The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for January 16, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           01/12/2001 - 01/16/2001

                              ** EVENT NUMBERS **

37554  37626  37660  37661  37662  37663  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37554       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PILGRIM                  REGION:  1  |NOTIFICATION DATE: 11/28/2000|
|    UNIT:  [1] [] []                 STATE:  MA |NOTIFICATION TIME: 16:50[EST]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        11/28/2000|
+------------------------------------------------+EVENT TIME:        15:13[EST]|
| NRC NOTIFIED BY:  BOB COOLIDGE                 |LAST UPDATE DATE:  01/12/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |ANIELLO DELLA GRECA  R1      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HIGH PRESSURE COOLANT INJECTION (HPCI) DECLARED INOPERABLE DUE TO            |
| INSTRUMENTATION FAILURE                                                      |
|                                                                              |
| "The HPCI System was taken out of service for surveillance testing earlier   |
| in the day.  The surveillance's were completed and HPCI was placed back in   |
| service in standby lineup.  At this time, the high flow isolation            |
| instrumentation was found to be reading well beyond the limits of the normal |
| in service band (+10 to -10).  At that time, HPCI was removed from service   |
| (availability) and isolated.  The proper LCO was entered and troubleshooting |
| is underway."                                                                |
|                                                                              |
| The licensee informed the NRC resident inspector.                            |
|                                                                              |
| * * * UPDATE 1415EST ON 1/12/01 FROM OLSON TO MacKINNON * * *                |
|                                                                              |
| The licensee is retracting this report based on the following:               |
|                                                                              |
| "This is a retraction of event no. 37554 made on November 28, 2000 at 1651   |
| in accordance with 10CFR50.72(b)(2)(iii)(D).                                 |
|                                                                              |
| "An Engineer had noted a flow switch that provides a high steam flow to the  |
| HPCI system reading -17 inches of water while the other indicated -2 inches  |
| of water.  The Primary Containment Isolation capability of the HPCI          |
| isolation valves was declared inoperable and the valves de-energized in the  |
| isolated condition.  HPCI was declared inoperable and a 14 day cold shutdown |
| LCO entered.  Subsequent testing of the differential pressure switches found |
| the trip setpoints to be correct.  The face plate had not been 'zeroed'      |
| during previous calibration.  This had no effect on switch operation,        |
| therefore could not have prevented fulfillment of safety function."          |
|                                                                              |
| The licensee informed the NRC resident inspector.  Notified R1DO(Lew).       |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37626       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: GINNA                    REGION:  1  |NOTIFICATION DATE: 12/20/2000|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 22:25[EST]|
|   RXTYPE: [1] W-2-LP                           |EVENT DATE:        12/20/2000|
+------------------------------------------------+EVENT TIME:        20:14[EST]|
| NRC NOTIFIED BY:  ROBERT McCOY                 |LAST UPDATE DATE:  01/12/2001|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |ANTHONY DIMITRIADIS  R1      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC CONTROL ROOM VENTILATION SYSTEM SHIFT FROM NORMAL TO EMERGENCY     |
| RECIRCULATION MODE WHILE A PLANNED GAS DECAY TANK RELEASE WAS IN PROGRESS    |
|                                                                              |
| The following text is a portion of a facsimile received from the licensee:   |
|                                                                              |
| "At 2014, with a gas decay tank release in progress (total activity 0.215    |
| Ci, (Kr-85 = 0.214 Ci, Xe-133 = 0.001 Ci)), control room ventilation gas     |
| monitor R-36 went into alarm causing ventilation to shift to mode F.  During |
| the [2-second] spike, R-36 counts went from 30 cpm to 856 cpm and back to 30 |
| cpm.  Local air samples taken by the RP Tech both in the control room and in |
| the area of the control room ventilation intake revealed no activity."       |
|                                                                              |
| The licensee stated that the gas decay tank release was planned and that the |
| counts going through the plant stack were considered normal.  (These counts  |
| peaked at 120 cpm.)  The licensee stated that the planned gas decay tank     |
| release was within both the expected and required release limits.  The wind  |
| was blowing in a favorable direction, and the stability class for            |
| meteorological conditions was stable.  Although counts have returned to      |
| normal, the licensee plans to leave control room ventilation in the          |
| emergency recirculation mode until tomorrow morning.                         |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
|                                                                              |
| * * * UPDATE ON 1/12/01 @ 1113 BY GOMEZ TO GOULD * * *  RETRACTION           |
|                                                                              |
| Rochester Gas and Electric (RG&E) is retracting this notification. This      |
| event was originally thought to be in response to a valid radiological       |
| condition because a waste gas decay tank release was in progress at the same |
| time as this event.  RG&E has confirmed that the alarm on Control Room Noble |
| Gas radiation monitor                                                        |
| R-36 that occurred at 20:14 EST on December 20, 2000, causing the shift in   |
| Control Room ventilation to "Mode F" (emergency recirculation mode), was the |
| result of a spurious spike on R-36.  The alarm was not in response to any    |
| radiation condition,                                                         |
