Event Notification Report for January 25, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/24/2001 - 01/25/2001 ** EVENT NUMBERS ** 37682 37683 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37682 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 01/24/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 07:36[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 01/23/2001| +------------------------------------------------+EVENT TIME: 07:25[EST]| | NRC NOTIFIED BY: ABRAMSKI |LAST UPDATE DATE: 01/24/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |STEVEN DENNIS R1 | |10 CFR SECTION: | | |*INB 50.72(b)(3)(v)(B) POT RHR INOP | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION SYSTEM DECLARED INOPERABLE. | | | | The flow controller for the High Pressure Coolant Injection (HPCI) system is | | indicating approximately 1400 gpm with the HPCI system in the standby | | condition. Because the cause of this condition is not known at this time, | | the HPCI system is considered inoperable. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37683 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 01/24/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 12:20[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 01/24/2001| +------------------------------------------------+EVENT TIME: 03:30[EST]| | NRC NOTIFIED BY: KEVIN DONNELLY |LAST UPDATE DATE: 01/24/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVEN DENNIS R1 | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 86 Power Operation |86 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HR REPORT REQUIRED BY STATION ADMINISTRATIVE ORDERS FOR THE FIRE | | PROTECTION PLAN | | | | "Indian Point #2 Station | | | | "High Pressure Fire Header Impairment | | | | "Fire Impairment and Surveillance per Station Administration Order 703. | | | | "NRC event # 37683. The high pressure Fire Water Protection System is | | degraded due to planned maintenance work. The inner and outer high-pressure | | fire headers are split to provide protection for work on the valves for 12 | | Fire Main Booster Pump. 12 Fire main booster pump is inoperable during this | | tag-out. The diesel fire pump is in service as the alternate fire protection | | for the outside fire header. 11 and 12 fire maintenance pumps are supplying | | the inside header with 11 Fire Main Booster Pump available as a back up. | | SAO-703 states one fire main booster pump out of service is a 7-day action | | statement to return it to operable status. The headers being separated or | | any part of the fire protection piping or valves not being able to perform | | its function other than the specific instances described in SAO-703 requires | | an alternate fire protection system shall be established. This was | | established within 24 hours to ensure compliance with SAO-703 as described | | above. A special report shall be submitted to the NRC Regional Administrator | | of the Region 1 Office outlining this event within 14 Days." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021