Event Notification Report for September 26, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/25/2000 - 09/26/2000 ** EVENT NUMBERS ** 37374 37375 37376 37377 37378 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37374 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 09/25/2000| |LICENSEE: ARIAF & KEZAR INC |NOTIFICATION TIME: 09:14[EDT]| | CITY: SAN ANTONIO REGION: 4 |EVENT DATE: 09/25/2000| | COUNTY: STATE: TX |EVENT TIME: 07:30[CDT]| |LICENSE#: L04964-001 AGREEMENT: Y |LAST UPDATE DATE: 09/25/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHUCK CAIN R4 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: OGDEN (FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TEXAS DEPARTMENT OF HEALTH WAS NOTIFIED BY ONE OF THEIR LICENSEES OF A | | STOLEN TROXLER GAUGE IN BROWNSVILLE, TEXAS | | | | A Troxler Model 3430, Serial No. 31532, sources: 8 millicurie Cs-137, Serial | | No. 750-6340; and 40 millicurie Am-241 /Be, Serial No. 47-28154 was | | apparently stolen from the back of a company truck at an overnight lodging | | in Brownsville Texas. The operator/driver discovered the theft between 7:30 | | a.m. and 8:00 a.m. this morning. The security chains in the bed of the truck | | had been cut. The gauge and the operators tool box were stolen. A police | | report has been filed with the Brownsville Police Department. The gauge was | | to be used at a temporary jobsite today. The owner of the stolen gauge is a | | Texas Licensee, L04964-001. The licensee is considering offering a reward | | for return of the gauge. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37375 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 09/25/2000| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 11:18[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/25/2000| +------------------------------------------------+EVENT TIME: 10:33[EDT]| | NRC NOTIFIED BY: HOWARD |LAST UPDATE DATE: 09/25/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 78 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP FROM 78% POWER DUE TO A LOW STEAM GENERATOR LEVEL | | | | The event was initiated at 1030 EDT when the "1A" main feedwater pump | | tripped. An automatic runback [from 100%] to 75% turbine power occurred, | | however, the "1B" main feedwater pump did not automatically speedup to full | | load as designed. An attempt to manually load the "1B" main feedwater pump | | was ineffective and a trip occurred as a result of a low steam generator | | level. All rods fully inserted, no ECCS initiated and no safety valves | | lifted. They are investigating the cause of this event. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37376 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 09/25/2000| | UNIT: [1] [2] [] STATE: MD |NOTIFICATION TIME: 12:47[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 09/25/2000| +------------------------------------------------+EVENT TIME: 08:15[EDT]| | NRC NOTIFIED BY: O'MEARA |LAST UPDATE DATE: 09/25/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE TECHNICAL REQUIREMENT 24 HOUR REPORT | | | | The licensee, in accordance with their Technical Review (Requirement) Manual | | 15.7.5.c, reported that one of their diesel fire pumps and one pretreatment | | water storage tank (# 12) was removed from service for planned maintenance. | | The diesel fire pump was taken out of service to install a flange to isolate | | the pretreatment water storage tank for maintenance. The pump being | | out-of-service and having one of two sources of water out-of-service | | prompted the 24 hour report. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | See similar Event # 37367 reported on 09/22/00. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37377 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 09/25/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 14:30[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/25/2000| +------------------------------------------------+EVENT TIME: 14:00[EDT]| | NRC NOTIFIED BY: UNDERWOOD |LAST UPDATE DATE: 09/25/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 95 Power Operation |95 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Unescorted access granted inappropriately. Immediate compensatory measures | | taken upon discovery. | | | | Refer to the HOO Log for additional details. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37378 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 09/26/2000| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 01:23[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/26/2000| +------------------------------------------------+EVENT TIME: 00:43[EDT]| | NRC NOTIFIED BY: THOMAS MARSHALL |LAST UPDATE DATE: 09/26/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |THOMAS DECKER R2 | |10 CFR SECTION: |BILL BATEMAN NRR | |AAEC |JOSEPH GIITTER IRO | | |CANUPP FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 MET THE CONDITIONS FOR AN UNUSUAL EVENT BASED ON RCS LEAKAGE > 25 GPM | | WHILE IN MODE 4. | | | | "While placing the '1A' RHR Pump in service for shutdown cooling, the Unit | | experienced an RCS leak of approximately 45 gpm. It is believed that the | | cause of the leak is a relief valve that lifted and failed to reseat. The | | leak was isolated from the RCS when the RHR suction valves from the RCS | | (1-FCV-74-1 and 1-FCV-74-2) were closed. The leak lasted approximately 10 | | minutes. | | | | "According to the Plant's Radiological Emergency Plan, the conditions for a | | Notification of Unusual Event (NOUE) were met, but before it could be | | declared the leak was isolated, so an NOUE was not declared but will be | | reported." | | | | The RCS which leak occurred at 0002EDT was terminated at 0012EDT (10 | | minutes). Operators estimated the leakage at 45 gpm based on the change in | | PRT (pressurizer relief tank) level. The two relief valves involved are | | 1-VLV-63-626 and 1-VLV-63-627 with setpoints of approximately 600 psig. RCS | | pressure was 345 psig when the RHR suction valves were opened. The RHR | | pumps develop approximately 180 psig which combined with the 345 psig RCS | | pressure (inlet) indicated about 525 psig RHR discharge pressure in the | | control room. Both trains of RHR have been declared inoperable pending | | identification and correction of the problem. Decay heat is current being | | removed by the main condenser through the steam dumps using both | | motor-driven auxiliary feedwater pumps. The licensee has no plans for a | | press release at this time and did inform the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021