Event Notification Report for September 22, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/21/2000 - 09/22/2000 ** EVENT NUMBERS ** 37251 37300 37304 37330 37358 37359 37360 37361 37362 37363 37364 37365 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37251 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 08/23/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 18:22[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/23/2000| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: BOB KIDDER |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 98 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - ECC SYSTEM MOV MAY NOT CLOSE DURING A LOCA AND A LOOP AS REQUIRED - | | | | While reviewing motor operated valve (MOV) data from December, 1999, plant | | staff personnel identified an error in the analyzed data for the closing | | torque for an MOV in the Emergency Closed Cooling (ECC) System that is | | required to close during a Loss of Coolant Accident (LOCA) and a Loss of | | Offsite Power (LOOP). | | | | The valve, #OP42-F0295B, isolates the ECC System from the Nuclear Closed | | Cooling (NCC) Water System. A second isolation valve, #OP42-F0290, was | | subsequently found to have insufficient data to ensure that it alone would | | have provided the required isolation. Failure of both valves to potentially | | not close completely could cause the ECC System to transfer the system's | | cooling water inventory via the NCC Water System to the Intermediate | | Building resulting in the loss of cooling capability of the ECC System. This | | would result in the loss of cooling capability for the systems required to | | support the Residual Heat Removal (RHR) 'B' and 'C' Subsystems. The #F0290 | | valve has been successfully tested to ensure that it has adequate torque to | | close under accident conditions; however, there is insufficient leakage test | | data available on this valve at this time. Therefore, assuming that valve | | #F0290 leaks and valve #F0295B does not fully close, a total loss of | | inventory would potentially occur for Division 2. | | | | Therefore, this condition is being conservatively reported to the NRC as a | | loss of safety function during a past outage which removed RHR 'A' from | | service, until further evaluation is completed. | | | | Valve #OP42-F0295B has been electrically closed under static flow conditions | | to ensure continued operability of the ECC System. | | | | Licensee planned actions include further evaluation of past test data or | | performance of a specific leak test on valve #OP42-F0290 and further | | evaluation of data on valve #OP42-F0295B. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * RETRACTED AT 1622 EDT ON 9/21/00 BY MICHAEL McFARLAND TO FANGIE JONES | | * * * | | | | "A 10 CFR 50.72, four (4) hour non-emergency notification was initially made | | on 8-23-2000, due to Emergency Closed Cooling Loop B inoperability | | subsequent to valve OP42-F0295B inoperability, due to inadequate closing | | torque under dynamic flow conditions concurrent with an outage on the | | alternate, Division 1, equipment. it was indeterminate at that time if | | sufficient torque existed for the valve to close under accident conditions. | | | | "Subsequent to the event notification, the valve has been tested under | | dynamic flow and reevaluated. This information has resulted in a | | determination that the OP42-F0295B valve has been, and continues to be, | | operable under both normal and accident conditions. | | | | "Since the valve was determined to have been continuously operable, no | | Technical Specification Required Actions were exceeded and both loops of ECC | | remained operable. This event was determined not reportable and ENF 37251 is | | retracted." | | | | The licensee notified the NRC Resident Inspector. The R3DO (Bruce Burgess) | | was notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37300 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/09/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:21[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/08/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 20:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/21/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |GARY SHEAR R3 | | DOCKET: 0707002 | | +------------------------------------------------+ | | NRC NOTIFIED BY: JEFF CASTLE | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT INVOLVING SAFETY SYSTEM ACTUATION | | | | "On 9/8/2000 at 2000 hours a safety system actuation occurred in the X344 | | building. Autoclave #4 was in Mode II 'Heating' when the High Condensate | | Level Shutoff safety system actuated. Per