Event Notification Report for November 20, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/17/2000 - 11/20/2000 ** EVENT NUMBERS ** 37530 37531 37532 37533 37534 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37530 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 11/17/2000| | UNIT: [] [2] [] STATE: TN |NOTIFICATION TIME: 10:41[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/17/2000| +------------------------------------------------+EVENT TIME: 08:42[EST]| | NRC NOTIFIED BY: HARRIS |LAST UPDATE DATE: 11/17/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 53 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD A REACTOR TRIP FROM 53% POWER DUE TO A TURBINE TRIP | | | | A "Turbine Trip/Reactor Trip" occurred at 53% reactor power due to a sudden | | pressure relay actuation on C phase Main Bank transformer which sent signal | | to the generator resulting in the turbine trip. Motor Driven Auxiliary | | Feedwater pumps started as required when level decreased to less than 10% in | | one Steam Generator and the Turbine Driven Auxiliary Feedwater pump started | | as required on less than 10% in two steam generators. Preliminary walkdown | | of the transformer showed no visible exterior damage or degradation. | | Investigation is in progress to determine the cause of this event. The Unit | | is stable and operating in accordance with Plant General Operating | | procedures. All rods fully inserted, there were no ECCS actuations and no | | safety relief valves lifted. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37531 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 11/17/2000| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 15:21[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 11/16/2000| +------------------------------------------------+EVENT TIME: 15:54[EST]| | NRC NOTIFIED BY: KEVIN DONNELLY |LAST UPDATE DATE: 11/17/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ERIC REBER R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SITE ACCESS INAPPROPRIATELY GRANTED TO UTILITY EMPLOYEE | | | | During a QA Audit it was determined that one (1) utility employee may have | | been granted access inappropriately following offsite drug testing conducted | | on 9/99. The employee was recalled to the site today for retesting. | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37532 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 11/17/2000| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 20:41[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/17/2000| +------------------------------------------------+EVENT TIME: 20:10[EST]| | NRC NOTIFIED BY: SCOTT RICHARDSON |LAST UPDATE DATE: 11/18/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 ENTERED TS 3.0.3 AFTER DECLARING BOTH LOOPS ECCS INOPERABLE | | | | "Tech Spec 3.5.2 requires two independent Emergency Core Cooling System | | (ECCS) loops, each capable of taking suction from the Refueling Water | | Storage Tank (RWST) and being transferred to the containment recirculation | | sump. This spec applies in modes 1 - 3. Following evaluation of recent | | modifications to the containment recirc sump ECCS suction isolation valves, | | it has been determined that neither of the two isolation valves (2-ICM-305 | | and 2-ICM-306) could be relied upon to open when transfer of ECCS suction is | | required. This is attributed to a lack of assurance that between seat | | relief valves on 2-ICM-305 and 2-ICM-306 would lift and preclude thermal | | hydraulic locking of the valves in the closed position. Since neither ECCS | | loop recirc sump suction is operable, the action statement of TS 3.5.2 is | | not valid. This led to the Shift Manager declaring entry into TS 3.0.3 with | | a requirement to place the unit in a mode for which TS 3.5.2 does not apply. | | A unit shutdown at 2% per hour has been initiated. Plans are to implement | | compensatory actions or have the unit in hot standby within 6 hours." | | | | The licensee anticipates exiting TS 3.0.3 after bleeding the fluid trapped | | between the double disk valves in approximately two hours. The licensee | | informed the NRC resident inspector. | | | | * * * UPDATE 0310 11/18/2000 FROM RICHARDSON TAKEN BY STRANSKY * * * | | | | The united exited the shutdown LCO at 2315. Reactor power had been reduced | | from 100% to 90%. The licensee removed approximately 4.5 gallons of water | | from the body of each valve in order to prevent thermal locking. The NRC | | resident inspector will be informed. Notified R3DO (Jorgensen). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37533 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 11/18/2000| | UNIT: [] [2] [] STATE: AZ |NOTIFICATION TIME: 17:36[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 11/18/2000| +------------------------------------------------+EVENT TIME: 11:47[MST]| | NRC NOTIFIED BY: RUSSELL A. STROUD |LAST UPDATE DATE: 11/18/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM ANDREWS R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 45 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED AN AUTOMATIC REACTOR TRIP FOLLOWING A REACTOR POWER | | CUTBACK | | | | "On November 18, 2000, at approximately 1147 MST, Palo Verde Unit 2 | | experienced an automatic reactor trip (RPS actuation) from approximately 45% | | rated thermal power. Unit 2 is stable at normal operating temperature and | | pressure in Mode 3. The event did not result in any challenges to the | | fission product barrier. There were no adverse safety consequences or | | implications as a result of this event. The event did not adversely affect | | the safe operation of the plant or the health and safety of the public. | | | | "Prior to the reactor trip, at approximately 1008 MST, Unit 2 was at 100 | | percent power and normal operating temperature and pressure, when testing | | began to validate various parts of the electrical generator and exciter | | model parameters. At approximately 1059 MST, Unit 2 experienced a | | generator/turbine trip. Steam bypass control valves opened and a reactor | | power cutback was initiated. | | | | "Operations personnel were in the process of plant stabilization after the | | reactor power cutback, when at approximately 1147 MST, the reactor tripped. | | All control element assemblies (CEAs) inserted as required and the trip was | | classified as uncomplicated with respect to the emergency plan. The primary | | plant is now stabilized in Mode 3 in forced circulation with both steam | | generators being used for heat removal, | | | | "The cause of the reactor trip has not been determined and is under | | investigation at this time. APS [Arizona Public Service] will supplement | | this report if information is developed which significantly alters this | | information." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37534 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 11/19/2000| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 13:15[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/19/2000| +------------------------------------------------+EVENT TIME: 06:20[EST]| | NRC NOTIFIED BY: VINCENT WOODS |LAST UPDATE DATE: 11/19/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSED EMPLOYEE DETERMINED POSITIVE FOR FAILURE TO PROVIDE A FOR-CAUSE | | TEST SAMPLE | | | | A licensed employee was determined to be under the influence of alcohol | | after refusing to provide a sample during a for-cause test. The employee's | | left the site and access to the plant has been terminated. The licensee | | informed the NRC resident inspector. Contact the Headquarters Operations | | Officer for additional details. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021