVENT NUMBERS **
37682 37683
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|Power Reactor |Event Number: 37682 |
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| FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 01/24/2001|
| UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 07:36[EST]|
| RXTYPE: [1] GE-4 |EVENT DATE: 01/23/2001|
+------------------------------------------------+EVENT TIME: 07:25[EST]|
| NRC NOTIFIED BY: ABRAMSKI |LAST UPDATE DATE: 01/24/2001|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: |STEVEN DENNIS R1 |
|10 CFR SECTION: | |
|*INB 50.72(b)(3)(v)(B) POT RHR INOP | |
|*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| HIGH PRESSURE COOLANT INJECTION SYSTEM DECLARED INOPERABLE. |
| |
| The flow controller for the High Pressure Coolant Injection (HPCI) system is |
| indicating approximately 1400 gpm with the HPCI system in the standby |
| condition. Because the cause of this condition is not known at this time, |
| the HPCI system is considered inoperable. |
| |
| The NRC Resident Inspector was notified of this event by the licensee. |
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|Power Reactor |Event Number: 37683 |
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| FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 01/24/2001|
| UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 12:20[EST]|
| RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 01/24/2001|
+------------------------------------------------+EVENT TIME: 03:30[EST]|
| NRC NOTIFIED BY: KEVIN DONNELLY |LAST UPDATE DATE: 01/24/2001|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |STEVEN DENNIS R1 |
|10 CFR SECTION: | |
|NONR OTHER UNSPEC REQMNT | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2 N Y 86 Power Operation |86 Power Operation |
| | |
| | |
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EVENT TEXT
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| 24-HR REPORT REQUIRED BY STATION ADMINISTRATIVE ORDERS FOR THE FIRE |
| PROTECTION PLAN |
| |
| "Indian Point #2 Station |
| |
| "High Pressure Fire Header Impairment |
| |
| "Fire Impairment and Surveillance per Station Administration Order 703. |
| |
| "NRC event # 37683. The high pressure Fire Water Protection System is |
| degraded due to planned maintenance work. The inner and outer high-pressure |
| fire headers are split to provide protection for work on the valves for 12 |
| Fire Main Booster Pump. 12 Fire main booster pump is inoperable during this |
| tag-out. The diesel fire pump is in service as the alternate fire protection |
| for the outside fire header. 11 and 12 fire maintenance pumps are supplying |
| the inside header with 11 Fire Main Booster Pump available as a back up. |
| SAO-703 states one fire main booster pump out of service is a 7-day action |
| statement to return it to operable status. The headers being separated or |
| any part of the fire protection piping or valves not being able to perform |
| its function other than the specific instances described in SAO-703 requires |
| an alternate fire protection system shall be established. This was |
| established within 24 hours to ensure compliance with SAO-703 as described |
| above. A special report shall be submitted to the NRC Regional Administrator |
| of the Region 1 Office outlining this event within 14 Days." |
| |
| The licensee informed the NRC resident inspector. |
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