TSR 2.1.3.7, the autoclave was | | placed in Mode VII 'Shutdown', a mode in which the High Condensate level | | Shutoff system is not required, and declared inoperable. This is being | | reported as a valid safety system actuation. An engineering evaluation has | | been initiated to review the system conditions that surrounded the actuation | | of the safety system." | | | | Operations notified both the NRC resident inspector and DOE site | | representative. | | | | * * * RETRACTED AT 2323 EDT ON 9/21/00 BY ERIC SPAETH TO FANGIE JONES * * * | | | | "RETRACTION: On 09/21/00, the Plant Shift Superintendent retracted the | | above Event. At the time of the High Condensate Level Shutoff (HCLS) system | | actuation, the autoclave was being cycled on and off in accordance with the | | applicable procedure for heating a Russian cylinder. Follow up investigation | | by engineering and operations has determined the HCLS actuation occurred | | while AC #4 was in Mode VII 'Shutdown'. | | | | "Discussions with building supervision and the operator who witnessed the | | HCLS actuation revealed the AC #4 had been shutdown as part of the on/off | | heating cycle before the actuation occurred. Based on the configuration of | | AC #4 at the time, the AC would have been in Mode VII 'Shutdown'. | | | | "Since the HCLS system is not required to be operable in Mode VII | | 'Shutdown', the HCLS system actuation was invalid, and is not reportable in | | accordance with 10CFR76.120(c)(2). Accordingly, this event is being | | retracted." | | | | The plant has informed the NRC Resident Inspector. The R3DO (Bruce Burgess) | | and NMSS EO (John Greeves) has been notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37304 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: LAKEHEAD PIPE LINE CO., INC |NOTIFICATION DATE: 09/11/2000| |LICENSEE: LAKEHEAD PIPE LINE CO., INC |NOTIFICATION TIME: 11:20[EDT]| | CITY: LEWISTON REGION: 3 |EVENT DATE: 09/11/2000| | COUNTY: STATE: MI |EVENT TIME: 08:00[EDT]| |LICENSE#: 22-26732-01 AGREEMENT: N |LAST UPDATE DATE: 09/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MARK RING R3 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT POLLOCK | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REPORT INVOLVING POSSIBLE EQUIPMENT SAFETY DEVICE FAILURE | | | | THE LAKEHEAD PIPE LINE RADIATION SAFETY OFFICER (RSO), WAS INFORMED AT 0800 | | ON 9/11/00 THAT THE COUNTER ON A NUCLEAR DENSITY GAUGE HAD STOPPED WORKING | | SOMETIME IN MAY OF THIS YEAR AT THEIR LEWISTON STATION LOCATED IN LEWISTON, | | MICHIGAN. THE SOURCE IS IN THE SHIELDED AND LOCKED POSITION. THE DEVICE IS | | A MODEL 7400 MANUFACTURED BY BERTHOLD SYSTEMS CONTAINING A 350 MILLICURIE | | CS-137 SOURCE. | | | | * * * RETRACTED AT 1601 EDT ON 9/21/00 BY ROBERT POLLOCK TO FANGIE JONES * * | | * | | | | After discussion with NRC Region 3 (Geoffrey Wright), it was determined that | | this event was not reportable as the source was not involved, safely stored | | at all times, and the problem was only with the electronics. This event | | notification is retracted. | | | | The R3DO (Bruce Burgess) and the NMSS EO (John Greeves) has been informed. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37330 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 09/15/2000| | UNIT: [2] [] [] STATE: PA |NOTIFICATION TIME: 17:57[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 09/15/2000| +------------------------------------------------+EVENT TIME: 15:05[EDT]| | NRC NOTIFIED BY: JESSE JAMES |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES TRAPP R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 M/R Y 15 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUALLY SCRAMMED THE REACTOR AFTER ENTERING THE RESTRICTIVE AREA OF THE | | POWER TO FLOW MAP. | | | | On September 15, 2000 at Peach Bottom Atomic Power Station, Unit 2 was | | manually scrammed per operating procedure during turbine testing in | | preparation for the refuel outage. | | | | The manual scram was due to entering restricted area of the power to flow | | map from Technical Specification 3.4.1, after the trip of the "2B" | | recirculation pump. All rods fully inserted and the reactor was shutdown. | | Reactor level during the scram lowered to 0" and a Group II and III primary | | and secondary containment isolation was received. The isolations functioned | | as designed. The plant is stable in hot shutdown with the main condenser as | | a heat sink and the feedwater system is in service for level control. No | | radioactive release or Emergency Core Cooling System injection occurred | | during the scram. | | | | The turbine was tripped in accordance with the refuel outage plan when the | | recirculation pump tripped. The plan was to perform turbine testing and | | then to manually scram the reactor at the same power level. | | | | The reactor was manually scrammed less than one minute after entering the | | restricted area of the power to flow map. No power oscillations were seen. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * RETRACTED AT 1715 EDT ON 9/21/00 BY ANDREW WINTER TO FANGIE JONES * * | | * | | | | "On September 15, 2000 PBAPS reported that Unit 2 was manually scrammed in | | accordance with operating instructions during turbine testing. The report | | identified that the manual scram was initiated based on entering the | | restricted area of the power to flow map after the tripping of the 2B | | Recirculation Pump. This notification is being retracted based on the | | following: | | | | "NUREG 1022 Revision 1 specifically states that 'The Commission is | | interested both in events where an ESF was needed to mitigate the | | consequences (whether or not the equipment performed properly) and events | | where an ESF actuated unnecessarily....This indicates an intent to require | | reporting actuations of features that mitigate the consequences of | | significant events.' Therefore, the following is an analysis of these two | | underlying reasons for reporting ESF actuations: | | | | 1. The need for the ESF to mitigate the consequences of an event: | | | | The September 15, 2000 PBAPS manual scram was initiated because the plant | | operator made a conservative decision in accordance with station procedures | | to initiate a reactor scram. At the time this decision was made, the plant | | conditions were approximately 16 percent power and 24 percent core flow. | | Although this condition is close to an operational limit conservatively | | established by the licensee and the operator made the correct decision to | | commence the plant shutdown, the ESF actuation was not necessary to mitigate | | the consequences of this evolution. Moreover, plant conditions were not | | changing in a direction that would have required the manual scram to | | mitigate the consequences of significant events. | | | | 2. Events where an ESF actuated unnecessarily: | | | | The actuation of a manual scram and the subsequent PCIS Group II and Ill | | actuations were part of a preplanned shutdown for the commencement of the | | PBAPS Unit 2's thirteenth refueling outage (2R13) and were necessary to | | complete the plant shutdown. The decision to insert the manual scram in | | accordance with station procedures, resulted in the preplanned shutdown | | commencing slightly early. Therefore, the ESP did not actuate unnecessarily | | since it was already planned to shutdown the plant by inserting a manual | | scram. | | | | "Therefore, based on the above discussion, this event is not reportable | | because the manual scram resulted from and was, in accordance with the | | licensee's procedure, and part of a preplanned sequence of reactor | | operation." | | | | The licensee notified the NRC Resident Inspector. The R1DO (William Ruland) | | has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37358 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 09/20/2000| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 17:51[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 09/20/2000| +------------------------------------------------+EVENT TIME: 16:05[CDT]| | NRC NOTIFIED BY: RYAN RODE |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT OUTSIDE 10 CFR PART 50 APPENDIX R DESIGN BASIS DUE TO PROCEDURAL | | ISSUES | | | | "During the final review of the new Appendix R rebaselining project, it was | | discovered that the refueling water storage tank (RWST) inventory could be | | lost if AOP 10A, 'Safe Shutdown-Local Control' and AOP 10B 'Safe to Cold | | Shutdown in Local Control' were performed as written. The postulated event | | occurs during an Appendix R fire where SI-851(RHR pump suction from | | containment sump B) encounters a spurious open signal, causing the RWST to | | drain via backflow into containment. The procedures do not address this | | potential failure early enough into the event to preclude a potential loss | | of RWST inventory. This puts Point Beach Nuclear Power Plant outside of its | | design basis because 10CFR50 Appendix R Section III.L.2.b performance goals | | might not be met for the above scenario." | | | | The NRC resident inspector will be informed of this notification by the | | licensee. | | | | * * * UPDATE AT 1424 EDT ON 9/21/00 BY RYAN RODE TO FANGIE JONES * * * | | | | "This is an update to Event Notification 37358. That notification reported a | | procedural deficiency involving AOP 10A, 'Safe Shutdown - Local Control' and | | AOP 10B. 