Event Notification Report for October 17, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/16/2000 - 10/17/2000 ** EVENT NUMBERS ** 37432 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37432 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 10/16/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 12:43[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 10/16/2000| +------------------------------------------------+EVENT TIME: 09:21[CDT]| | NRC NOTIFIED BY: JIM SCHOTTEL |LAST UPDATE DATE: 10/16/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL SCRAM INSERTED PRIOR TO REACHING AUTOMATIC SCRAM SETPOINT FOLLOWING | | REPLACEMENT OF ATWS POWER SUPPLIES | | | | "Clinton Power Station is currently in day 3 of refueling outage RF-7. At | | 09:20 I&C Technicians were performing PMs (PCIMSA017 and PCIMSA019) which | | replaced power supplies in the Anticipated Transient Without Scram system | | (ATWS). During reenergization of the ATWS system, the ARI (Alternate Rod | | Insertion) initiation alarm occurred. The 'A' RO observed Scram Discharge | | Volume Vents and Drains closing and a rising level in the Scram Discharge | | Volume (SDV). At 09:21 a manual scram was inserted at approximately 11 | | gallons SDV level prior to reaching the automatic scram setpoint of 19.6 | | gallons Scram Discharge Volume level. | | | | "Prior to this event Reactor Water Level was at 195 inches. The extra input | | of water into the reactor due to this scram caused a level rise to 200 | | inches. The Reactor Operators raised Reactor Water Cleanup letdown rate from | | the RPV to bring level back to the preferred range of 190 - 200 inches. | | | | "Investigation has revealed that reenergizing the ATWS instrumentation | | causes actuation of the ATWS trip system." | | | | There was no rod motion since all rods were fully inserted prior to the | | event. The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
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