Event Notification Report for December 11, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/08/2000 - 12/11/2000 ** EVENT NUMBERS ** 37579 37580 37581 37582 37583 37584 37585 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37579 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 12/08/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 08:05[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/08/2000| +------------------------------------------------+EVENT TIME: 06:30[EST]| | NRC NOTIFIED BY: STEVE SAUER |LAST UPDATE DATE: 12/08/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EXPERIENCED A REACTOR TRIP/TURBINE TRIP DUE TO LOW-LOW STEAM | | GENERATOR WATER LEVEL | | | | "Unit 1 reactor and turbine trip, first out annunciator was '13' steam | | generator low-low level. Preliminary indications are that a feedwater | | isolation signal was generated, although actual conditions were not present. | | This resulted in the feed reg and its bypass valves closing, resulting in | | the low-low level. All aux feedwater pumps started on the level signal and | | maintained steam generator water inventory. The plant is currently in mode | | 3 (hot standby) at normal operating temperature and pressure." | | | | All control rods fully inserted. The main condenser is in service removing | | decay heat via the bypass valves. There were no maintenance activities | | ongoing which could have resulted in the trip. All systems functioned as | | required. The licensee will inform local agencies and has informed the NRC | | resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37580 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 12/08/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 12:07[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 12/08/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 11:15[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 12/08/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MICHAEL PARKER R3 | | DOCKET: 0707002 |PAUL FREDRICKSON R2 | +------------------------------------------------+BRIAN SMITH NMSS | | NRC NOTIFIED BY: DALE NOEL |CHARLES MILLER IRO | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAAA 20.1906(d) SURFACE CONT/ EXT RAD | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF SURFACE RADIATION READINGS IN EXCESS OF TRANSPORTATION LIMITS | | ON 3 OF 30 CYLINDERS SHIPPED FROM WESTINGHOUSE ELECTRIC COMPANY IN COLUMBIA, | | SOUTH CAROLINA | | | | At 1115 hours on 12/08/00, USEC Portsmouth health physics personnel | | determined that an inbound shipment of empty, 2.5-ton, healed cylinders had | | external radiation levels in excess of the limits in 10CFR71.47. The | | shipment involved 30, empty, 2.5-ton, healed cylinders from Westinghouse | | Electric Company in Columbia, South Carolina; and surveys showed that three | | rear cylinders had radiation readings of 225 to 250 millirem per hour on | | contact. This exceeds the 10CFR71.47 limit of 200 millirem per hour and | | meets the 1-hour reporting criteria of 10CFR20.1906(d)(1). | | | | The truck will be properly dispositioned on the plant site. Portsmouth | | personnel are in the process of making notifications to Westinghouse | | Electric Company (the shipper) and Hitman Transport Company (the carrier). | | There was nothing unusual or misunderstood, and all systems functioned as | | required. | | | | Portsmouth personnel notified the NRC resident inspector and plan to notify | | the Department of Energy. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37581 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TRU-TEC SERVICES, INC. |NOTIFICATION DATE: 12/08/2000| |LICENSEE: TRU-TEC SERVICES, INC. |NOTIFICATION TIME: 18:47[EST]| | CITY: LA PORTE REGION: 4 |EVENT DATE: 12/08/2000| | COUNTY: HARRIS STATE: TX |EVENT TIME: 03:30[CST]| |LICENSE#: 07-28386-01 AGREEMENT: Y |LAST UPDATE DATE: 12/08/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BLAIR SPITZBERG R4 | | |PAUL FREDRICKSON R2 | +------------------------------------------------+THOMAS ESSIG NMSS | | NRC NOTIFIED BY: NORMAN LANIER |CHARLES MILLER IRO | | HQ OPS OFFICER: LEIGH TROCINE |JOHN ROGGE R1 | +------------------------------------------------+STAMBAUGH DOE | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | |NTRA TRANSPORTATION EVENT | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RECEIPT OF A TRU-TEC SERVICES, INC., CONTAINER OF BROMINE-82 THAT APPEARED | | TO HAVE BEEN OPENED AND RE-PACKAGED INCORRECTLY DURING TRANSPORT BETWEEN | | TEXAS A&M AND ST. CROIX IN THE VIRGIN ISLANDS | | | | On 12/04/00, Tru-Tec Services, Inc., shipped an empty container from their | | facility in La Porte, Texas, to Texas A&M via Acme Trucking. The container | | was similar in shape to a propane tank (but taller). It was lead filled and | | weighed between 700 and 750 pounds. It also had a 3-inch by 3-inch cavity | | inside and a lid with a T-bar to hold the lid in place. Texas A&M loaded | | the empty container with bromine-82, and the activity of the bromine-82 at | | noon on 12/04/00 was 900 millicuries. The bromine-82 