Event Notification Report for November 28, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/27/2000 - 11/28/2000 ** EVENT NUMBERS ** 37469 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37469 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 10/28/2000| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 17:40[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 10/28/2000| +------------------------------------------------+EVENT TIME: 15:11[EDT]| | NRC NOTIFIED BY: HARROW |LAST UPDATE DATE: 11/27/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANNE BOLAND R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N N 0 Hot Shutdown |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RWST CROSS-TIE VALVES UNEXPECTEDLY OPENED DURING PLANNED MAINTENANCE | | | | At 1511 hours, with Unit 2 in Intermediate Shutdown (ISD), approximately 375 | | degrees F, Unit 1 and Unit 2 RWST Cross-tie-valves opened when the High | | Steam Flow SI signal was unblocked for planned maintenance. By design, the | | Header to Line SI signal which opens these valves is unblocked when High | | Steam Flow is unblocked. At the time of the unblock, a header to line | | condition existed on Unit 2 due to plant conditions. This design was newly | | implemented during the current Unit 2 refueling outage and procedures did | | not provide adequate steps to prevent the valves from opening. A Header to | | Line SI signal was not received as it was properly defeated in accordance | | with station procedures. The cross-tie valves were manually closed when the | | condition was identified as not required. | | | | Unit 1 is currently at 100% power. Unit 2 is in Intermediate Shutdown with | | RCS heatup and pressurization in progress. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE 1725EST ON 11/27/00 FROM ALLEN HARROW TO S. SANDIN * * * | | | | The licensee is retracting this report based on the following: | | | | "At 1740 hours on 10/28/00, Surry Power Station made a 4 hour Non-Emergency | | Notification in accordance with 10CFR50.72(b)(2)(ii) due to the opening of | | the RWST Cross-tie valves when the High Steam Flow SI signal was unblocked | | for planned maintenance (Event Number 37469). | | | | "Based on further review of the event reported on October 28, 2000 it has | | been determined that the conditions did not meet the criteria of 10CFR50.72 | | as clarified in NUREG 1022, Rev 1. The NUREG states: | | | | 'Usually, the staff would not consider this to include single component | | actuations because single components of complex systems, by themselves, | | usually do not mitigate the consequences of significant events. However, in | | some cases a component would be sufficient to mitigate the event (i.e. | | perform the ESF function) and its actuation would, therefore, be reportable. | | This position is consistent with the statement that the reporting | | requirement is based on the premise that ESFs are provided to mitigate the | | consequence of a significant event. | | | | 'Single trains do mitigate the consequences, and, thus, train level | | actuations are reportable.' | | | | "Specifically, the initial assessment considered the event as an ESF | | actuation and therefore reportable under criterion 10CFR50.72(b)(2)(ii). The | | nature of this event does not constitute a train actuation. The only signal | | affected was that going to the RWST Cross-tie valves. This occurred because | | the block signal was unblocked due to placing the RCS narrow range | | temperature loops in trip while performing the RTD cross calibrations while | | heating up Unit 2 following a refueling outage. The details of this event | | are consistent with the discussion and examples of NUREG 1022 that would not | | be reported. | | | | "This notification is being made to retract the report made on 10/28/00 | | based on the above discussion." | | | | The licensee informed the NRC resident inspector. Notified R2DO(Rodgers). | +------------------------------------------------------------------------------+
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