Event Notification Report for January 18, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/17/2001 - 01/18/2001 ** EVENT NUMBERS ** 37647 37658 37664 37665 37666 37667 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37647 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 01/05/2001| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 06:38[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 01/05/2001| +------------------------------------------------+EVENT TIME: 06:20[EST]| | NRC NOTIFIED BY: SCHORK |LAST UPDATE DATE: 01/17/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE MOTOR FOR MS-V-1C HAS BEEN DECLARED INOPERABLE | | | | TMI identified a condition that is outside the design basis of the facility | | at 0620 hours on January 5, 2001. The condition is that MS-V-1C may not be | | capable of being closed within 120 seconds as described in the bases for | | Technical Specification 4.8.2 and FSAR Section 10.3. The bases for TS 4.8.2 | | and FSAR Section 10.3 both state that the valve is capable of being remotely | | closed within 120 seconds from the Control Room. With the motor inoperable, | | the valve cannot be remotely closed within 120 seconds. The condition was | | found during routine surveillance testing and subsequent evaluation. During | | the surveillance testing the valve is stroke closed 10% and then returned to | | its normal operation position of full open. The valve stroke closed to the | | 10% closed position without incident. During the return of the valve to the | | full open position sparks were observed and a burning odor was present. | | However, the sparking ceased and the motor successfully traveled to the fail | | open position (verified by visual observation of the valve stern position). | | Subsequent visual inspection of the valve and motor, interviews with the | | technicians, the system engineer and the Electrical Foreman resulted in the | | declaration of the inoperability of the motor for MS-V-1C. | | | | This deficient condition has been documented in the TMI Corrective Action | | program. Troubleshooting of the motor for MS-V-1C is in progress. Interim | | action has been taken to provide for the expeditious manual closure of the | | valve and those actions are contained in an approved plant procedure. | | | | The Resident Inspector will be informed. | | | | * * * RETRACTION ON 01/17/01 AT 1729ET BY J. SCHORK TAKEN BY MACKINNON * * | | * | | | | | | Based on additional information gathered during trouble shooting and repair | | of MS-V-IC conducted on January 5, 2001, subsequent to the submittal of the | | immediate notification, it was determined that there is reasonable assurance | | that MS-V-IC would have performed its intended safety function to remotely | | close from the control room when demanded. Therefore, no condition outside | | the design basis for the facility existed and the immediate report made on | | January 5, 2001 is being withdrawn. The basis for the reasonable assurance | | that the valve would have performed its intended safety function is | | described below. | | | | During the partial stroke surveillance test, the spark and burn smell | | occurred very briefly while the valve was traveling open. The sparking | | immediately stopped and the valve continued to travel uninterrupted until it | | was full open. The surveillance was completed satisfactorily. | | | | The breaker for the valve motor did not trip and no fuses were blown. Power | | remained available to stroke the valve after the event. Based on the short | | duration of the spark and the fact that the motor continued to operate, | | there was no reason to believe the stroke time would have changed. | | | | Prior to opening or disturbing the motor terminal box, the breaker was | | manually opened and the resistance from each phase to ground was checked | | from the breaker. A high voltage Meggar was used to perform the test. The | | Meggar results showed that neither the power cables, termination, nor motor | | windings were grounded. This indicated that the motor and cables were in | | working condition. | | | | The motor terminal box was opened without disturbing the power cables inside | | the box. There was clear evidence that a bare point on one of the ring lug | | terminations had made contact with the aluminum terminal box. A small | | portion of a ring connector was bare. There was a burn mark on the ring | | connector and on the terminal box. A small piece of the aluminum terminal | | box was missing at the point where the lug would have contacted the box. | | The as-found gap between what were the contact points was approximately | | 0.25". Based on this evidence, it was clear that a sharp corner of the | | ring lug had rubbed against the terminal box until it wore through the | | insulating tape that was wrapped around the lug. The metal lug then | | contacted the aluminum terminal box, which temporarily shorted the phase to | | ground. The resulting spark knocked off a small piece of the terminal box at | | the contact point creating a gap that immediately cleared the short. The | | duration of the short was not long enough to cause the breaker to open. | | | | Based on the above, there is reasonable certainty that the component would | | have performed its function when commanded. Therefore, from a past | | operability perspective, the component was always capable of performing its | | design basis function. When the component was declared out of service, the | | plant entered a maintenance evolution to determine and correct the cause of | | the spark. Entering the maintenance evolution to trouble shoot and correct | | the cause of the spark was not a condition prohibited by the Technical | | Specifications. There is no time clock associated with removing the remote | | closing capability from service for maintenance. | | NRC Region 1 RDO (Barkley) notified. | | | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37658 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 01/09/2001| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 13:08[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/09/2001| +------------------------------------------------+EVENT TIME: 12:20[EST]| | NRC NOTIFIED BY: ROBERT KIDDER |LAST UPDATE DATE: 01/17/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: |ED GOODWIN NRR | |KSNM 70.52(a) LOSS OF SNM/CRIT |FRITZ STURZ NMSS | |KFIS 70.52(b) LOSS OF SNM/FISSILE |JOSEPH GIITTER IRO | |DDDD 73.71 UNSPECIFIED PARAGRAPH |ROBERT SKELTON IAT | | |JOHN DAVIDSON IAT | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 87 Power Operation |87 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NEUTRON MONITORING DETECTOR MISSING FROM SHIPMENT | | | | The licensee reported that one local power range monitor (LPRM) detector was | | missing out of a shipment from GE Reuter-Stokes in Twinsburg, OH. The | | missing detector contains 0.00027g of U-235 (0.00121g total U) in the form | | of solid uranium oxide. The licensee has contacted the vendor to determine | | whether an error occurred in preparation of the shipping papers. The NRC | | resident inspector will be informed of this event by the licensee. | | | | * * * UPDATE 1529 FROM KIDDER TAKEN BY STRANSKY * * * | | | | At 1355, the licensee was informed that the missing LPRM detector is | | currently located at the GE Reuter-Stokes facility and had not been shipped. | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Jacobson). | | | | * * * RETRACTION 1015 01/17/2001 FROM RUSSELL TAKEN BY STRANSKY * * * | | | | "Investigation by the licensee and the manufacturer discovered that the LPRM | | had been maintained in a secure, locked area at GE Reuter-Stokes and had | | been kept under appropriate controls. Accordingly, no reporting criterion is | | applicable to this event under 10CFR50.72 or 10CFR70.52. Additionally, the | | SNM is not of sufficient quantity that 10CFR73.71(a)(1) or 10CFR20.2201 | | apply. | | | | "Event Notification 37658 is therefore retracted." | | | | The NRC resident inspector has been informed of this retraction by the | | licensee. Notified R3DO (Lanksbury). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37664 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 01/17/2001| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 07:47[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 01/16/2001| +------------------------------------------------+EVENT TIME: [EST]| | NRC NOTIFIED BY: J. MILL |LAST UPDATE DATE: 01/17/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY REPORT | | | | A contract manager tested positive for illegal drug use. The individual's | | site access privileges have been terminated. The licensee will contact the | | NRC resident inspector regarding this report. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37665 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 01/17/2001| | UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 11:43[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 01/11/2001| +------------------------------------------------+EVENT TIME: 11:00[EST]| | NRC NOTIFIED BY: GAMBRELL |LAST UPDATE DATE: 01/17/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 18 Power Operation |18 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DURING A SMALL BREAK LOSS OF COOLANT ACCIDENT PEAK CLADDING TEMPERATURES | | COULD EXCEED 2200 DEGREES F. | | | | B&W Owners Group Preliminary Safety Concern (PSC) was written on July 28, | | 2000 to document a concern with RELAPS analyses of Core Flood Tank (CFT) | | line break LOCAs. The issue involves the impact of a 2 minute delay in | | tripping reactor coolant pumps (RCPs). In the event of a small break loss | | of cooling accident involving the core