was double | | encapsulated (inside three glass ampoules which were also inside a metal | | swagelock container with a screw on cap). After Texas A&M loaded the | | container, Acme Trucking transported the container to Federal Express at | | Intercontinental Airport in Houston, Texas, on 12/04/00. Apparently, the | | container arrived at a Federal Express hub in Memphis, Tennessee, on | | 12/05/00, and it remained there until 12/07/00. On 12/07/00, the shipment | | left Memphis, Tennessee, via Federal Express and arrived in Puerto Rico on | | the morning of 12/08/00. It was then transported by 4 Star Air Cargo to St. | | Croix in the Virgin Islands. Tru-Tec Services, Inc., received the container | | between approximately 1600 and 1630 EST on 12/08/00. | | | | Upon arrival in St. Croix, Tru-Tec personnel discovered a problem with the | | container. It appeared that the container had been opened and put back | | together incorrectly. The container's T-bar was missing, and the lid was | | upside-down with the bromine-82 on the outside of the container rather than | | shielded on the inside of the container. The bromine-82 appeared to be | | intact. Smear tests were performed using a GM detector, and there was no | | evidence of contamination or of a breech in the double encapsulated | | material. Survey readings with the bromine-82 unshielded on the outside of | | the package resulted a dose rate of 6 millirem per hour at a distance of 6 | | feet. The bromine-82 is currently under control and in the possession of | | the Tru-Tec Services, Inc. | | | | The bromine-82 was intended for use in tracer studies at chemical plants, | | and it was manufactured at Texas A&M. It was reported that the half life of | | bromine-82 is 35 hours, and the estimated activity of the material at noon | | on 12/08/00 would have been 140 millicuries. bromine-82 is a strong gamma | | emitter. The Tru-Tec Services, Inc. main office is located in Delaware. | | | | The licensee plans to contact the carriers and plans to attempt to trace its | | path and discover who came into contact with the container. | | | | (Call the NRC operations officer for licensee contact information.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37582 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 12/08/2000| |LICENSEE: ASSOCIATED SOILS ENGINEERING, INC. |NOTIFICATION TIME: 20:06[EST]| | CITY: ORANGE REGION: 4 |EVENT DATE: 12/04/2000| | COUNTY: STATE: CA |EVENT TIME: 05:30[PST]| |LICENSE#: 2446-19 AGREEMENT: Y |LAST UPDATE DATE: 12/08/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BLAIR SPITZBERG R4 | | |THOMAS ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PAUL BALDENWEG | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN ASSOCIATED SOILS ENGINEERING, INC, MOISTURE DENSITY GAUGE | | | | The following text is a portion of a facsimile received from the State of | | California, Department of Health Services, Radiologic Health Branch: | | | | "A CPN Moisture/Density gauge, model MC1 DR, S/N MD 01005909, was picked up | | from the office [in Long Beach, CA] on 12/03/00. It was locked down in the | | back of the truck of the gauge user [...]. The gauge was stolen between | | 2100 [PST] on 12/03/00 and 0530 [PST] on 12/04/00 from [the user's] trailer | | [park located in ...] Orange, CA [...]." | | | | It was reported that the licensee notified the local Police Department and | | that the gauge contained an unknown quantity of americium-241/beryllium. | | | | (Call the NRC operations officer for contact information.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37583 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 12/09/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 12:40[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/09/2000| +------------------------------------------------+EVENT TIME: 10:15[EST]| | NRC NOTIFIED BY: CECIL H. WILLIAMS, JR. |LAST UPDATE DATE: 12/09/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PAUL FREDRICKSON R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DURING PERFORMANCE OF A REVISED PROCEDURE FOR A SOLID | | STATE PROTECTION SYSTEM (SSPS) AND REACTOR TRIP BREAKER OPERABILITY TEST | | | | The following text is a portion of a facsimile received from the licensee: | | | | "While performing a new revision to [procedure] 14421-1, 'SOLID STATE | | PROTECTION SYSTEM AND REACTOR TRIP BREAKER TRAIN B OPERABILITY TEST,' a | | reactor trip occurred from Intermediate Range High Flux while performing | | section 5.3, SAFETY INJECTION RESET TIMING CIRCUIT TEST. Both trains of | | [the] reactor protection system functioned as expected. A feedwater | | isolation was received as expected from P4-Low Tavg, but only from SSPS | | Train A due to SSPS Train B being in 'TEST' for the surveillance in | | progress. Also, an [auxiliary feedwater] actuation signal (AFWAS) was | | received from Steam Generator Lo-Lo level in all four steam generators, but | | only the [turbine-driven auxiliary feedwater pump] pump and [motor-driven | | auxiliary feedwater pump] pump A started, again due