Event Notification Report for November 6, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/03/2000 - 11/06/2000 ** EVENT NUMBERS ** 37485 37486 37487 37488 37489 37490 37491 37492 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37485 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/03/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 11:29[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/02/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:45[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/03/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WHITE | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR 91-01 BULLETIN | | | | At 1645 CST on 11-02-00, the Plant Shift Superintendent (PSS) was notified | | of a violation of NCSA GEN-15 Machining waste, defined in NCSE GPS-11 to be | | potentially fissile, was collected in a 55-gallon drum in the C-720 machine | | shop in violation of NCSA GEN-15. GEN-15 limits the containers used for | | accumulating fissile/potentially fissile waste to approved 5.5-gallon | | container. The purpose of this requirement is to ensure that fissile | | material will be accumulated in approved containers. | | | | SAFETY SIGNIFICANCE OF EVENTS; | | The mass of fissile material contained in the waste drum is less than what | | is required to achieve criticality. Therefore, no possibility exists for an | | inadvertent criticality. However, double contingency was not maintained. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR: | | In order for a criticality to be possible, an additional violation would | | have to occur resulting in unsafe mass of fissile material accumulating in | | an unsafe geometry. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC): | | Double contingency for this scenario is established by implementing one | | control on mass and one control on volume. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITICAL MASS): | | A process limit of 22.3 kg. At 5.5 wt. % 235U would have to be exceeded for | | a criticality | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES; | | The two process conditions relied upon for double contingency for this | | scenario are mass and volume, | | | | The first leg of double contingency is based on limiting the mass of uranium | | accumulated. Analysis has shown that the machining waste from approximately | | 1490 machining operations would have to be accumulated before exceeding an | | unsafe mass. The waste would occupy more than eighteen 5.5-gallon | | containers, which exceeds the volume of the 55-gallon waste container (drum) | | in the machine shop. This control was not violated. | | | | The second leg of double contingency is based on the accumulation of fissile | | waste only in approved containers, limited to 5.5 gallons. This is | | controlled by limiting the volume of the containers used for accumulating | | fissile waste. Potentially fissile waste was placed In a container other | | than an approved 5.5 gallon container, violating this control. The | | machining waste exceeded the allowed volume of 5.5 gallons and resulted in a | | loss of the process condition. | | | | Since the volume process condition was lost, double contingency was not | | maintained. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: | | Access to the area containing the 55 gallon drum has been controlled by | | ropes and signs. Remediation of violation will be made following development | | of a Remediation Guide. | | | | The NRC Resident Inspector was notified. | | | | The DOE Representative will be informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37486 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/03/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:27[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/02/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 14:30[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/03/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MIKE UNDERWOOD | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CRITICALITY ALARM HORNS AIR PRESSURE FOUND OUT OF SPECIFICATION DURING | | SURVEILLANCE | | | | "At 1330 on 11/2/00, the Plant Shift Superintendent was notified that the | | testing of the C-337 and C-337-A Criticality Accident Alarm System (CAAS) | | air horn regulators resulted in as found data which is outside of the | | optimum air pressure band allowed to insure desired horn sound quality. | | Twelve of the twenty-five CAAS horn regulators located in these two areas | | were discovered outside the desired pressure band. The effect of this as | | found condition is unknown at this time and is being evaluated by | | Engineering. This evaluation will require greater than the 24-hour reporting | | time limit allowed by 10 CFR 76.120.c.2. Due to the uncertainties and the | | length of time required to complete the engineering evaluation the condition | | is being conservatively reported. | | | | "Reasonable assurance of operability of CAAS horns in these and other | | buildings exists based on the successful completion of quarterly and annual | | TSR surveillances. In addition, all CAAS horn regulators found outside of | | established criteria during this and previous tests on other building CAAS | | systems were returned to acceptable values prior to returning the systems to | | service. | | | | "This event is reportable under 10 CFR 76.120(c)(2) as an event in which | | equipment required by the TSR is disabled or fails to function as designed. | | | | "The NRC Senior Resident has been notified of this event." The DOE | | representative will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37487 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 11/04/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 08:27[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 11/04/2000| +------------------------------------------------+EVENT TIME: 08:22[EST]| | NRC NOTIFIED BY: THOMAS VEITCH |LAST UPDATE DATE: 11/04/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 98 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF POWER TO THE EOF DUE TO PLANNED MAINTENANCE | | | | "LOSS OF POWER TO THE EMERGENCY OPERATIONS FACILITY. THIS IS A PREPLANNED | | MAINTENANCE ACTIVITY ON BREAKER H2110. THE REMOVAL OF THIS BREAKER CAUSES | | THE FACILITY (EOF) TO LOSE POWER AND IS, THEREFORE, 'POTENTIALLY' | | UNAVAILABLE FOR GREATER THAN 90 MINUTES. THE TOTAL ESTIMATED DURATION OF | | THE ACTIVITY IS 8 