flood line, peak cladding | | temperatures could exceed 2200 degrees F. However, this issue does not | | impact Oconee during normal operation since Oconee has three high pressure | | injection (HPI) pumps. The Oconee design basis includes starting a second | | HPI pump within 10 minutes, which would prevent excessive peak clad | | temperatures. | | | | On January 17, 2001, at 1100 hours, preliminary analyses revealed that plant | | conditions, allowed by Oconee Technical Specifications 3.5.2.B and 3.5.2.C | | may necessitate either reducing reactor power to approximately 50% (versus | | 75%) or tripping RCPs within 1 minute versus 2 minutes of loss of subcooling | | margin to maintain clad temperatures less than 2200 degrees F. In these | | specific plant conditions, the single failure of the second HPI pump or | | failure of an HPI train would prevent starting a second HPI pump and | | injecting within 10 minutes. | | | | This is being conservatively reported as a condition that alone could | | prevent the fulfillment of a safety function. This condition is only a | | concern during extended operation with one HPI pump or train out of service. | | Procedural guidance in place requires turning off the RCPs as an immediate | | manual action in response to loss of subcooling margin. Operators in | | training typically secure the RCPs well within 1 minute of loss of | | subcooling margin during unannounced casualty scenarios. Operators are | | evaluated on the time critical action of securing the ROPs within two | | minutes; however, the time critical action of securing the RCPs within 1 | | minute has not yet been validated using our appropriate processes. | | Therefore, as an interim measure, Oconee intends to reduce thermal power to | | <50% rated thermal power (RTP) instead of <75% RTP whenever TS 3.5.2.B or | | 3.5.2.0 is entered. This action ensures that the acceptance criteria of | | 10CFR50.46 are satisfied. | | | | The NRC Resident Inspector was notified. | | Problems encountered during the event: None. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37666 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 01/17/2001| |LICENSEE: UNKNOWN |NOTIFICATION TIME: 16:20[EST]| | CITY: SAN ANTONIO REGION: 4 |EVENT DATE: 12/20/2000| | COUNTY: STATE: TX |EVENT TIME: 12:00[CST]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 01/17/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KRISS KENNEDY R4 | | |DON COOL, EO NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN JR. | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST HUMBOLDT 5001EX NUCLEAR GAUGE | | | | This is an initial notification of a lost nuclear gauge. The gauge was lost | | on December 20, 2000, while being transported in an unsecured manner and not | | in it's transport case. The gauge was a one month old Humboldt 5001EX. The | | gauge was probably lost along Highway 90 and 36th Street in San Antonio, | | Texas. A Police Report was filed (Report # 00805997/01). The operator | | performed an extensive search for the gauge along the highway. A notice was | | posted in the San Antonio Express News with a reward offered. The gauge has | | not been recovered to date. Investigation is on going. | | | | Further details will be sent as they are received at the Texas Department of | | Health. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37667 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 01/17/2001| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 19:12[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/17/2001| +------------------------------------------------+EVENT TIME: 16:20[EST]| | NRC NOTIFIED BY: DON BRADLEY |LAST UPDATE DATE: 01/17/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TURBINE TRIP/REACTOR TRIP DURING TURBINE CONTROL TESTING. | | | | Reactor Trip due to Turbine Generator trip greater than 69% power. All rods | | fully inserted into the core. Feedwater isolation due to reactor trip with | | Tave less than 564 degrees F (this is a design feature and was expected). | | Both Motor Driven Auxiliary Feedwater pumps automatically started as | | expected due to the Feedwater Isolation. As far as the licensee knew at the | | time of the call no Primary or Secondary PORVs or Code Safety Valves opened. | | All Emergency Core Cooling Systems and the Emergency Diesel Generators are | | fully operable. "1A" Nuclear Service Water pump is out of service for | | planned maintenance (currently being returned to service) and the "1A" | | Auxiliary Building Ventilation is also inoperable for planned maintenance. | | | | Currently the cause of the turbine trip is unknown. Turbine Control Testing | | was in progress at the time of the trip. | | | | The licensee will notify North & South Carolina and surrounding counties of | | the reactor trip. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021