Event Notification Report for January 8, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/05/2001 - 01/08/2001 ** EVENT NUMBERS ** 37637 37646 37647 37648 37649 37650 37651 37652 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37637 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 12/28/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 12:21[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 12/28/2000| +------------------------------------------------+EVENT TIME: 07:41[CST]| | NRC NOTIFIED BY: STEVE WHEELER |LAST UPDATE DATE: 01/05/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL BUILDING VENTILATION ISOLATION | | | | "At 0741 CST the Control Building Emergency Filtration System automatically | | initiated on a Control Building Intake Gas High Activity alarm. The cause of | | the Gas High Activity alarm is under investigation." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * UPDATE ON 12/29/00, 0024 ET BY MYERS TAKEN BY MACKINNON * * * | | | | During the day, trouble shooting was performed to determine the source of | | the actuation at 0741 CST today. Surveillance Procedure 6.PRM.317, CONTROL | | ROOM AIR SAMPLING SYSTEM ELECTRONIC CALIBRATION, was performed, and all | | indications were within specification. A source check of the gaseous | | channel was also performed per Instrument Operating Procedure 4.17, and the | | response of the monitor was normal. Air sampling was conducted, and no | | indications of abnormal radiation were identified. The Control Room | | Emergency Filtration System was returned to the standby lineup. | | | | At 1933, the Control Room Emergency Filtration System again initiated on a | | high gaseous activity signal. All equipment functioned as required. The | | Control Building Ventilation Radiation Monitor has been declared inoperable, | | and the Control Room Emergency Filtration System remains in service, aligned | | in the accident mode. | | | | The NRC Resident Inspector was notified. | | | | Note: The Control Building Ventilation Radiation Monitor consists of three | | channels, with two required to be operable. The Iodine channel is also | | presently inoperable. The actuation logic requires only one channel of the | | three to initiate Control Room Isolation and start the Emergency Booster | | (pressurization) fan. | | | | Noble gas sample was taken at 2142 CST. All readings were normal. NRC | | R4DO (C. Marschall) notified. | | | | * * * UPDATE ON 1/5/01 @ 1113 BY VAN DER KAMP TO GOULD * * * RETRACTION | | | | Event Number 37637 reported a condition at Cooper Nuclear Station (CNS) | | where the Control Room Emergency Filtration System (CREPS) automatically | | initiated on a Control Building Intake Gas High Activity alarm. Surveillance | | testing found no abnormalities with the system and air sampling found no | | indications of abnormal radiation levels. A subsequent identical event | | occurred later the same day and was reported to the NRC Operations Center in | | an update. | | | | Subsequent troubleshooting has found a solder connection, that connects gas | | monitor components to ground, had come apart. Discussions with the | | manufacturer of the monitor confirm that the loss of ground can cause | | spiking in the displayed background reading. | | | | CNS investigation has found that the initiation of the CREPS was due to an | | invalid signal, i.e., not due to an actual elevated radioactive | | concentration. Per 10CFR50.72(b)(2)(ii), invalid actuations of CREFS are | | not required to be reported and EN 37637 is retracted. | | | | The NRC Resident Inspector will be notified of this event by the licensee. | | | | The Reg 4 RDO(Johnson) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37646 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: HOLTEC INTERNATIONAL |NOTIFICATION DATE: 01/04/2001| |LICENSEE: HOLTEC INTERNATIONAL |NOTIFICATION TIME: 15:59[EST]| | CITY: MARLTON REGION: 1 |EVENT DATE: 10/18/2000| | COUNTY: STATE: NJ |EVENT TIME: 12:00[EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 01/05/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MELVYN LEACH R3 | | |VERN HODGE, FAX NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: BRIAN GUTHERMAN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 NOTIFICATION FOR DISCREPANT WEIGHT OF SPENT FUEL RACKS | | | | Spent fuel racks removed from Byron Nuclear Power Plant were discovered to | | have as-found weights ranging from approximately 8,200 to 10,500 lbs more | | than the weights used in the analyses supporting the original design and | | licensing of these racks and in the design of the lifting equipment used to | | lift the racks. The analyses related to seismic loadings, bearing pad | | design, spent fuel pool liner fatigue, and possibly others used to design | | and license these racks may no longer be conservative when the additional | | weight is considered. The actual impact on these analyses has not, to our | | knowledge, been evaluated. The impact on the design of the lifting | | equipment is that the design safety factors for the lifting equipment, while | | still above 1.0, may not meet the minimum safety factors in NUREG-0612 and | | associated reference documents. | | | | Braidwood Nuclear Station has four similarly designed racks provided by the | | same supplier. | | | | | | * * * UPDATE ON 1/5/01 @ 0946 BY GUTHERMAN TO GOULD * * * | | | | The manufacturer of the spent fuel racks reported in the initial reports was | | Joseph Oat Co of Camden, NJ. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37647 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 01/05/2001| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 06:38[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 01/05/2001| +------------------------------------------------+EVENT TIME: 06:20[EST]| | NRC NOTIFIED BY: SCHORK |LAST UPDATE DATE: 01/05/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE MOTOR FOR MS-V-1C HAS BEEN DECLARED INOPERABLE | | | | TMI identified a condition that is outside the design basis of the facility | | at 0620 hours on January 5, 2001. The condition is that MS-V-1C may not be | | capable of being closed within 120 seconds as described in the bases for | | Technical Specification 4.8.2 and FSAR Section 10.3. The bases for TS 4.8.2 | | and FSAR Section 10.3 both state that the valve is capable of being remotely | | closed within 120 seconds from the Control Room. With the motor inoperable, | | the valve cannot be remotely closed within 120 seconds. The condition was | | found during routine surveillance testing and subsequent evaluation. During | | the surveillance testing the valve is stroke closed 10% and then returned to | | its normal operation position of full open. The valve stroke closed to the | | 10% closed position without incident. During the return of the valve to the | | full open position sparks were observed and a burning odor was present. | | However, the sparking ceased and the motor successfully traveled to the fail | | open position (verified by visual observation of the valve stern position). | | Subsequent visual inspection of the valve and motor, interviews with the | | technicians, the system engineer and the Electrical Foreman resulted in the | | declaration of the inoperability of the motor for MS-V-1C. | | | | This deficient condition has been documented in the TMI Corrective Action | | program. Troubleshooting of the motor for MS-V-1C is in progress. Interim | | action has been taken to provide for the expeditious manual closure of the | | valve and those actions are contained in an approved plant procedure. | | | | The Resident Inspector will be informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37648 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COLORADO DEPARTMENT OF HEALTH |NOTIFICATION DATE: 01/05/2001| |LICENSEE: SAN LUIS VALLEY REGIONAL MED CENTER |NOTIFICATION TIME: 10:02[EST]| | CITY: ALAMOSA REGION: 4 |EVENT DATE: 01/05/2001| | COUNTY: STATE: CO |EVENT TIME: 08:00[MST]| |LICENSE#: 14202 AGREEMENT: Y |LAST UPDATE DATE: 01/05/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JOHNSON R4 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PENTECOST | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - MOLYBDENUM-99/TECHNETIUM-99m GENERATOR LOST WHILE | | IN SHIPMENT | | | | DUPONT PHARMACEUTICALS SHIPPED A 750 MILLICURIE MOLYBDENUM/TECHNETIUM | | GENERATOR VIA FEDEX TO THE SAN LUIS VALLEY REGIONAL MEDICAL CENTER IN | | ALAMOSA, CO ON 12/28/00. AS OF THIS DATE THE SHIPMENT HAS NOT BEEN | | RECEIVED. THERE WAS NO FEDEX TRACKING NUMBER AND DUPONT COULD NOT GIVE THE | | STATE ANY INFORMATION BECAUSE THEIR COMPUTERS WERE DOWN. | | | | * * * UPDATE ON 1/5/01 @ 1037 BY PENTECOST TO GOULD * * * | | | | THE GENERATOR WAS LOCATED @ 0830MST AT THE FEDEX DENVER FACILITY AND IT IS | | IN TRANSIT TO THE MEDICAL FACILITY. | | | | NOTIFIED REG 4 RDO(JOHNSON) AND NMSS(SMITH) WERE NOTIFIED | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37649 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 01/05/2001| |LICENSEE: PACIFIC SOILS ENGINEERING |NOTIFICATION TIME: 11:22[EST]| | CITY: OCEANSIDE REGION: 4 |EVENT DATE: 01/02/2001| | COUNTY: STATE: CA |EVENT TIME: [PST]| |LICENSE#: 3142 AGREEMENT: Y |LAST UPDATE DATE: 01/05/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JOHNSON R4 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: GREGER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN NUCLEAR MOISTURE DENSITY GAUGE | | | | The licensee reported that a Campbell Pacific Nuclear moisture density gauge | | was stolen from a storage unit in Oceanside, Ca between 1530 on 12/29/00 and | | noon on 12/30/00. Model # of the gauge was MC-3 and its serial # is | | M380504284. The gauge contained approximately 8 millicuries of cesium-137 | | and 40 millicuries of americium/beryllium. The licensee will offer a | | reward. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37650 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 01/05/2001| | UNIT: [1] [] [] STATE: AR |NOTIFICATION TIME: 12:25[EST]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 01/05/2001| +------------------------------------------------+EVENT TIME: 08:48[CST]| | NRC NOTIFIED BY: JAMES PORTER |LAST UPDATE DATE: 01/05/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR MANUALLY TRIPPED FROM 80% POWER LEVEL DUE TO EXCESSIVE MAIN TURBINE | | GENERATOR HYDROGEN LEAK. | | | | "At 0848 CT on 01/05/01 ANO Unit 1 reactor was manually tripped due to | | excessive hydrogen leakage on the main turbine generator. Reactor power was | | reduced from 100% to 80% prior to the manual reactor trip. No ESF actuations | | occurred following the trip. The unit is currently stable at Hot Shutdown | | conditions." | | | | Hydrogen leak on the main turbine generator was first noticed around 2100 | | hours CT on 01/04/01. Normal hydrogen pressure in the main turbine | | generator is 70 psi. The licensee stated that they were losing | | approximately 3 psi per hour. The licensee evacuated the Turbine Building | | as a precaution. After reactor power had been reduced to 80% power the | | hydrogen leak increased at which point the licensee manually tripped the | | reactor. All rods fully inserted into the core. Once Through Steam | | Generator atmospheric valves operated properly. The licensee stated that | | they have a 0.17 gallon per day primary leak to secondary system leak. All | | Emergency Core Cooling Systems and the Emergency Generators are fully | | operable if needed. Once Through Steam Generator water levels are being | | maintained using main feedwater, one main feedwater pump operating. At the | | time of the notification the licensee had not located the source of the | | hydrogen leak. | | | | The licensee notified Arkansas Department of Health. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE ON 01/05/01 AT 1734 ET BY REX KNIGHT TAKEN BY MACKINNON * * * | | | | When the reactor was tripped, discharge canal temperature dropped from 52 | | degrees F to 37 degrees F. This caused a large number of Thread Fin Shad to | | die. A member of the public called the Arkansas Game and Fish (AG&F) | | Commission about the Shad. ANO has contacted the AG&F Commission and | | explained the situation. A Press Release is not planned at this time. NRC | | R4DO (Bill Johnson) notified. | | | | The NRC Resident Inspector was notified of the event update by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37651 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 01/06/2001| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 20:50[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 01/06/2001| +------------------------------------------------+EVENT TIME: 18:30[CST]| | NRC NOTIFIED BY: LES ANDERSON |LAST UPDATE DATE: 01/06/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |MELVYN LEACH R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |90 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | COURTESY CALL TO THE NATIONAL RESPONSE CENTER (NRC) MADE AFTER SPILLING | | APPROXIMATELY 25 GALLONS OF SULFURIC ACID. | | | | A courtesy call was made to the National Response Center that was made to | | report a sulfuric acid spill at the plant water treatment area. The | | Corporate Environmental and Regulatory Affairs Department, which the | | licensee calls ERAD, was notified. ERAD, in turn, notified the Minnesota | | State Pollution Control Agency. The Minnesota State Pollution Control | | Agency suggested a courtesy call to the National Response Center. | | | | Approximately 25 gallons of sulfuric acid was spilled (reportable quantity | | is 65 gallons of greater). A small amount, less than 10 gallons, of acid | | drained to their Turbine Building Sump of which a very small amount may have | | been released. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37652 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 01/07/2001| | UNIT: [] [2] [3] STATE: CT |NOTIFICATION TIME: 09:50[EST]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 01/07/2001| +------------------------------------------------+EVENT TIME: 06:00[EST]| | NRC NOTIFIED BY: ROBERT SMITH |LAST UPDATE DATE: 01/07/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 90 Power Operation |90 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT | | | | Safeguard system degradation related to area boundary. Immediate | | compensatory measures taken upon discovery. The licensee notified the NRC | | Resident Inspector. | | | | Refer to HOO Log for additional details. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021