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Event Notification Report for November 24, 2000

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           11/22/2000 - 11/24/2000

                              ** EVENT NUMBERS **

37486  37545  37546  37547  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   37486       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 11/03/2000|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:27[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/02/2000|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        14:30[CST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/22/2000|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |DAVID HILLS          R3      |
|  DOCKET:  0707001                              |BRIAN SMITH          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  MIKE UNDERWOOD               |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBB 76.120(c)(2)(ii)    EQUIP DISABLED/FAILS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CRITICALITY ALARM HORNS AIR PRESSURE FOUND OUT OF SPECIFICATION DURING       |
| SURVEILLANCE                                                                 |
|                                                                              |
| "At 1330 on 11/2/00, the Plant Shift Superintendent was notified that the    |
| testing of the C-337 and C-337-A Criticality Accident Alarm System (CAAS)    |
| air horn regulators resulted in as found data which is outside of the        |
| optimum air pressure band allowed to insure desired horn sound quality.      |
| Twelve of the twenty-five CAAS horn regulators located in these two areas    |
| were discovered outside the desired pressure band. The effect of this as     |
| found condition is unknown at this time and is being evaluated by            |
| Engineering. This evaluation will require greater than the 24-hour reporting |
| time limit allowed by 10 CFR 76.120.c.2. Due to the uncertainties and the    |
| length of time required to complete the engineering evaluation the condition |
| is being conservatively reported.                                            |
|                                                                              |
| "Reasonable assurance of operability of CAAS horns in these and other        |
| buildings exists based on the successful completion of quarterly and annual  |
| TSR surveillances. In addition, all CAAS horn regulators found outside of    |
| established criteria during this and previous tests on other building CAAS   |
| systems were returned to acceptable values prior to returning the systems to |
| service.                                                                     |
|                                                                              |
| "This event is reportable under 10 CFR 76.120(c)(2) as an event in which     |
| equipment required by the TSR is disabled or fails to function as designed.  |
|                                                                              |
| "The NRC Senior Resident has been notified of this event."  The DOE          |
| representative will be notified.                                             |
|                                                                              |
| * * * RETRACTION 1450 11/22/2000 FROM TOM WHITE TAKEN BY BOB STRANSKY * * *  |
|                                                                              |
| "On November 2, 2000, the PSS was notified that the testing of the C-337 and |
| C-337A CAAS air horns had resulted in the discovery that the horn air        |
| regulator pressure was outside of the allowed optimum air pressure band used |
| to ensure desired horn sound quality. This condition potentially affected    |
| the audibility of twelve of the twenty-five horns located in the C-337 and   |
| C-337A. The actual affect on the system was unknown at the time and could    |
| not be determined within the 24-hour reporting limit. Thus, the condition    |
| was conservatively reported to the NRC per 10CFR76.120(c)(2).                |
|                                                                              |
| Subsequently, System Engineering issued Engineering Notice EN-C-822-00-035   |
| that transmitted the results of Operability Evaluation OE-C-822-00-005. This |
| documented the results of additional CAAS horn testing at the air regulator  |
| pressure values noted on November 2, 2000 and testing data in other          |
| buildings. The evaluation concluded that although there is an expected       |
| amount of drift or variance in the settings of the air pressure regulators   |
| [for] the CAAS horns, in the as-found condition, could have performed their  |
| intended safety function and pass the audibility criteria described in the   |
| SAR."                                                                        |
|                                                                              |
| The NRC resident inspector has been informed of this retraction. Notified    |
| R3DO (Creed), NMSS (Smith).                                                  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   37545       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 11/22/2000|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:50[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/22/2000|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        03:40[CST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/22/2000|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |JAMES CREED          R3      |
|  DOCKET:  0707001                              |BRIAN SMITH          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  T. WHITE                     |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NCFR                     NON CFR REPORT REQMNT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SAFETY SYSTEM ACTUATION                                                      |
|                                                                              |
| "At 0340 on 11/22/00, the PSS office was notified that a primary condensate  |
| alarm was received on the C-333A position 3 South autoclave Water Inventory  |
| Control System (WICS). The WICS system is required to be operable while      |
| heating in mode 5 according to TSR 2.2.4.2. The autoclave was checked        |
| according to the alarm response procedure, removed from service and the      |
| Water Inventory Control System was declared inoperable by the Plant Shift    |
| Superintendent. The WICS actuation has been determined to be a valid         |
| actuation by the System Engineer.                                            |
|                                                                              |
| "This safety system actuation is reportable to the NRC as required by Safety |
| Analysis Report, section 6.9, table 1 criteria J.2, Safety System actuation  |
| due to a valid signal as a 24-hour event notification."                      |
|                                                                              |
| The NRC Senior Resident Inspector has been notified of this event.           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37546       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  ILLINOIS DEPT OF NUCLEAR SAFETY      |NOTIFICATION DATE: 11/22/2000|
|LICENSEE:  JOHNS MANVILLE INTERNATIONAL         |NOTIFICATION TIME: 17:23[EST]|
|    CITY:  WAUKEGAN                 REGION:  3  |EVENT DATE:        11/21/2000|
|  COUNTY:                            STATE:  IL |EVENT TIME:             [CST]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  11/22/2000|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JAMES CREED          R3      |
|                                                |PHILIP TING          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TOM SIKES                    |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT                                                       |
|                                                                              |
| The licensee contacted the State of Illinois to request assistance in        |
| locating a 20 mCi Cs-137 source. The source was mounted in an Omart model    |
| SH-F1 holder, and was licensed under a general license. Representatives of   |
| the state surveyed warehouses and other buildings throughout the licensee's  |
| facility and other licensee locations, but were unable to locate the source. |
| The licensee is currently investigating whether the source may have been     |
| sent to a licensee facility in Colorado; however, the source may have been   |
| discarded during renovations to the warehouse in which it had been located.  |
| In this instance, the source may have been deposited in a landfill in        |
| Wisconsin. The state is continuing its investigation of this matter.         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37547       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: ARKANSAS NUCLEAR         REGION:  4  |NOTIFICATION DATE: 11/23/2000|
|    UNIT:  [1] [2] []                STATE:  AR |NOTIFICATION TIME: 04:25[EST]|
|   RXTYPE: [1] B&W-L-LP,[2] CE                  |EVENT DATE:        11/23/2000|
+------------------------------------------------+EVENT TIME:        03:15[CST]|
| NRC NOTIFIED BY:  WAYNE AHO                    |LAST UPDATE DATE:  11/23/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GAIL GOOD            R4      |
|10 CFR SECTION:                                 |                             |
|AARC 50.72(b)(1)(v)      OTHER ASMT/COMM INOP   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SPDS OUT OF SERVICE FOR PLANNED MAINTENANCE                                  |
|                                                                              |
| The safety parameter display system (SPDS) was deenergized for planned       |
| maintenance.  The system is expected to be down for 2 to 3 hours.            |
|                                                                              |
| The licensee notified the NRC Resident Inspector and intends to notify the   |
| state authorities.                                                           |
+------------------------------------------------------------------------------+


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