HOURS." | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37488 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 11/05/2000| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 04:21[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/05/2000| +------------------------------------------------+EVENT TIME: 00:30[PST]| | NRC NOTIFIED BY: LAURA KENNEDY |LAST UPDATE DATE: 11/05/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GAIL GOOD IAT | |10 CFR SECTION: |ROBERTA WARREN IAT | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 1-HR SECURITY REPORT | | | | POTENTIAL BOMB THREAT. IMMEDIATE COMPENSATORY MEASURE TAKEN UPON | | DISCOVERY. LICENSEE HAS INFORMED STATE/LOCAL AGENCIES AND WILL INFORM THE | | NRC RESIDENT INSPECTOR. CONTACT THE HEADQUARTERS OPERATIONS OFFICER FOR | | ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37489 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 11/05/2000| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 04:39[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/05/2000| +------------------------------------------------+EVENT TIME: 01:20[PST]| | NRC NOTIFIED BY: DAVID PIERCE |LAST UPDATE DATE: 11/05/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |PHIL HARRELL R4 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC |JOSEPH GIITTER IRO | | |KEN BROCKMAN R4 | | |ELLIS MERSCHOFF R4 | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO A POTENTIAL BOMB THREAT | | | | THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO A POTENTIAL BOMB THREAT. THE | | LICENSEE INFORMED STATE/LOCAL AUTHORITIES AND WILL INFORM THE NRC RESIDENT | | INSPECTOR. | | | | THE NRC WAS PLACED IN THE MONITORING PHASE OF THE NORMAL MODE OF OPERATION | | BY THE RIV RA ( MERSCHOFF) AT 0400CST FOLLOWING DISCUSSIONS WITH IRO | | (GIITTER) AND THE EO (RICHARDS) . REGION IV INCIDENT RESPONSE CENTER WAS | | OPERATIONAL AT 0456CST. NOTIFIED CHAIRMAN'S STAFF (TSCHILTZ) , EDO STAFF | | (SMITH), AND HEADQUARTERS PAO (GAGNER). | | | | * * * 0610EST ON 11/5/00 FROM DAVID PIERCE TO S. SANDIN * * * | | | | THE LICENSEE TERMINATED THE UNUSUAL EVENT AT 0237PST AFTER DETERMINING THAT | | THE BOMB THREAT WAS NOT CREDIBLE. THE LICENSEE INFORMED STATE/LOCAL | | AGENCIES AND THE NRC RESIDENT INSPECTOR. RIV IRC AND FEMA (SULLIVAN) | | NOTIFIED. | | | | * * * 0700EST ON 11/5/00 * * * | | | | COMMISSIONER'S ASSISTANTS BRIEFING CONDUCTED. | | | | * * * 1655 EST ON 11/4/00 * * * | | | | The NRC exited Monitoring Phase of the Normal Mode of Operation by NRC | | Region 4 Regional Administrator (Ellis Merschoff) following discussion with | | IRO (Joseph Giitter) and R4 DRP (Kenneth Brockman). Notifications made | | include EDO's office (Garrett Smith), Chairman's office (Alan Levin), PAO | | (Sue Gagner). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37490 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 11/05/2000| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 16:38[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 11/05/2000| +------------------------------------------------+EVENT TIME: 14:07[CST]| | NRC NOTIFIED BY: RICK ROBBINS |LAST UPDATE DATE: 11/05/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNEXPECTED AUTOMATIC START OF THE G-03 EDG | | | | "During 2A06 Bus recovery work, from a scheduled bus maintenance outage, | | there was an automatic start of G-03 Emergency Diesel Generator (EDG). This | | was an inadvertent actuation and not part of the planned bus recovery work. | | G-03 EDG started and ran unloaded due to a 4160 Bus under voltage, that was | | caused by fuse replacement as part of the bus restoration procedure. The | | G-03 EDG output breaker 2A52-87 is currently out of service as part of the | | 2A06 bus outage, so the diesel could not have closed onto the dead bus. G-03 | | EDG was and is still lined up for normal operation to the 1A06 bus. Further | | investigation is continuing into the root cause of this actuation. | | | | "All buses remained energized and there were no other abnormal indications. | | Currently Unit 2 is in a refueling outage and is defueled at this time. Unit | | 1 is at 100% power normal operation." | | | | The sequence of actions taken were wrong in that the fuses were replaced | | when they should not have been. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37491 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 11/05/2000| | UNIT: [1] [] [] STATE: CA |NOTIFICATION TIME: 20:44[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/05/2000| +------------------------------------------------+EVENT TIME: 17:07[PST]| | NRC NOTIFIED BY: DAVE BAHNER |LAST UPDATE DATE: 11/05/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PHIL HARRELL R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 0 Startup |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP ON ROD CONTROL PROBLEM | | | | "Reactor startup was in progress. Power was stabilized at 10E-8 amps in the | | intermediate range to take critical data. A rod control urgent failure was | | received when the last rod step was taken to stabilize power. Maintenance | | was called to investigate. After troubleshooting, a card was replaced in the | | logic cabinet. Rods were requested to be inserted 1 step after card | | replacement for post maintenance testing. Rods continued to move in with no | | demand. Rods inserted 2.5 steps until another urgent failure came in and | | stopped rod motion. The reactor trip breakers were opened at this time." | | | | All rods fully inserted and all other systems functioned as required. | | Troubleshooting will continue for the rod control system. | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37492 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 11/06/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 05:29[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 11/06/2000| +------------------------------------------------+EVENT TIME: 03:38[CST]| | NRC NOTIFIED BY: DOUG HITZEL |LAST UPDATE DATE: 11/06/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PHIL HARRELL R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |90 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 1-HOUR SECURITY REPORT | | | | SAFEGUARDS SYSTEM DEGRADATION RELATED TO PERIMETER MONITORING. IMMEDIATE | | COMPENSATORY MEASURES TAKEN UPON DISCOVERY. THE LICENSEE WILL INFORM THE | | NRC RESIDENT INSPECTOR. CONTACT THE HEADQUARTERS OPERATIONS OFFICER FOR | | ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021