Event Notification Report for December 26, 2000
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
12/22/2000 - 12/26/2000
** EVENT NUMBERS **
37630 37631 37632
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|Power Reactor |Event Number: 37630 |
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| FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 12/22/2000|
| UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 11:29[EST]|
| RXTYPE: [1] W-4-LP |EVENT DATE: 12/22/2000|
+------------------------------------------------+EVENT TIME: 09:45[CST]|
| NRC NOTIFIED BY: RICK HUBBARD |LAST UPDATE DATE: 12/22/2000|
| HQ OPS OFFICER: DOUG WEAVER +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |BILL JONES R4 |
|10 CFR SECTION: | |
|AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
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EVENT TEXT
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| LOSS OF POWER TO THE TECHNICAL SUPPORT CENTER (TSC) |
| |
| Breaker 13-40 tripped with the ground flag dropped. This breaker supplies |
| primary power to the TSC. There is a backup diesel generator available to |
| supply power to the TSC but will not be energized until it is determined |
| that there is no ground at the TSC. Once the TSC D/G is energized the |
| facility will once again be available. |
| |
| The licensee notified the NRC resident inspector. |
| |
| * * * Update at 1150 on 12/22/00 by Hubbard received by Weaver * * * |
| |
| The diesel generator is now supplying the TSC with electrical power (as of |
| 1041 CST). Investigation continues into why breaker 13-40 tripped. |
| |
| Notified the R4DO(Jones). |
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!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
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|Power Reactor |Event Number: 37631 |
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| FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 12/22/2000|
| UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 16:54[EST]|
| RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 12/22/2000|
+------------------------------------------------+EVENT TIME: 12:25[CST]|
| NRC NOTIFIED BY: NACOSTE |LAST UPDATE DATE: 12/23/2000|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |MIKE ERNSTES R2 |
|10 CFR SECTION: | |
|AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | |
|NLCO TECH SPEC LCO A/S | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
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EVENT TEXT
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| PLANT ENTERED 14 DAY LCO DUE TO HIGH PRESSURE COOLANT INJECTION BEING |
| INOPERABLE |
| |
| HPCI was declared inoperable after failing testing. During the performance |
| of 2-SI-3.5.1.7 HPCI MAIN AND BOOSTER PUMP SET DEVELOPED HEAD AND FLOW RATE |
| TEST AT RATED REACTOR PRESSURE, the HPCI system could not be verified to be |
| vented. |
| |
| The probable reason for not being able to make this verification is due to a |
| faulty flow gauge in the HPCI piping system. |
| |
| The NRC Resident Inspector will be notified. |
| |
| * * * RETRACTED AT 0240 EST 0N 12/23/00 BY MICKEY HUNTER TO FANGIE JONES * * |
| * |
| |
| "The 4 hour report made in accordance with 10CFR50.72.b.2.iii at 1630 on |
| 12/22/2000 is being retracted for the following reasons: During the |
| performance of 2-SR-3.5.1.7 HPCI MAIN AND BOOSTER PUMP SET DEVELOPED HEAD |
| AND FLOW RATE TEST AT RATED REACTOR PRESSURE, there were indications of flow |
| through the vent line during initial Surveillance testing however; the test |
| methodology used in the Surveillance could not verify that flow. We revised |
| the Surveillance methodology to prescribe an alternate process of |
| determining flow. The Surveillance test was reperformed satisfactorily and |
| verified indications of flow that was observed in the previous performance |
| of the Surveillance test. Thus this proved operability of HPCI during |
| previous performance of Surveillance test." |
| |
| The licensee notified the NRC Resident Inspector. The R2DO (Mike Ernstses) |
| was notified. |
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+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 37632 |
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| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 12/23/2000|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 15:02[EST]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 12/23/2000|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 06:15[CST]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 12/23/2000|
| CITY: PADUCAH REGION: 3 +-----------------------------+
| COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION |
|LICENSE#: GDP-1 AGREEMENT: Y |THOMAS KOZAK R3 |
| DOCKET: 0707001 |JOHN HICKEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: BEASLEY | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| FACILITY HAS PROBLEMS WITH FREEZING STANDPIPES THAT SUPPLY WATER TO THEIR |
| HIGH PRESSURE FIRE WATER SYSTEMS. |
| |
| During a discussion between the Paducah and Portsmouth Plant Shift |
| Superintendents (PSS), the Portsmouth PSS stated that their facility was |
| having a problem with the standpipes freezing that supply water to their |
| High Pressure Fire Water (HPFW) systems. Following this discussion, the |
| Paducah PSS instructed all building managers containing HPFW systems to |
| check the temperatures of the standpipes. Following this temperature |
| survey, two systems in the C-337 building were discovered to have abnormally |
| low temperatures. In order to verify operability, Fire Services personnel |
| performed flow tests on these two systems. During this testing, it was |
| discovered that the standpipe for HPFW system D-2 was frozen, and the system |
| could not perform its specified safety function. The High Pressure Fire |
| Water System is required to be operable according to TSR 2.4.4.5. HPFW |
| system D-2 was declared inoperable at 0615 on 12-23-00, and a fire patrol |
| was initiated as required by the TSR. During follow up investigation, it |
| was discovered that six of the eight exhaust fans and a section of |
| recirculating louvers that supply heat to this area were not functioning. |
| |
| |
| The NRC Resident Inspector has been notified of this event. |
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