Event Notification Report for December 15, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/14/2000 - 12/15/2000 ** EVENT NUMBERS ** 37552 37594 37595 37596 37597 37598 37599 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37552 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 11/26/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 06:13[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 11/26/2000| +------------------------------------------------+EVENT TIME: 01:54[CST]| | NRC NOTIFIED BY: WILLIAM GREEN |LAST UPDATE DATE: 12/14/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GAIL GOOD R4 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF LOOSE SERVICE WATER PUMP FOUNDATION BOLTS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 0154 [CST] on 11/26/00, a station operator noticed that 2 foundation | | bolts on service water pump (SWP) C were loose and 3 foundation bolts on | | [SWP] D were loose. Both service water loops were declared inoperable, and | | [limiting condition for operation (LCO)] 3.7.2, condition A, was entered | | twice and condition B once. This required placing the plant in Mode 3 | | within 12 hours and Mode 4 within 36 hours. Personnel were called to the | | site, and all foundation bolts on all 4 [SWPs] were torqued. No loose bolts | | were found on SWP A, 4 loose bolts were found on SWP B, and 5 loose bolts | | were found on SWPs C [and] D. An operability determination was written to | | justify operability of the service water system, and all LCOs were exited at | | 0428 [CST]. Engineering [personnel are] evaluation the condition." | | | | The licensee notified the NRC resident inspector. | | | | * * * RETRACTED AT 1244 EST ON 12/14/00 BY STEVEN JOBE TO FANGIE JONES * * | | * | | | | "Subsequent evaluation has determined that all Service Water Pumps were | | operable at all times and this event is not reportable under either 10 CFR | | 50.72(b)(2)(iii)(B) or 10 CFR 50.72(b)(2)(iii)(D). | | | | "Engineering evaluation has determined that a Service Water Pump is operable | | with one or more pedestal nuts (foundation bolts) having less than | | installation torque provided a minimum finger tight torque exists. That | | justification is based on evaluation of loading stress and the impact of not | | having a preload stress applied to the nut. The determination is that the | | finger tight nut is an acceptable condition for pump operability. This | | evaluation has considered the effects of various loading conditions | | including seismic, barge impact and normal operational loads." | | | | The licensee has notified the NRC Resident Inspector. The R4DO (Chuck Cain) | | has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37594 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 12/14/2000| | UNIT: [] [2] [] STATE: WI |NOTIFICATION TIME: 08:40[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 12/14/2000| +------------------------------------------------+EVENT TIME: 06:30[CST]| | NRC NOTIFIED BY: R. HASTINGS |LAST UPDATE DATE: 12/14/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 0 Startup |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO A BLOWN CONTROL POWER FUSE ON AN INTERMEDIATE | | RANGE NEUTRON DETECTOR | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[The Unit 2] reactor automatically tripped at 0630 [CST] due to a blown | | control power fuse on intermediate range neutron detector 2N35. Reactor | | power at the time of the trip was in the source range [10E+4] cps, well | | below the actual intermediate range trip setpoint. [Unit 2] is exiting a | | refueling outage, the reactor was made critical at 0543 [CST]. | | Troubleshooting is in progress. The heat removal mechanism is steam dump | | discharge from the steam generator atmospheric relief valves. There are no | | known steam generator tube leaks." | | | | The licensee stated that auxiliary feedwater was supplying water to the | | steam generators both before and after the trip. The unit is currently | | stable in Mode 3. Pressurizer heaters and sprays, normal charging and | | letdown, and the reactor coolant pumps are being utilized for primary system | | pressure, inventory, and transport control. Containment parameters are | | normal, and offsite power is available. There were no engineered safety | | actuations or emergency core cooling system actuations, and none were | | required. The licensee stated that all systems functioned as required and | | that there was nothing unusual or misunderstood. There were no related | | maintenance activities ongoing at the time if the trip. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37595 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 12/14/2000| | UNIT: [] [2] [] STATE: AR |NOTIFICATION TIME: 14:15[EST]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 12/14/2000| +------------------------------------------------+EVENT TIME: 11:50[CST]| | NRC NOTIFIED BY: LARRY McLERRAN |LAST UPDATE DATE: 12/14/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHUCK CAIN R4 | |10 CFR SECTION: |FEMA,DOE,DOA FAX | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |HHS,EPA,DOT FAX | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 60 Power Operation |60 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO THE U.S. COAST GUARD ABOUT A FUEL OIL SPILL | | | | The licensee notified the U.S. Coast Guard of a spill of less than 5 gallons | | of diesel fuel oil released to the discharge canal. Absorbent booms are | | deployed across the discharge canal and in the storm drain discharge to the | | canal. | | | | The licensee notified the NRC Resident Inspector and will notify the state | | of Arkansas. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37596 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 12/14/2000| | UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 18:02[EST]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 12/14/2000| +------------------------------------------------+EVENT TIME: 17:15[EST]| | NRC NOTIFIED BY: DAVID DVORAK |LAST UPDATE DATE: 12/14/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LOCATION OF 2 FUEL PINS IN THE SPENT FUEL POOL IS UNKNOWN | | | | "As part of the ongoing decommissioning of Millstone Unit 1, a detailed | | documentation of the fuel currently in the Unit 1 spent fuel pool is | | underway. A detailed verification of spent fuel pool content records was | | part of this effort. During this process, workers identified a discrepancy | | in the paperwork relating to the location of two spent fuel pins that were | | removed from a fuel assembly in October 1972. A search is underway; however, | | these fuel pins have not yet been located among the 2,884 fuel assemblies | | containing more than 140,000 fuel pins currently in the spent fuel pool. In | | addition, workers are also searching pertinent records. | | | | "Due to the radiation levels of the fuel pins, if they were removed from the | | spent fuel pool, the use of a shielded cask would have been required and the | | shipment could have only been made to a licensed facility. Any other | | movement of these pins from the site would have been immediately detected by | | the site radiation monitoring system. Therefore, there is a high degree of | | confidence that these pins are not in an unrestricted area and are under the | | control of a licensed facility; either here in the spent fuel pool or | | possibly at a licensed radioactive waste disposal site. As a result, we are | | also confident that no overexposure of workers or members of the public has | | resulted. An independent team with relevant expertise is on-site to assist | | in an ongoing investigation to determine the location of the 2 fuel pins." | | | | The licensee notified NRC Region 1 (Todd Jackson) and the state of | | Connecticut. The licensee intends notifying the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37597 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 12/14/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 18:33[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/14/2000| +------------------------------------------------+EVENT TIME: 06:00[CST]| | NRC NOTIFIED BY: DAVID BRAGLIA |LAST UPDATE DATE: 12/14/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OVERPOWER CONDITION DUE TO FEED TEMPERATURE CALCULATION ERROR | | | | "Braidwood Station Operating License condition 2.C.1 restricts licensed | | thermal power level to 3411 MW thermal. From December 13, 2000 at 0410 to | | December 14, 2000 at 0600, Braidwood Unit 2 was operated at a power level of | | 100.55 percent in violation of this license condition. | | | | "On December 14, 2000 at 0600 the station Thermal Performance Engineer | | discovered that Feedwater inlet temperature was not being calculated | | correctly by the plant process computer. Following a transfer of computer | | room ventilation trains on December 12, 2000 at 1800 feedwater calculated | | temperatures were 3 degF higher than actual feedwater temperatures. This | | resulted in the process computer calorimetric reading 0.6% low. Reactor | | power was adjusted using this incorrect calculation resulting in the | | overpower condition. | | | | "Following identification of the error, Unit load was reduced to ensure that | | reactor power was less than 100%. Nuclear instrumentation was verified to be | | indicating less than 100%. No adjustment to the nuclear instrumentation was | | performed using the incorrect calculation. | | | | "This is being reported pursuant to License Condition 2.g, which requires | | notification within 24 hours of the violation of any condition in section | | 2.c of the Operating License." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37598 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: DRIESENGA & ASSOCIATES, INC. |NOTIFICATION DATE: 12/14/2000| |LICENSEE: DRIESENGA & ASSOCIATES, INC. |NOTIFICATION TIME: 21:28[EST]| | CITY: WYOMING REGION: 3 |EVENT DATE: 12/14/2000| | COUNTY: STATE: MI |EVENT TIME: 08:00[EST]| |LICENSE#: 21-26634-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE BURGESS R3 | | |JOHN GREEVES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DANIEL DRIESENGA | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TROXLER GAUGE STOLEN AND RECOVERED | | | | A model 3440 Troxler moisture/density gauge was stolen from a company truck | | by cutting the chain restraining it. The theft occurred about 0800 on | | 12/14/00 in Wyoming , MI. The gauge contains <10 mCi Cs-137 and <50 mCi | | Am-241. A report was filed with the Wyoming Police Department, who also | | recovered the gauge. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37599 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WNP-2 REGION: 4 |NOTIFICATION DATE: 12/15/2000| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 03:53[EST]| | RXTYPE: [2] GE-5 |EVENT DATE: 12/14/2000| +------------------------------------------------+EVENT TIME: 21:30[PST]| | NRC NOTIFIED BY: ARTHUR J. MOORE |LAST UPDATE DATE: 12/15/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHUCK CAIN R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ISOLATION OF A CONTAINMENT INSTRUMENT AIR HEADER FROM ITS NORMAL SUPPLY AND | | ACTUATION OF THE ASSOCIATED BACKUP NITROGEN BOTTLE BANK PROGRAMMER | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 2130 PST, the plant experienced an isolation of the 'B' Containment | | Instrument Air (CIA) header from its normal supply and actuation of the | | associated backup nitrogen bottle bank programmer. The isolation and | | actuation were due to an actual system low pressure caused by performance of | | a maintenance procedure in conjunction with a failed heater in the | | non-safety related normal Containment Nitrogen (CN) system." | | | | "The CIA system supplies nitrogen to provide motive force for safety-related | | valves inside the primary containment. The valves are reactor pressure | | vessel Safety Relief Valves (SRVs) and inboard Main Steam Isolation Valves | | (MSIVs)." | | | | "Evaluation of computer information indicates that pressure on the 'A' CIA | | header may have been below the administrative allowable value for the | | associated pressure switch. Investigation continues as to why the isolation | | and [actuation] involved only the 'B' train." | | | | "The plant is stable, and there were no other abnormal occurrences in | | conjunction with this event." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021