Event Notification Report for November 2, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/01/2000 - 11/02/2000 ** EVENT NUMBERS ** 37478 37479 37480 37481 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37478 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 11/01/2000| | UNIT: [1] [2] [] STATE: MN |NOTIFICATION TIME: 15:32[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 11/01/2000| +------------------------------------------------+EVENT TIME: 13:40[CST]| | NRC NOTIFIED BY: JERRY GOSMAN |LAST UPDATE DATE: 11/01/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNITS IN UNANALYZED CONDITION DUE TO INOPERABLE SAFEGUARDS COOLING WATER | | PUMPS | | | | "Due to a support system being unqualified (bearing lubrication water | | supply) the three safeguards cooling water (essential service water) pumps | | have been declared inoperable. This puts units outside their design basis. | | The pumps continue to be physically functional. | | | | "Compensatory measures are being implemented including provisions for | | standby replacement water supply and instructions for personnel for | | implementation. Preparations for an orderly plant two unit shutdown are in | | progress. A request for a NOED (Notice of Enforcement Discretion) has been | | initiated with NRR and Region III to allow continued operation until | | installation of a temporary modification is complete." | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37479 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SCHERING-PLOUGH |NOTIFICATION DATE: 11/01/2000| |LICENSEE: SCHERING CORPORATION |NOTIFICATION TIME: 16:08[EST]| | CITY: KENILWORTH REGION: 1 |EVENT DATE: 11/01/2000| | COUNTY: STATE: NJ |EVENT TIME: [EST]| |LICENSE#: 29-00244-02 AGREEMENT: N |LAST UPDATE DATE: 11/01/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JACK MCFADDEN R1 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAEGER | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING SHIPMENT OF I-125 | | | | The licensee reported that a shipment of I-125 (10 vials, 100 �Ci each) that | | was scheduled to arrive via FedEx on 10/31/00 cannot be located. When the | | package was not checked in to the RSO on 10/31/00, the licensee contacted | | the local FedEx office and attempted to locate the package. According to | | FedEx, the package was delivered on 10/26/00. The licensee stated that | | incoming FedEx packages are not invoiced and signed for individually; | | instead, a master list of packages is presented with the delivery (the | | packages are scanned when they are loaded onto the truck). The package has | | not been reported as misdelivered by any other FedEx customers. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37480 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 11/01/2000| | UNIT: [1] [2] [] STATE: TN |NOTIFICATION TIME: 16:20[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/01/2000| +------------------------------------------------+EVENT TIME: 14:20[EST]| | NRC NOTIFIED BY: CALVIN FIELDS |LAST UPDATE DATE: 11/01/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO OIL SPILL | | | | "A minor oil spill generated a small oil sheen on the Sequoyah Diffuser | | Pond. This was reported to the National Response Center at 1420 EST today. | | Based on reporting to another government agency this notification is being | | made. The oil spill is contained and cleanup in underway at this time." | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37481 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 11/01/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 19:51[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/01/2000| +------------------------------------------------+EVENT TIME: 17:54[CST]| | NRC NOTIFIED BY: ERICK MATZKE |LAST UPDATE DATE: 11/01/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PHIL HARRELL R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SHUTDOWN PROCEDURE NOT IN ACCORDANCE WITH LTOP ASSUMPTIONS | | | | "During review of plant procedures associated with the conditions for Low | | Temperature Overpressurization Protection (LTOP) it was noted that the plant | | procedure associated with pressurizer cooldown did not appear to be in | | accordance with the assumptions in the LTOP analysis. An investigation was | | conducted to determine if this was the case and it has been determined that | | the analysis assumes that the plant is not operated in a water solid | | condition in the pressurizer at temperatures above 130 F. Plant procedures | | do allow water solid plant operation at temperatures below 200 F. A check | | with operations has determined that it is normal shutdown procedure to take | | the plant solid soon after temperature is below 200 F (about 180 F). The | | plant is currently in the process of starting up and heating up. Plant | | temperature is about 250 F with a bubble in the pressurizer. Current plant | | operation is in accordance with the LTOP analysis." | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021