|                                                                              |
| Local samples taken by radiation protection technicians on December 20, both |
| in the Control Room and in the area of the Control Room ventilation intake,  |
| revealed no activity.  The Plant Process Computer (PPCS) plots show that     |
| R-36 counts were steady just before and immediately after the spike.         |
| Further engineering evaluation of this event has determined that the alarm   |
| on R-36 was caused by a sudden spike and was not in response to any          |
| radiation condition. Therefore, this event is not reportable and is          |
| retracted.                                                                   |
|                                                                              |
| Other occurrences of spiking on R-36 took place during December 2000 and     |
| January 2001.  Some of these spikes resulted in alarms on R-36 and           |
| subsequent shift in Control Room ventilation to "Mode F".  These alarms were |
| recognized at the time of alarm as invalid actuations of the HVAC System for |
| the Control Room, and did not result in NRC notification.  Trouble-shooting  |
| and corrective maintenance is on-going on the R-36 monitor.                  |
|                                                                              |
| The licensee has notified the NRC Resident Inspector.                        |
|                                                                              |
| The Region 1 RDO (Lew) was notified.                                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37660       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: WATTS BAR                REGION:  2  |NOTIFICATION DATE: 01/12/2001|
|    UNIT:  [1] [] []                 STATE:  TN |NOTIFICATION TIME: 13:36[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        01/12/2001|
+------------------------------------------------+EVENT TIME:        10:30[EST]|
| NRC NOTIFIED BY:  TERRY KNUETTEL               |LAST UPDATE DATE:  01/12/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES R. OGLE      R2      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AN ACTING SUPERVISOR TESTED POSITIVE FOR AN ILLEGAL DRUG DURING A RANDOM     |
| TEST                                                                         |
|                                                                              |
| A non-licensed employee was determined to be under the influence of          |
| marijuana during a random test.  The employee's access to the plant has been |
| terminated.  Contact the Headquarters Operations Officer for additional      |
| details.                                                                     |
|                                                                              |
| The licensee will inform the NRC resident inspector.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37661       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CALLAWAY                 REGION:  4  |NOTIFICATION DATE: 01/12/2001|
|    UNIT:  [1] [] []                 STATE:  MO |NOTIFICATION TIME: 13:40[EST]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        01/12/2001|
+------------------------------------------------+EVENT TIME:        09:28[CST]|
| NRC NOTIFIED BY:  R BARTON                     |LAST UPDATE DATE:  01/12/2001|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DALE POWERS          R4      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| INVALID ACTUATION OF AN ENGINEERED SAFETY FEATURE SYSTEM                     |
|                                                                              |
| During performance of "A" Train Trip Actuations Device Operational Test a    |
| reactor protection signal was generated when a procedure step was            |
| inadvertently skipped.  At the time this occurred the "A" reactor trip       |
| bypass breaker was closed when the trip signal was generated.  This caused   |
| the "A" reactor trip breaker to open.  The reactor did not trip because the  |
| "A" bypass breaker was closed.                                               |
|                                                                              |
| This event resulted in an invalid actuation of an Engineered Safety Feature  |
| system.  It was concluded that this event was reportable per                 |
| 10CFR50.72(b)(2)(ii)  since:                                                 |
| (1) This actuation was not anticipated to occur as part of this pre-planned  |
| evolution since the trip signal was expected to be inhibited by the omitted  |
| procedure step and                                                           |
| (2) The omitted step resulted in the system not being properly removed from  |
| service as required by the surveillance procedure (source range trip signal  |
| not being bypassed or inhibited).                                            |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37662       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TENNESSEE DIV OF RAD HEALTH          |NOTIFICATION DATE: 01/12/2001|
|LICENSEE:  AEROJET ORDNANCE TENNESSEE, INC.     |NOTIFICATION TIME: 15:33[EST]|
|    CITY:  JONESBOROUGH             REGION:  2  |EVENT DATE:        01/11/2001|
|  COUNTY:                            STATE:  TN |EVENT TIME:        11:30[EST]|
|LICENSE#:  S-90009               AGREEMENT:  Y  |LAST UPDATE DATE:  01/12/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES R. OGLE      R2      |
|                                                |JOSEPH HOLONICH      NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DEBRA SHULTZ (via fax)       |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT INVOLVING FIRE IN AN INCINERATOR AIR EFFLUENT         |
| CLEANING SYSTEM                                                              |
|                                                                              |
| "Event description: The licensee called to report a fire in their            |
| incinerator's air effluent cleaning system. The fire in the baghouse lasted  |
| approximately two hours. The building was evacuated, and onsite personnel    |
| extinguished the fire. The baghouse filter has not yet been opened to assess |
| the damage. The area is secured and no routine operations are ongoing at     |
| this time. Smears taken in the area were maximum of 100-dpm/100 sq. cm.      |
| Clean up of the area has not begun. The total release from this event is     |
| estimated to be 0.013 microcuries of depleted uranium. Sample results will   |