'Safe to Cold Shutdown in Local Control,' in the event of a | | postulated Appendix R fire which results in a spurious open signal to the | | SI-851A/B valves, 'RHR Pump Suction from Containment Sump B.' This | | notification discussed the concern with this spurious valve opening | | occurring during AOP 10A, which was a potential loss of RWST inventory to | | the containment sump through the SI-856A/B, 'RHR Pump Suctions From RWST,' | | valves. | | | | "Although appropriately identified in the License's condition report, this | | notification did not include a discussion of the concern identified during | | conduct of procedure AOP 10B. Specifically, since no action is specified to | | verify that the SI-851 A/B valves are closed in either AOP 10A or AOP 10B, | | in the event of the Appendix R fire which results in the spurious opening of | | those valves, when the RHR system is aligned for normal recirculation during | | the cooldown, the RCS inventory could be reduced by leakage through the open | | SI-851 valve to the containment sump. As mentioned in the original event | | notification, 10 CFR 50 Appendix R Section III.L.2.b requires the | | performance goal for maintaining RCS level within the level indication in | | the pressurizer be met. The procedures as written do not assure this | | performance goal would be met and are reported as a potential condition that | | is outside the Appendix R design basis." | | | | The licensee notified the NRC Resident Inspector. The R3DO (Bruce Burgess) | | has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37359 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 09/21/2000| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 06:51[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 09/21/2000| +------------------------------------------------+EVENT TIME: 06:00[EDT]| | NRC NOTIFIED BY: LUCAS |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |AUNA 50.72(b)(1)(ii)(A) UNANALYZED COND OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 96 Power Operation |96 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TURBINE DRIVEN EMERGENCY FEED PUMP DISCHARGE VALVE WAS DISCOVERED LOCKED. | | | | The turbine driven Emergency Feed pump discharge valve (XV601036-EF) was | | discovered locked closed instead of locked open as required. This condition | | rendered the turbine driven Emergency Feed pump inoperable. The valve was | | last operated on 8/4/00. During the period when the discharge valve was | | closed, both diesels had been removed from service for maintenance. The "A" | | D/G was removed from service between 9/5/00 - 9/6/00 and the "B" D/G was | | removed from service between 9/19/00 - 9/20/00. The licensee is | | investigating the cause. | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37360 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MARYLAND DEPART. OF THE ENVIRONMENT |NOTIFICATION DATE: 09/21/2000| |LICENSEE: D W KOZERA INC |NOTIFICATION TIME: 09:48[EDT]| | CITY: BALTIMORE REGION: 1 |EVENT DATE: 09/20/2000| | COUNTY: STATE: MD |EVENT TIME: 14:30[EDT]| |LICENSE#: MD0514901 AGREEMENT: Y |LAST UPDATE DATE: 09/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM RULAND R1 | | |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MANLEY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST TROXLER MOISTURE DENSITY GAUGE REPORTED TO THE MARYLAND DEPARTMENT OF | | THE ENVIRONMENT (MDE) | | | | Maryland licensee, D W Kozera Inc. of Baltimore, Md. lost a Troxler moisture | | density gauge model 3430 serial # 25607 in Adamstown, Md. The gauge was | | missing from the back of a flat bed truck , which had its tailgate down, | | that was being driven around the Greenhill Manor Residential subdivision(New | | Design Rd & Union Ridge Rd in Fredrick City). The gauge, which apparently | | fell out of the back of the truck, was not in its case and the source rod | | was not padlocked. The source (7.2 millicuries of cesium 137 and 39.7 | | millicuries of americium 241), as far as they know, was in the shielded | | position and has not been found. MDE has conducted an initial investigation | | and it appears that they may issue a press release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37361 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 09/21/2000| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 16:07[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 09/21/2000| +------------------------------------------------+EVENT TIME: 15:30[EDT]| | NRC NOTIFIED BY: JOHN POPIELARSKI |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM RULAND R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Cold Shutdown |0 Cold Shutdown | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE EMERGENCY SIRENS IN DEGRADED CONDITION | | | | "On September 21, 2000 at 1530, it was identified that at least 17 of Peach | | Bottom's 97 Emergency Offsite Sirens were in a degraded condition. The exact | | cause of the degraded sirens is not known at this time, but the ability of | | the licensee to detect the degraded sirens has been compromised due to poor | | maintenance practices. A plan is being developed and implemented to repair | | the degraded sirens and appropriate interim compensatory measures are being | | put in place to compensate for the degraded condition." | | | | An investigation is underway into this matter. The contractor responsible | | for the siren maintenance has no other responsibilities on site. | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37362 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 09/21/2000| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 16:15[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 09/21/2000| +------------------------------------------------+EVENT TIME: 11:38[CDT]| | NRC NOTIFIED BY: DONALD CHASE |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 | |10 CFR SECTION: | | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBILITY THAT BOTH DIVISION 1 AND 2 DIESEL GENERATORS WERE INOPERABLE FOR | | 9 HOURS | | | | "This condition deals with a past Reportability issue. During a condition | | report review for Functional Failure/Maintenance Preventable Functional | | Failure determination (FF/MPFF), River Bend has determined that both Standby | | Diesel Generators may have been inoperable at the same time. | | | | "A failure in a light socket related to the Division I Diesel Generator | | created a functional failure in that during a seismic event, the breaker | | logic for the Division I diesel generator output breaker could have been | | affected in such a way that the breaker would not close. The failed light | | socket was identified and corrected on 9/5/00 as part of work to replace the | | light bulb. Since the MAI on the light bulb failure was written on 8/22/00, | | it is assumed that the socket failure occurred at that time. | | | | "During the same time period, a lube oil leak developed on the Division II | | oil supply which has been determined to be a functional failure. The damaged | | oil line was replaced on 8/30/00. | | | | "Therefore, based on the functional failure determinations, there is an | | overlapping period of approximately 9 hours that the Division I and II | | diesel generators may not have been capable of performing their design bases | | function. | | | | "This report is being made based on the information available at this time. | | River Bend will continue to evaluate the condition associated with the | | potential Division I inoperability and will assess the reportability of this | | condition further based on the results of that evaluation." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37363 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 09/21/2000| | UNIT: [] [2] [3] STATE: CA |NOTIFICATION TIME: 19:09[EDT]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 09/19/2000| +------------------------------------------------+EVENT TIME: 07:30[PDT]| | NRC NOTIFIED BY: CLAY WILLIAMS |LAST UPDATE DATE: 09/21/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KRISS KENNEDY R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO A SULFURIC ACID LEAK CONTAINED ON SITE | | | | "This 4-hour telephone notification is being provided in accordance with | | 10CFR50.72(b)(2)(vi) for notification of other government agencies. For the | | event below, on September 19, 2000, at 0920 PDT, SCE notified the Department | | of Environmental Health and the Office of Emergency Services (OES Incident | | number 00-4232). This notification was delayed due to an internal | | miscommunication. | | | | "On September 19, 2000, at about 0730 PDT, control room personnel were | | notified of a sulfuric acid leak from the High Flow Makeup Demineralizer | | Bulk Acid Storage Tank. The leak was from a gasket located between level | | transmitter 2/3LT5045 and isolation valve AST-38. The isolation valve was | | closed and the leak stopped. All acid (estimated to be about 650 gallons) | | was contained within the tank's bermed area and then routed to the waste | | neutralization sump. The entire sump contents (about 2,500 gallons of | | sulfuric acid and water) were removed for disposal off-site. This occurrence | | was not a significant impact to the environment and did not hamper site | | personnel in the performance of their duties necessary for safe operation. | | | | "At the time of this occurrence, both Units 2 and 3 were operating at about | | 100 percent power; Unit 1 remains permanently defueled. SCE will notify the | | NRC resident inspectors about this notification and will provide them with a | | copy of this report." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37364 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 09/22/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 04:26[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/22/2000| +------------------------------------------------+EVENT TIME: 04:00[EDT]| | NRC NOTIFIED BY: HAMM/SCHALL |LAST UPDATE DATE: 09/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |THOMAS DECKER R2 | |10 CFR SECTION: |BILL BATEMAN NRR | |AAEC |JOSEPH GIITTER IRO | | |LUIS REYES R2 | | |HEYMAN FEMA | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FIRE IN THE PROTECTED AREA LASTING GREATER THAN 10 MINUTES RESULTING IN A | | REACTOR SCRAM. | | | | AN UNUSUAL EVENT WAS DECLARED @ 0400 DUE TO A FIRE IN THE MAIN TRANSFORMER | | THAT LASTED >10 MINUTES. OFF SITE FIRE DEPARTMENT WAS CALLED IN TO RESPOND | | AND THE FIRE WAS EXTINGUISHED WITHIN 14 MINUTES, HOWEVER THE PLANT STILL | | REMAINS IN THE UNUSUAL EVENT. A REACTOR SCRAM FROM 100% POWER OCCURRED | | FOLLOWING A MAIN TURBINE GENERATOR LOCKOUT WHICH RESULTED FROM THE | | TRANSFORMER FAILURE. THERE WERE SOME ERRONEOUS INDICATIONS OF CONTROL ROD | | POSITION, BUT ALL RODS APPEAR TO BE FULLY INSERTED. THERE WAS NO ECCS | | ACTUATION AND NO SAFETY RELIEF VALVES LIFTED DURING THIS EVENT. THE PLANT | | DID NOT LOSE OFFSITE POWER DUE TO THE AUTO TRANSFER FROM THE MAIN | | TRANSFORMER TO THE STARTUP AUXILIARY TRANSFORMER. THE DIESELS AUTOMATICALLY | | STARTED AND WERE STILL RUNNING AT THE TIME OF THIS REPORT. GROUP 2,6 AND 8 | | ISOLATIONS WERE ALSO RECEIVED. THERE WAS A PROBLEM WITH THE STARTUP LEVEL | | CONTROL VALVE WHEN THEY REESTABLISHED REACTOR FEED PUMP, VALVE DID NOT OPEN | | PROPERLY SO THEY HAD TO USE THE BACKUP PATH IN THE FEED SYSTEM. AS A | | RESULT OF THIS THE LEVEL WENT LOW ENOUGH TO RECEIVE A SECOND REACTOR SCRAM | | SIGNAL. THE CONDENSER IS BEING USED AS THE HEAT SINK AND THE PLANT IS | | STABLE. THE CAUSES FOR THE TRANSFORMER FIRE AND THE ERRONEOUS CONTROL ROD | | INDICATIONS ARE BEING INVESTIGATED. THERE HAVE BEEN NO INJURIES REPORTED | | AND IT IS NOT KNOWN AT THIS TIME IF A PRESS RELEASE WILL BE ISSUED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED. | | | | * * * UPDATE ON 9/22/00 @ 0528 BY HAMM TO GOULD * * * | | | | THE NOUE WAS TERMINATED AT 0512 DUE TO THE FIRE BEING COMPLETELY | | EXTINGUISHED. | | THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED. | | THE EO(BATEMAN), RDO(DECKER), FEMA (HEYMAN) AND IRO(GIITTER) WERE | | NOTIFIED. | | | | SEE EVENT # 37365. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37365 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 09/22/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 06:37[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/22/2000| +------------------------------------------------+EVENT TIME: 03:40[EDT]| | NRC NOTIFIED BY: SCHALL |LAST UPDATE DATE: 09/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD ESF ACTUATIONS DURING A REACTOR SCRAM | | | | A main turbine trip resulted in a reactor scram. As expected following the | | scram, reactor water level dropped to the actuation setpoint for Groups 2, 6 | | and 8 isolations. The main turbine trip apparently resulted from a fire in B | | main power transformer. The fire was reported to the control room at 0346. | | The site fire brigade responded and the fire was extinguished at 0402 using | | the automatic deluge system and fire hoses. Offsite fire department | | assistance was requested but was not needed to extinguish the fire. An | | Unusual Event was declared at 0400 in accordance with the plant's emergency | | procedures. The Unusual Event was terminated at 0512 based on the plant | | being in a stable condition. During the transient the startup level | | control did not control level in the automatic mode. Reactor level was | | controlled using a feedwater bypass valve. A second reactor scram signal | | was generated due a low reactor water level signal received while manual | | level control was being established, however all rods were already tully | | inserted. The plant emergency diesels started but did not load. Offsite | | power remained available throughout the event. The NRC Resident Inspector | | was notified. | | | | HOO Note: see event # 37364 | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021