to SSPS Train B being in | | 'TEST.' The steam generator blowdown system also isolated properly on the | | AFWAS signal. The plant is currently stable in Mode 3, and an Event Review | | Team is currently being formed. At 1207, Train B SSPS was restored to [its] | | normal configuration. No estimated restart date is currently available." | | | | The licensee stated that all control rods fully inserted as a result of the | | trip. It was also reported that all systems functioned as required based on | | the configuration of the plant at the time of the event (SSPS Train B in | | test) and that there was nothing unusual or misunderstood. The root cause | | of the reactor trip is currently under investigation. | | | | The unit is currently stable in Mode 3 (Hot Standby). Normal charging and | | letdown, pressurizer heaters and sprays, and the reactor coolant pumps are | | being utilized for primary system inventory, pressure, and transport | | control. Secondary steam is being dumped to the condenser, and auxiliary | | feedwater is being supplied to the steam generators. All containment | | parameters are normal, and offsite power is available. | | | | The NRC resident inspector was in the control room watching performance of | | the surveillance procedure at the time of the event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37584 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 12/09/2000| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 13:23[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/09/2000| +------------------------------------------------+EVENT TIME: 11:55[CST]| | NRC NOTIFIED BY: FRANK WEAVER |LAST UPDATE DATE: 12/09/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BLAIR SPITZBERG R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A DEFICIENCY THAT COULD POTENTIALLY COMPROMISE THE ABILITY OF A | | FIRE BARRIER TO PROVIDE ADEQUATE PROTECTION IN THE EVENT OF A FIRE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During destructive examination of the Kaowool fire barrier system used to | | protect Appendix R raceways, a deficiency was identified that could | | potentially compromise the ability of the fire barrier to provide adequate | | protection for at least one train of redundant safe shutdown capability in | | the event of a fire. The affected plant area is the Division 2 [engineered | | safety feature] switchgear room, where redundant functions of both the | | Division 1 and 2 Standby Service Water systems could be affected. Fire | | protection program compensatory actions, i.e., [an] hourly firewatch has | | been in place since the deficiencies as identified in SECY 99-204 were | | documented at Grand Gulf. The area has detection and automatic fire | | suppression [systems] that are OPERABLE. Additionally, because of the | | outcome of the above mentioned examination, a continuous firewatch has been | | established as an additional compensatory measure." | | | | The licensee stated that the hourly fire watch has been in place since | | 09/01/99. The hourly fire watch is required be technical specifications; | | however, the continuous fire watch has been established as an additional | | conservative measure. | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37585 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 12/11/2000| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 04:42[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 12/11/2000| +------------------------------------------------+EVENT TIME: 04:05[EST]| | NRC NOTIFIED BY: THOMAS |LAST UPDATE DATE: 12/11/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |50 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED TECHNICAL SPECIFICATION REQUIRED SHUTDOWN PRIMARY LEAK | | EXCEEDING ALLOWABLE VALUES. | | | | At 0320 Unit 2 received indications of a primary leak in containment that | | exceeded allowable values in Tech Spec 3.4.6.2. These indications included | | containment gas activity alert alarm, Pressurizer level reduction, | | Pressurizer spray valve closure and an increase in charging flow. Indicated | | charging/letdown mismatch is 7 gpm. Calculated primary leak rate estimate | | based on VCT and Pressurizer level changes was 9.5 gpm at 0400. At 0412 Unit | | 2 began a plant shutdown at 2% per minute. This constitutes the initiation | | of a plant shutdown required by Tech Specs. A containment entry is planned | | to identify the source of the leak. The entry will be made after the reactor | | is subcritical. | | | | The NRC Resident Inspector will be notified. | | | | | | * * * UPDATE ON 12/20/00 @ 0603 BY THOMAS TO GOULD * * * | | | | Update at 0543: Estimated RCS leak rate based on charging/letdown mismatch | | exceeds 10 gpm. An Unusual Event was declared at 0536 due to Unidentified | | Leakage exceeding 10 gpm. Current leak rate estimate is between 12 and 20 | | gpm. Plant is currently at 22% power. | | | | The NRC Resident Inspector was notified. FEMA(Bagwell), RDO(Rogge), | | EO(Zwolinski), and IRO(Miller) | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021