| be available soon.                                                           |
|                                                                              |
| "These events do not pose a threat to public health and safety but may be    |
| reportable under 1200-2-5-.141(2)c.(4).                                      |
|                                                                              |
|                                                                              |
| "Media attention: None"                                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37663       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  ABB POWER DISTRIBUTION               |NOTIFICATION DATE: 01/15/2001|
|LICENSEE:  ABB POWER DISTRIBUTION               |NOTIFICATION TIME: 16:33[EST]|
|    CITY:  Florence                 REGION:  2  |EVENT DATE:        01/15/2001|
|  COUNTY:                            STATE:  SC |EVENT TIME:        15:20[EST]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  01/15/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES R. OGLE      R2      |
|                                                |RICHARD BARKLEY      R1      |
+------------------------------------------------+JOHN JACOBSON        R3      |
| NRC NOTIFIED BY:  DARALL  HARRIS               |DALE POWERS          R4      |
|  HQ OPS OFFICER:  JOHN MacKINNON               |VERN HODGE           NRR     |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|CCCC 21.21               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| POTENTIAL DEFECT PER 10 CFR PART 21 CONTROL DEVICE FOR HK AND K-LINE CIRCUIT |
| BREAKERS                                                                     |
|                                                                              |
|                                                                              |
| In December 1998, Sequoyah Nuclear Plant (Chattanooga, TN) experienced a     |
| failure to close of a 7.5HK500/1200 Medium Voltage circuit breaker (Serial   |
| Number 48672-A101-1-3B) manufactured 3/30/1973. The cause of the breaker     |
| failure as determined by TVA was a failure of the Control Device (Part       |
| Number 191921T06). Specifically, a movable contact within the Control Device |
| was found to have a broken spring retainer, which is a protuberance holding  |
| the return spring in place on the contact. This broken spring retainer       |
| allowed the spring to move out of its intended position, causing failure of  |
| the control contacts to make and break properly. This occurrence was         |
| documented and evaluated by the Tennessee Valley Authority Central           |
| Laboratories & Field Testing Service in their Technical Report #99-0550 on   |
| 11 February 1999.                                                            |
|                                                                              |
| On February 29, 2000, Catawba Nuclear Station (York, SC) experienced a       |
| failure to close of a 5HK250/1200 Medium Voltage circuit breaker (Serial     |
| Number 50465F-1 -10186) manufactured 3/28/1979. The cause of the breaker     |
| failure as determined by Duke Power and ABB Florence was similar to the      |
| failure reported by TVA in 1998. Material analysis of the failed movable     |
| contact concluded that the material for the contact was correct to that      |
| specified. A dissected profile analysis of the failed contact revealed that  |
| the material at the base of the spring retainer on the movable contact was   |
| thin and failed due to fatigue. This failure was documented and evaluated by |
| Duke Engineering Testing and Laboratory Services in their Metallurgical      |
| Analysis Report #2624 on 29 March 2000.                                      |
|                                                                              |
| On October 30, 2000, during a routine inspection of a Control Device on a    |
| 7.5HK500/1200 Medium Voltage circuit breaker (Serial Number 50464L-2-07210)  |
| manufactured 2/29/1979, Catawba Nuclear Station found a movable contact that |
| had failed in a similar manner as the other two previously reported. This    |
| failure was documented and evaluated by Duke Engineering Testing and         |
| Laboratory Services in their Metallurgical Analysis Report #2726 on 01       |
| November 2000.                                                               |
|                                                                              |
| The cause of these three failures was fatigue of the metal at the base of    |
| the spring retainer on the movable contacts, due to insufficient metal mass  |
| at the base of the retainer. The spring retainer on the contact is formed    |
| with a die by punching the movable contact from the opposite side of the     |
| electrical contact mounting location during fabrication. The height of the   |
| spring retainer, therefore, determines the amount of material left at the    |
| base.                                                                        |
|                                                                              |
| Corrective action for this incident has been taken. After further            |
| investigation, ABB Florence has determined that the height of the spring     |
| retainer was changed in September 1979 to a lower specification, leaving     |
| more material at the base of the spring retainer. The movable contact formed |
| with the greater spring retainer height specification prior to 1979 has a    |
| small possibility of failure as discussed above. There have been no other    |
| reports of movable contact failures.                                         |
|                                                                              |
| There have been only these three reports of this movable contact failure     |
| since the control device was introduced to the market in 1960. Since its     |
| introduction, more than 22,000 control devices have been produced for both   |
| HK and K-line type circuit breakers, each with 5 movable contacts. ABB       |
| therefore believes this problem is not significant enough to require         |
| immediate action from users. However, we recommend that control devices      |
| older than 1981 be replaced with new control devices on both HK and K-line   |
| breakers at the next scheduled maintenance of the breaker.                   |
|                                                                              |
| ABB will notify all customers who purchased this product.                    |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021