Event Notification Report for November 16, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/15/2000 - 11/16/2000 ** EVENT NUMBERS ** 37524 37525 37526 37527 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37524 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 11/15/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 15:49[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/15/2000| +------------------------------------------------+EVENT TIME: 14:22[EST]| | NRC NOTIFIED BY: VERITA BELLAMY |LAST UPDATE DATE: 11/15/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO FAILURE OF TURBINE RUNBACK ACTUATION CIRCUITS | | | | Unit 2 experienced a turbine runback at 1410 EST. The control room | | operators noticed all status lights for overpower and overtemperature delta | | T runback were illuminated. The operators decided to manually trip the | | reactor from about 23 % rated thermal power. The reactor trip resulted in a | | turbine trip as expected. Auxiliary feedwater pumps started due to low-low | | steam generator levels. The unit is stable in Mode 3. | | | | The runback bistables are locked in without having the logic bistables | | tripped that feed the trip circuit. The licensee is troubleshooting the | | problem and the cause is unknown at this time. The plant will remain in | | Mode 3 until the problem is corrected. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37525 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 11/15/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 19:04[EST]| | RXTYPE: [1] GE-2 |EVENT DATE: 11/15/2000| +------------------------------------------------+EVENT TIME: 17:50[EST]| | NRC NOTIFIED BY: JERE FREEMAN |LAST UPDATE DATE: 11/15/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 1 Startup |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM DUE TO LOW REACTOR WATER LEVEL | | | | The plant received a low water level reactor scram during turbine | | manipulation after 2 turbine bypass valves opened. All systems functioned | | as designed. The actual cause is not fully understood and is under | | investigation. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37526 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 11/15/2000| | UNIT: [1] [2] [] STATE: GA |NOTIFICATION TIME: 20:30[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/15/2000| +------------------------------------------------+EVENT TIME: 19:30[EST]| | NRC NOTIFIED BY: HARRY RUSSELL |LAST UPDATE DATE: 11/15/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF PRIMARY METEOROLOGICAL TOWER INDICATIONS | | | | The licensee suffered a loss of all indications from the primary | | meteorological tower and loss of backup meteorological tower delta | | temperature in the control room and safety parameter display system. The | | backup meteorological tower indications available are wind speed and | | direction. This reduces the ability to perform prompt offsite dose | | assessment. The cause is unknown and is being investigated. There were no | | operations or work ongoing at the time. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37527 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 11/16/2000| | UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 05:10[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 11/16/2000| +------------------------------------------------+EVENT TIME: 03:23[CST]| | NRC NOTIFIED BY: BRAD MOORE |LAST UPDATE DATE: 11/16/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON HIGH-HIGH STEAM GENERATOR WATER LEVEL FOLLOWING A | | MASTER STEAM GENERATOR FEEDWATER PUMP CONTROLLER FAILURE AND SLUGGISH | | CONTROLS AFTER SWITCHING TO MANUAL | | | | The master steam generator feedwater pump controller failed low and caused | | feedwater pump speeds to slow down. (Both pumps dropped to 3,200 rpm.) In | | an attempt to regain feedwater pump speed and steam generator water level in | | manual, a high-high level was reached in the 2A steam generator. This | | caused a turbine trip and subsequent reactor trip. All control rods fully | | inserted. Auxiliary feedwater actuation and feedwater isolation occurred as | | expected. All systems functioned as required. | | | | It was reported that the controller was sluggish after manual control was | | taken and that operators were not able to terminate the rising level in the | | 2A steam generator before the high-high level trip setpoint was reached. | | The lowest steam generator water level attained was approximately 27%. The | | low level trip occurs at 25%. The cause of the controller failure is | | currently under investigation. | | | | The unit is currently stable in Hot Standby. Pressurizer heaters and | | sprays, normal charging and letdown, and the reactor coolant pumps are | | currently being utilized for primary system pressure, level, and transport | | control. Secondary steam is being dumped to the main condenser, and | | auxiliary feedwater is supplying water to the steam generators. All | | containment parameters are normal. | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021