Event Notification Report for December 21, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/20/2000 - 12/21/2000 ** EVENT NUMBERS ** 37597 37621 37622 37623 37624 37625 37626 37627 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37597 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 12/14/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 18:33[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/14/2000| +------------------------------------------------+EVENT TIME: 06:00[CST]| | NRC NOTIFIED BY: DAVID BRAGLIA |LAST UPDATE DATE: 12/20/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OVERPOWER CONDITION DUE TO FEED TEMPERATURE CALCULATION ERROR | | | | "Braidwood Station Operating License condition 2.C.1 restricts licensed | | thermal power level to 3411 MW thermal. From December 13, 2000 at 0410 to | | December 14, 2000 at 0600, Braidwood Unit 2 was operated at a power level of | | 100.55 percent in violation of this license condition. | | | | "On December 14, 2000 at 0600 the station Thermal Performance Engineer | | discovered that Feedwater inlet temperature was not being calculated | | correctly by the plant process computer. Following a transfer of computer | | room ventilation trains on December 12, 2000 at 1800 feedwater calculated | | temperatures were 3�F higher than actual feedwater temperatures. This | | resulted in the process computer calorimetric reading 0.6% low. Reactor | | power was adjusted using this incorrect calculation resulting in the | | overpower condition. | | | | "Following identification of the error, Unit load was reduced to ensure that | | reactor power was less than 100%. Nuclear instrumentation was verified to be | | indicating less than 100%. No adjustment to the nuclear instrumentation was | | performed using the incorrect calculation. | | | | "This is being reported pursuant to License Condition 2.g, which requires | | notification within 24 hours of the violation of any condition in section | | 2.c of the Operating License." | | | | The licensee notified the NRC Resident Inspector. | | | | ***** UPDATE AT 1539 CST ON 12/20/00 FROM JIM ROYSTON TO LEIGH TROCINE | | ***** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "The initial report to the NRC (Event #37597) was based upon an observation | | of a 3�F increase in the indicated Feedwater temperature (a primary input to | | the Calorimetric calculation) following a Computer room temperature change | | initiated by a swap of the ventilation system. An increase of 3�F in | | Feedwater temperature results in a 0.55% reduction in Calorimetric power. A | | declining Calorimetric indication results in Operator action to increase and | | maintain that indication at 100%. Because of this, the initial indication | | was that the Unit was inadvertently increased to 100.55%." | | | | "Upon execution of troubleshooting it was discovered that the temperature | | measurement problem was caused by miss-wired RTD temperature elements, which | | are used to compensate thermocouples for their cold reference junction | | temperature. From this data, a correction to the temperature measurements | | was performed such that the true Feedwater temperatures were determined | | during the event. After applying this correction, it was determined that | | prior to the event the unit was operating at 99.488%. Following the event, | | at the highest power level period, the unit was operating at 99.935%. This | | data also confirms the conclusion that Unit 2 did not exceed 100% power. As | | an additional check, Calorimetric calculations were performed independently | | of those executed on the Plant Process Computer which indicate that no | | problems exist." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R3DO (Kozak). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37621 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 12/20/2000| | UNIT: [] [2] [] STATE: WI |NOTIFICATION TIME: 06:31[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 12/20/2000| +------------------------------------------------+EVENT TIME: 04:17[CST]| | NRC NOTIFIED BY: RANDY HASTINGS |LAST UPDATE DATE: 12/20/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS KOZAK R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 63 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP CAUSED BY TRANSFORMER GROUND | | | | The apparent cause of the reactor trip was a turbine trip caused by a ground | | overcurrent relay actuation on the 2X01 transformer (main power out | | transformer). Heat removal is via the steam dumps to the main condenser | | with main feedwater supplying the steam generators. All systems operated as | | required. The licensee is investigating the cause of the ground | | indication. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37622 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HADDAM NECK REGION: 1 |NOTIFICATION DATE: 12/20/2000| | UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 11:37[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 12/20/2000| +------------------------------------------------+EVENT TIME: 10:35[EST]| | NRC NOTIFIED BY: CHARLES REID |LAST UPDATE DATE: 12/20/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANTHONY DIMITRIADIS R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO STATE DEP DUE TO OIL SPILL ON SITE | | | | The licensee notified the Connecticut Department of Environmental Protection | | (DEP) about an oil spill due to operator error. The waste oil separator was | | in operation filling a 55-gallon drum when the operator overflowed the drum. | | The spill was contained on the concrete pad, there was no release offsite or | | to the water. Cleanup is now in progress. | | | | The licensee notified NRC Region 1 (John Wray). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37623 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SOUTHEAST MO STATE UNIVERSITY |NOTIFICATION DATE: 12/20/2000| |LICENSEE: SOUTHEAST MO STATE UNIVERSITY |NOTIFICATION TIME: 13:52[EST]| | CITY: CAPE GIRARDEAU REGION: 3 |EVENT DATE: 12/19/2000| | COUNTY: CAPE GIRARDEAU STATE: MO |EVENT TIME: 13:30[CST]| |LICENSE#: 24-09296-02 AGREEMENT: N |LAST UPDATE DATE: 12/20/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS KOZAK R3 | | |CHERYL TROTTIER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHRIS McGOWLAN | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST STRONTIUM-90 SOURCE | | | | The school has lost a 20 mCi Sr-90 sealed source. It is unknown how long it | | has been missing. A search of physical areas and records have been | | unsuccessful in locating the source. As long as the source remains sealed | | it presents little of no threat to the public. | | | | The source was used as part of an ionization cell for an ion capture | | detector. The equipment was sold sometime back at auction. The paperwork | | for the equipment does not indicate that the source was included in the | | sale. | | | | The school has been in contact with NRC Region 3 (Kevin Null). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37624 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 12/20/2000| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 18:01[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/20/2000| +------------------------------------------------+EVENT TIME: 08:55[EST]| | NRC NOTIFIED BY: DEAN BRUCK |LAST UPDATE DATE: 12/20/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS KOZAK R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 0 Startup |2 Startup | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS-FOR-DUTY REPORT REGARDING A NON-LICENSED SUPERVISOR'S RANDOM | | POSITIVE TEST FOR ALCOHOL | | | | A non-licensed supervisor tested positive for alcohol during a random test. | | This was a first time positive test for this individual. The individual was | | removed from site, and the individual's badge was placed on administrative | | hold. | | | | The licensee made this 24-hour event notification in accordance with 10 CFR | | 26.73(a)(2)(iv). | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37625 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 12/20/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 19:04[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 12/20/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:05[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 12/20/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |THOMAS KOZAK R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC G. WALKER | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 RESPONSE (24-HOUR REPORT) - LOSS OF ONE CONTROL IN THE | | DOUBLE CONTINGENCY | | | | The following text is a portion of a facsimile received from the Paducah | | personnel: | | | | "The C-331 E and F surge drum room temperature was found to be at 103 | | degrees F in violation of NCSA.CAS-005. Requirement 3.2.6 of this NCSA | | states that when the surge drums contain UF6, they shall be operated at a | | minimum temperature of 105 degrees F. This temperature requirement prevents | | hydrogen fluoride (HF) from condensing at the maximum pressure rating of the | | drums. Should HF condense it could moderate any UF6 that might be | | present." | | | | "SAFETY SIGNIFICANCE OF EVENTS:" | | | | "HF cannot condense at 103 degrees F and 20 psia. The drum pressures were | | all less than 1 psia; therefore, it was not possible to condense HF." | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR:" | | | | "In order for a criticality to be possible, HF would have to condense. | | Therefore, the temperature of the drums would have to be less than 80 | | degrees F, and the drum pressures would have to exceed 20 psia." | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.):" | | | | "[Since the double] contingency is based on two controls on moderation and | | [since] the temperature control was lost, double contingency was not | | maintained." | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITICAL MASS):" | | | | "The surge drums contain an estimated 1425 pounds of UF6 at less than 1 | | weight % U235 assay." | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES:" | | | | "The first leg of double contingency is an administrative control, which | | limits the surge drum room temperature to a minimum of 105 degrees F. The | | control was violated, and the first leg of double contingency was lost." | | | | "The second leg of double contingency is an administrative control to | | maintain the drum pressures below 20 psia, which is the maximum rated | | pressure for the drums. This control was not violated, and this leg of | | double contingency was maintained." | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS | | IMPLEMENTED:" | | | | "Temperature loss was due to low outside ambient temperature. Building | | temperature was raised and surge drum room temperature rose above minimum | | required temperature. Additional heating for the area is being | | considered." | | | | Paducah personnel notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37626 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 12/20/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 22:25[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 12/20/2000| +------------------------------------------------+EVENT TIME: 20:14[EST]| | NRC NOTIFIED BY: ROBERT McCOY |LAST UPDATE DATE: 12/20/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANTHONY DIMITRIADIS R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC CONTROL ROOM VENTILATION SYSTEM SHIFT FROM NORMAL TO EMERGENCY | | RECIRCULATION MODE WHILE A PLANNED GAS DECAY TANK RELEASE WAS IN PROGRESS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 2014, with a gas decay tank release in progress (total activity 0.215 | | Ci, (Kr-85 = 0.214 Ci, Xe-133 = 0.001 Ci)), control room ventilation gas | | monitor R-36 went into alarm causing ventilation to shift to mode F. During | | the [2-second] spike, R-36 counts went from 30 cpm to 856 cpm and back to 30 | | cpm. Local air samples taken by the RP Tech both in the control room and in | | the area of the control room ventilation intake revealed no activity." | | | | The licensee stated that the gas decay tank release was planned and that the | | counts going through the plant stack were considered normal. (These counts | | peaked at 120 cpm.) The licensee stated that the planned gas decay tank | | release was within both the expected and required release limits. The wind | | was blowing in a favorable direction, and the stability class for | | meteorological conditions was stable. Although counts have returned to | | normal, the licensee plans to leave control room ventilation in the | | emergency recirculation mode until tomorrow morning. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37627 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 12/20/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 22:58[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 12/20/2000| +------------------------------------------------+EVENT TIME: 20:08[EST]| | NRC NOTIFIED BY: REINSBURROW |LAST UPDATE DATE: 12/20/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF A REACTOR CORE ISOLATION COOLING (RCIC) BYPASS TO CONDENSATE | | STORAGE TANK VALVE TO FULLY STROKE DURING STROKE TIME TESTING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "EVENT: At 2008 on 12/20/00 during performance of OPT-10.1.8 (RCIC System | | Valve Operability Test), the 2-E51-F022 (RCIC bypass to condensate storage | | tank) failed to fully stroke during stroke timing of the valve. A valve | | thermal overload annunciator was received. This rendered the Brunswick Unit | | 2 RCIC system inoperable. RCIC was not in operation at the time of this | | failure." | | | | "INITIAL SAFETY SIGNIFICANCE EVALUATION: Minimal safety significance. | | Remaining ECCS systems are operable." | | | | "CORRECTIVE ACTION(S): Determine the cause of the 2-E51-F022 valve failure. | | Return the Unit 2 RCIC system to operable following repair of 2-E51-F022." | | | | The licensee stated that this event did not result in any radiological | | release or reactor coolant leaks. The licensee also stated that all systems | | functioned as required and that there was nothing unusual or misunderstood. | | This event placed the unit in a 14-day technical specification limiting | | condition for operation. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021