Event Notification Report for November 30, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/29/2000 - 11/30/2000 ** EVENT NUMBERS ** 37555 37556 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37555 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 11/28/2000| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 17:16[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/28/2000| +------------------------------------------------+EVENT TIME: 16:25[EST]| | NRC NOTIFIED BY: JOHN SMALL |LAST UPDATE DATE: 11/29/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEORGE BELISLE R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH UNITS OUTSIDE OF DESIGN BASIS DUE TO MOMENTARY LOSS OF BOTH TRAINS OF | | CONTROL ROOM VENTILATION | | | | "Presently, 'A' Control Room Ventilation out of service for maintenance. | | 'B' Control Room Ventilation (VC/YC) inadvertently deenergized causing both | | trains of VC/YC to be inoperable. 'B' VC/YC restarted with no further | | complications. Deenergized from 1625 until 1643 which places both units one | | and two outside design basis. With VC/YC inoperable for 'A' and 'B' trains, | | entered [TS] 3.0.3 momentarily." | | | | The problem occurred when the technician performing maintenance on the "A" | | train went to the operating "B" train. The "B" train Chiller was tripped in | | error. The licensee informed the NRC resident inspector. | | | | * * * * UPDATE 1159EST ON 11/29/00 FROM JOHN JENKINS TO S. SANDIN * * * * | | | | The licensee is retracting this report based on the following: | | | | "On November 29, 2000, the above notification was made to the NRC under the | | requirements of 10 CFR 50.72 (b) (1) (ii) (B). Upon further evaluation, it | | has been determined that this condition did not place the plant outside of | | design basis. | | | | "The ability to pressurize the Main Control Room was not affected in this | | condition. The pressurization fans would start and run if needed during an | | accident. The pressurization function mitigates dose to the control | | operators. | | | | "During the 18 minutes that the chiller was out of service the temperature | | in the Control Room increased from 70 degrees to approximately 72 � degrees. | | The temperature rise was evaluated by the System Engineer. The temperature | | limit for the control room is listed as a maximum of 90 degrees in the | | Selected Licensee Commitments. This temperature is based on a continuous | | duty rating for equipment and instrumentation and for habitability of the | | Control Room. Annunciator alarms would alert the Operators of the increasing | | temperature and existing procedures would direct actions to be taken to | | limit the temperature affects. The Engineering evaluation determined that | | the chiller would need to be out of service for 2 hours before this limit | | was challenged. | | | | "This occurrence did not increase the probability of barrier failure or | | radiation releases. Remote shutdown capability outside the control room was | | not affected. For these reasons the plant remained within its design | | basis." | | | | The licensee will inform the NRC resident inspector. Notified | | R2DO(Belisle). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37556 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/29/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:11[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/29/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 11:35[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/29/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MICHAEL JORDAN R3 | | DOCKET: 0707002 |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICK LARSON | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REPORT INVOLVING ACTUATION OF A SAFETY SYSTEM | | | | "AT 1135 HOURS ON 11/29/00 AUTOCLAVE #3 IN THE X-343, EXPERIENCED A HIGH | | CONDENSATE LEVEL SHUTOFF ACTUATION WHEN BOTH PROBES IN THE CONDENSATE DRAIN | | LINE FIRED. THIS ACTUATION OCCURRED DURING MODE II OPERATIONS (HEATING), | | RESULTING IN THE SHUTTING OF THE STEAM ISOLATION VALVE AND SHUTTING DOWN OF | | THE AUTOCLAVE. OPERATORS FOLLOWING APPROVED RESPONSE PROCEDURES VERIFIED | | THE CYLINDERS STRUCTURAL INTEGRITY. APPROXIMATELY TEN MINUTES AFTER THE | | STEAM VALVE SHUT THE HIGH CONDENSATE PROBE ALARMS CLEARED BASED ON THE | | ACTUATION OF BOTH CONDENSATE LEVEL PROBES. THIS IS BEING REPORTED AS A | | SAFETY SYSTEM ACTUATION. THE AUTOCLAVE WAS DECLARED INOPERABLE AND | | ENGINEERING IS EVALUATING THIS SYSTEM ACTUATION. THERE WAS NO RELEASE OF | | RADIOACTIVE MATERIAL FROM THIS EVENT." | | | | OPERATIONS PERSONNEL INFORMED BOTH THE DOE SITE REPRESENTATIVE AND THE NRC | | RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
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