Event Notification Report for October 20, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/19/2000 - 10/20/2000 ** EVENT NUMBERS ** 37440 37441 37442 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37440 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 10/19/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 07:00[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 10/19/2000| +------------------------------------------------+EVENT TIME: 05:30[CDT]| | NRC NOTIFIED BY: MCLENNAN |LAST UPDATE DATE: 10/19/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MAIN STEAM LINE ISOLATION VALVES FAIL LOCAL LEAK RATE TEST | | | | At 0530 CT on 10/19/00, the total maximum pathway leakage for all main steam | | line isolation valves was determined by Local Leak Rate Testing to be in | | excess of Technical Specification 4.7.D.6 limit of < 46 scfh when tested at | | a test pressure of 25 psig. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37441 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WESTINGHOUSE ELECTRIC CORPORATION |NOTIFICATION DATE: 10/19/2000| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 08:53[EDT]| | COMMENTS: LEU CONVERSION (UF6 to UO2) |EVENT DATE: 10/18/2000| | COMMERCIAL LWR FUEL |EVENT TIME: 09:30[EDT]| | |LAST UPDATE DATE: 10/19/2000| | CITY: COLUMBIA REGION: 2 +-----------------------------+ | COUNTY: RICHLAND STATE: SC |PERSON ORGANIZATION | |LICENSE#: SNM-1107 AGREEMENT: Y |CAUDLE JULIAN R2 | | DOCKET: 07001151 |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM HEATH | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF VAPORIZE LEVEL PROBE IN "3A" VAPORIZER | | | | NRC BULLETIN 91-01 24 HOUR NOTIFICATION | | | | Periodic testing of the condensate level detection system in the 3A | | vaporizer steam chest determined that the system could not perform its | | intended function due to blockage in the system by loose debris. Further | | investigation determined that paint flaked from the recently processed | | cylinder and collected in the bottom of the vaporizer. However, the debris | | did not block the main condensate removal drain which allowed condensate to | | be removed from the vaporizer, so there was no condensate accumulation. | | | | The vaporizer bottom was cleaned and the level detection system was checked. | | The system responded correctly. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | No contingency occurred. No accumulation of water in the bottom of the | | vaporizer occurred. No SNM was involved. | | | | CONTROLLED PARAMETER: | | | | Mass and moderator are the controlled parameters for the vaporizer. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM of LICENSED MATERIAL: | | | | Cylinders heated in the vaporizer contain uranium hexafluoride gas with a | | uranium-235 enrichment less than 5.0 weight percent. No SNM was involved in | | this incident since uranium hexafluoride was contained at all times within | | the uranium hexafluoride piping system. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(s) OR CONTROLLED SYSTEM(s) AND | | DESCRIPTION OF THE FAILURES OR DEFICIENCIES: | | | | The condensate level detection system in the 3A vaporizer was rendered | | inoperable as a result of a drain line that was blocked by debris which came | | from the most recently processed cylinder. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: | | | | The debris in the 3A vaporizer was removed and proper functioning of the | | level detection system was verified. The 3A vaporizer was released for | | restart on October 19, 2000 at 0730 hours. Other vaporizers not in use at | | the time of the incident were checked for proper functioning of the level | | detection system; each system responded correctly. Other vaporizers in use | | at the time were subject to increased-frequency checks to verify proper | | functioning of the condensate removal system; all vaporizers were draining | | properly. In addition, the condensate level detection system for in-use | | vaporizers will be function-tested immediately after the uranium | | hexafluoride cylinder currently being processed is removed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37442 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 10/19/2000| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 15:53[EDT]| | RXTYPE: [3] CE |EVENT DATE: 10/19/2000| +------------------------------------------------+EVENT TIME: 13:40[CDT]| | NRC NOTIFIED BY: BRUCE PROCTOR |LAST UPDATE DATE: 10/19/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BORIC ACID RESIDUE DISCOVERED ON REACTOR COOLANT SYSTEM INSTRUMENT NOZZLES | | | | "During a bare metal inspection of reactor coolant system hot leg instrument | | nozzles, boric acid residue was found on two of the three mechanical nozzle | | seal assembly (MNSA) clamps installed during the previous refueling outage | | (3/99). The MNSA clamps were installed on previously identified leaking | | nozzles. The leakage from the clamps constitutes a reinitiation of RCS | | pressure boundary leakage, which is a degradation of the RCS pressure | | boundary." | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+
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