Event Notification Report for October 18, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/17/2000 - 10/18/2000 ** EVENT NUMBERS ** 37401 37429 37433 37434 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37401 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/02/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:52[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/02/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:41[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/17/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JOHN MADERA R3 | | DOCKET: 0707002 |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HISTORICAL INFORMATION REGARDING A FAILURE TO COMPLETE X-333 LOW ASSAY | | WITHDRAWAL (LAW) COMPRESSOR PYROTRONIC SMOKE DETECTION SYSTEM ENGINEERING | | MODIFICATIONS AS DESIGNED (24-hour report) | | | | The following text is a portion of a facsimile received from Portsmouth | | personnel: | | | | "The engineering modifications to the X-333 LAW compressor Pyrotronic smoke | | detection system were not completed as designed. The modifications were | | intended to cause the safety system to alarm with only one smoke head firing | | instead of requiring two smoke heads to activate the alarm. The | | investigation into this matter was completed 10/02/00 at 1541 [hours]. The | | investigation identified that on one occasion, a LAW station compressor was | | in an applicable operating mode where the Pyrotronic smoke detection safety | | system was required to be operable and one of the heads was in fact | | inoperable making the system inoperable. Operations personnel did post an | | immediate smoke watch to maintain [Technical Safety Requirement (TSR)] | | compliance." | | | | "This finding is reportable to the NRC as a 24-hour event due to the fact | | the equipment was required by the TSR to be available and operable and | | should have been operating, and no redundant equipment was available to | | provide the required safety function." | | | | "Note: The engineering modifications were completed 10/01/00, and | | applicable [post-maintenance tests were completed satisfactorily]." | | | | It was reported that the inoperable head that was identified to be | | inoperable on 10/01/99, but this issue was not identified until the | | investigation was completed today (10/02/00) at 1541 hours. It was also | | reported that there was nothing unusual or misunderstood and that all | | systems functioned as required. | | | | NOTE: The X-333 building LAW station was reported to be a UF6 withdrawal | | station. | | | | Portsmouth personnel have notified the NRC resident inspector and plan to | | notify the Department of Energy site representative. | | | | * * * UPDATE 2125EDT ON 10/17/00 FROM KURT SISLER TO S. SANDIN * * * | | | | "NRA [Nuclear Regulatory Affairs] has reviewed the basis for the above NRC | | event notification and determined that this event can be retracted. The | | following provides the basis for this conclusion. | | | | "On October 2, 2000, the NRC was notified of a design problem which caused | | the LAW UF6 Smoke Detection system to be inoperable at a time when the | | system was required to be operable in accordance with TSR 2.5.3.3 (outside | | each compressor housing one smoke detector must be operable in modes II or | | III). The design problem resulted from the fact that Pyrotronics smoke | | detectors were installed in series. In this configuration, the failure of | | one detector could prevent the redundant detector from activating the alarm | | contacts in the event of a UF6 release. | | | | "A review was conducted by engineering to determine if LAW had ever been in | | Mode II or III with a failed outside compressor housing Pyrotronics | | detector. The review identified one occasion in the past where this was the | | case. As a result of the series configuration, the remaining Pyrotronics | | detector would not have been able to perform its design function at that | | time. Although there were CADP smoke detectors available for this area, | | operating procedures did not recognize that CADP smoke detectors provided | | backup to the Pyrotronics detectors. Based on the fact that the Pyrotronics | | smoke detection system was inoperable and no redundant equipment was | | available to perform the required safety function, the PSS notified the NRC | | of this past safety system failure. This safety system failure was | | documented on Problem Report PR-PTS-00-04649. | | | | "A followup evaluation by engineering confirmed that there was an outside | | compressor housing CADP smoke detector available and operable at the time | | the event occurred. The evaluation also confirmed that the SAR, Table | | 3.2-4B, recognizes that CADP detectors provide smoke detection for outside | | compressor enclosures. Engineering also confirmed that CADP detectors were | | available and operable in all cases since March 3,1997, when any single | | Pyrotronics head was inoperable. | | | | "Based on the above, redundant outside compressor housing CADP smoke | | coverage was available at all times when the Pyrotronics heads were | | inoperable and this event may be retracted." | | | | The NRC resident inspector was informed. Notified R3DO(Lanksbury) and | | NMSS(Holonich). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37429 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 10/14/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 05:14[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 10/14/2000| +------------------------------------------------+EVENT TIME: 03:24[CDT]| | NRC NOTIFIED BY: WILLIAM GREEN |LAST UPDATE DATE: 10/18/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVE LOVELESS R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM DUE TO A MAIN GENERATOR TRIP FOR UNKNOWN REASONS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 0324 [CDT], a reactor scram occurred due to a main generator trip. | | Group isolations 2, 3[, and] 6 occurred due to low reactor water level. The | | lowest [reactor water] level recorded was -20 inches on [the] wide range | | level recorder. Reactor water level recovered, and both reactor [feedwater] | | pumps tripped on high reactor water level. Group isolations have been | | verified and reset. [The] 'A' reactor [feedwater] pump has been returned to | | service and is being used to control water level. [High pressure coolant | | injection] and [reactor core isolation cooling] did not inject and were not | | needed to control reactor water level. The plant will be placed in Cold | | Shutdown. The electrical grid is stable." | | | | The licensee stated that all control rods fully inserted and that all | | systems functioned as required. The licensee also stated that alternate rod | | insertion initiated as a result of high pressure due to the transient. The | | highest pressure observed was 1,085 psi. None of the relief valves lifted, | | and the main steam isolation valves remained open throughout the event. | | Steam is currently being dumped to the condenser. | | | | In addition, the licensee stated that the cause of the main generator trip | | is currently under investigation. There were no related surveillance or | | maintenance activities ongoing at the time of the event. | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE on 10/18/00 at 0428 ET by Myers taken by MacKinnon * * * | | | | A detailed review of the plant response to the scram has been conducted. | | This review indicated the following clarification to the initial report are | | needed: | | | | Alternate Rod Insertion initiated on low level, rather than high pressure. | | The low level was not in long enough to trip the Recirculation pumps. The | | pumps trip after a 9 second delay, and the low level signal was only in for | | ~ 7 seconds. | | | | Initial indications were that reactor pressure had reached 1085 psig, based | | on pressure recorder LRPR97, the highest reading of the pressure recorders. | | Additional pressure recorders and the plant computer indicate pressure | | reached a maximum of ~ 1068 psig. Evaluation of the recorder indicates it | | is in calibration, and the "overshoot" of indicated pressure is due to | | mechanical characteristics of the recorder linkage. NRC R4DO (John Pellet) | | notified. | | | | The NRC Resident Inspector was informed of this update by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37433 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 10/17/2000| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 12:13[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 10/16/2000| +------------------------------------------------+EVENT TIME: 18:30[CDT]| | NRC NOTIFIED BY: DARYL NOHR |LAST UPDATE DATE: 10/17/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N Y 95 Power Operation |95 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR FITNESS-FOR-DUTY REPORT INVOLVING A CONTRACT SUPERVISOR | | | | A contract supervisor was determined to be under the influence of alcohol | | during a test for cause. The individual's access to the plant has been | | terminated. Contact the Headquarters Operations Officers for additional | | details. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37434 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 10/17/2000| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 22:15[EDT]| | RXTYPE: [3] CE |EVENT DATE: 10/17/2000| +------------------------------------------------+EVENT TIME: 19:53[CDT]| | NRC NOTIFIED BY: BRUCE PROCTOR |LAST UPDATE DATE: 10/17/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INDICATION OF RCS PRESSURE BOUNDARY LEAKAGE DISCOVERED DURING INSPECTION OF | | PRESSURIZER HEATER SLEEVE | | | | "A SMALL AMOUNT OF BORIC ACID WAS DISCOVERED IN THE AREA AROUND PRESSURIZER | | HEATER SLEEVE NUMBER F4 DURING A BARE METAL INSPECTION PERFORMED ON | | 10/17/00. THE BORIC ACID IS BELIEVED TO BE EVIDENCE OF PRIMARY STRESS | | CORROSION CRACKING OF THE INCONEL ALLOY 600 HEATER SLEEVE. THE BORIC ACID | | IS BELIEVED TO BE EVIDENCE OF REACTOR COOLANT SYSTEM (RCS) PRESSURE BOUNDARY | | LEAKAGE, CONSTITUTING A DEGRADATION OF THE RCS PRESSURE BOUNDARY." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021