Event Notification Report for January 23, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/22/2001 - 01/23/2001 ** EVENT NUMBERS ** 37636 37674 37675 37676 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37636 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 12/27/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 18:03[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 12/27/2000| +------------------------------------------------+EVENT TIME: 13:30[CST]| | NRC NOTIFIED BY: JEFFREY EASLEY |LAST UPDATE DATE: 01/22/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE CORE INJECTION (HPCI) SYSTEM DISCOVERED INOPERABLE | | | | "On 12/27/00 at 1330 hours QCOS 2300-09 (U-1 HPCI Vent Verification) was in | | progress following QCOS 2300-11 (CCST/Torus Level Switch Functional | | Testing). During the process of vent verification of the U-1 HPCI system, | | the vent valves were open approximately 6.5 minutes prior to receiving water | | through the vent lines; the U-1 HPCI system was found inoperable. | | Performance acceptance criteria of QCOS 2300-09 states that venting times | | >40 seconds could he construed as a preconditioning action per NRC IN 97-16 | | and as such the U-1 HPCI system possibly could not have performed its' | | safety function prior to the venting that took place on 12/27/00 at 1330. | | The last successful vent of the U-1 HPCI system was completed on 11/30/00. | | An investigation is underway to try to determine the time of the loss of | | fill and the cause. This 4-hour ENS notification is being made in accordance | | with 10 CFR 50.72(b)(2)(iii)(D)." | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE 2052EST ON 1/22/01 FROM MIKE MacLENNAN TO S. SANDIN * * * | | | | The licensee is retracting this report based on the following: | | | | "This is a retraction of the ENS call made on 12/27/00, event #37636, | | concerning the inoperability of the Unit One HPCI system due to an | | inadequate fill and vent of the pump discharge line. | | | | "We have completed our evaluation and have determined that HPCI would have | | successfully injected coolant to the reactor if the system was initiated in | | response to a LOCA." | | | | The licensee informed the NRC resident inspector. Notified R3DO(Creed). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37674 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WATERBURY HOSPITAL |NOTIFICATION DATE: 01/22/2001| |LICENSEE: WATERBURY HOSPITAL |NOTIFICATION TIME: 16:22[EST]| | CITY: WATERBURY REGION: 1 |EVENT DATE: 01/18/2001| | COUNTY: STATE: CT |EVENT TIME: 16:00[EST]| |LICENSE#: 06-02406-01 AGREEMENT: N |LAST UPDATE DATE: 01/22/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |STEVEN DENNIS R1 | | |ERIC LEEDS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: GERALD RANDALL | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TREATMENT INVOLVING I-131 TO PREGNANT FEMALE | | | | In August of 2000, a female patient received 12.15 millicuries I-131 as | | prescribed for hyperthyroidism. The patient when questioned did not | | disclose that she was pregnant at the time. The licensee in discussion with | | Region I (Shanbaky) on 1/19 was requested to make a voluntary notification | | with a written followup report. | | | | Hoo Note: Region I issued PNO-I-01-002 to address this report. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37675 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 01/22/2001| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 16:35[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/22/2001| +------------------------------------------------+EVENT TIME: 14:05[EST]| | NRC NOTIFIED BY: LEE JOHNSON |LAST UPDATE DATE: 01/22/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |96 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 COMMENCED A UNIT SHUTDOWN FOLLOWING A FAILURE OF ROD POSITION | | INDICATION DURING SURVEILLANCE TESTING | | | | During control rod exercise surveillance testing, shutdown bank "C" | | indication failed to respond to rod motion. Tech Sec 3/4.1.3.1 action b was | | entered which requires that the unit be placed in mode 3 (Hot Standby) | | within 6 hours. The licensee commenced a shutdown and anticipates having | | Unit 2 offline by 1900 hours. The licensee informed the NRC resident | | inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37676 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 01/23/2001| | UNIT: [1] [] [] STATE: VA |NOTIFICATION TIME: 02:24[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/23/2001| +------------------------------------------------+EVENT TIME: 01:46[EST]| | NRC NOTIFIED BY: JOHN VOISSEM |LAST UPDATE DATE: 01/23/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |RUDOLPH BERNHARD R2 | |10 CFR SECTION: |JOHN HANNON NRR | |AAEC |JOSEPH GIITTER IRO | | |BELCHER FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED ON LOSS OF ALL ANNUCIATORS FOR GREATER THAN 15 | | MINUTES | | | | The licensee was conducting daily light checks of annuciators when they did | | not clear when the test signal was reset. The declaration of Unusual Event | | was made at 0146 EST in accordance with the Emergency Action Level procedure | | and entry was also made into the abnormal procedure for the loss of | | annuciators. | | | | The plant computer was still available for alarm monitoring and 2 operators | | were placed at the control panels for close monitoring of plant conditions. | | The plant was maintained at stable conditions. The watch stations outside | | of the control room were augmented to provide additional monitoring of | | outside control panel alarms which would not be received in the control | | room. Electricians and Instrumentation Technicians have started | | investigating the problem. | | | | The licensee notified the NRC Resident Inspector and the state and local | | authorities. | | | | * * * UPDATED AT 0242 EST ON O1/23/01 BY JOHN VOISSEM TO FANGIE JONES * * * | | | | | | The Unusual Event was terminated at 0237 EST. The alarm lights cleared on | | their own and subsequent test of alarm function was satisfactory. | | Additional personnel are in transit to the site to conduct further testing. | | | | The licensee will notify the NRC Resident Inspector as well as state and | | local authorities. Notified the R2DO (Rudolph Bernhard), NRR EO ( John | | Hannon), IRO Manager (Joseph Giitter), and FEMA (Belcher). | +------------------------------------------------------------------------------+
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