Event Notification Report for September 14, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/13/2000 - 09/14/2000 ** EVENT NUMBERS ** 37312 37313 37314 37315 37316 37317 37318 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37312 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 09/13/2000| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 07:35[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 09/12/2000| +------------------------------------------------+EVENT TIME: 07:40[EDT]| | NRC NOTIFIED BY: WILLIAM HOFFNER |LAST UPDATE DATE: 09/13/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES TRAPP R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR FITNESS FOR DUTY REPORT | | | | A licensed operator was administered a for-cause breathalyzer test after | | observation by operating staff that the individual's breath smelled of | | alcohol. The operator was oncoming and was not allowed to take the watch. | | Operations management personnel directed that the individual be taken home | | pending management review of the situation. Corrective action for | | consideration of resumption of licensed duties will follow management's | | review. | | | | The licensee notified the NRC Resident Inspector and will notify the State | | of Connecticut. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37313 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 09/13/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 07:58[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 09/13/2000| +------------------------------------------------+EVENT TIME: 04:33[EDT]| | NRC NOTIFIED BY: MATT WALDECKER |LAST UPDATE DATE: 09/13/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES TRAPP R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC START OF THE HIGH PRESSURE CORE SPRAY PUMP | | | | The licensee reported that the high pressure core spray (HPCS) pump | | automatically started when the pump control switch was taken out of the | | "pull-to-lock" position. The HPCS system was out of service for maintenance | | at the time of the event and had been declared inoperable on 09/12/00 at | | 0520 EDT. The HPCS spray injection valve did not open, as it was | | deenergized closed. The divisional diesel generator did not start as it was | | configured in the maintenance mode. | | | | There was no impact on the plant. The plant is in cold shutdown with the | | mode switch in the refuel position. The cause of the actuation is unknown | | and an investigation is in progress. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37314 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 09/13/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 13:15[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 09/13/2000| +------------------------------------------------+EVENT TIME: 09:54[CDT]| | NRC NOTIFIED BY: OKOPNY |LAST UPDATE DATE: 09/13/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK RING R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE "2A" DIESEL GENERATOR WAS INADVERTENTLY STARTED BY THE UNIT OPERATOR | | | | Unit 2 was operating at 100% power. A Division 2 Residual Heat Removal | | (RHR) Surveillance was in progress, which required the "2A" Diesel Generator | | Cooling Water Pump to be started. The Unit Operator inadvertently placed the | | Control Switch for the "2A" Diesel Generator to START. The Unit Operator | | recognized the error and the Diesel Generator Control Switch was immediately | | placed in STOP. The "2A" Diesel Generator and | | Diesel Generator Cooling Water Pump switches are side by side on the panel. | | The Diesel Generator reached at Least 150 RPM as indicated by the Auto Start | | of the "2A" Diesel Generator Cooling Water Pump. The Diesel Generator was | | returned to a Standby Operable condition. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37315 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WNP-2 REGION: 4 |NOTIFICATION DATE: 09/13/2000| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 14:38[EDT]| | RXTYPE: [2] GE-5 |EVENT DATE: 09/13/2000| +------------------------------------------------+EVENT TIME: 11:19[PDT]| | NRC NOTIFIED BY: ARBUCKLE |LAST UPDATE DATE: 09/13/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT OUTSIDE DESIGN BASIS FOR CONTROL ROOM EMERGENCY FILTRATION SYSTEM | | UNFILTERED INLEAKAGE BASED UPON TRACER GAS TESTING - IMPACT ON CONTROL ROOM | | DOSE CONSIDERATIONS | | | | "During September 8 through 11, 2000, a series of special tests, using a | | tracer gas decay methodology, were performed to determine the total | | inleakage into the control room and the associated impact on control room | | dose. These tests were performed in support of a proposed Technical | | Specification amendment request that is in the process of being developed | | for removal of main steam leakage control system test requirements and | | resolution of a long-standing issue pertaining to secondary | | containment/standby gas treatment system performance, using alternative | | source term methodology. The testing was also performed in response to | | NRC-industry initiative efforts to resolve the generic issue of the validity | | of control room unfiltered air infiltration rate assumed by licensees in | | control room habitability assessments. | | | | "On September 13, 2000, test results were evaluated and a preliminary | | assessment shows the highest train measured unfiltered inleakage for the | | control room emergency filtration system, as determined by the tracer gas | | testing, to be 83 � 37 cfm. This is in excess of the current licensing and | | design basis limit of 10.55 cfm. The impact of this unfiltered inleakage | | increase on control room dose was evaluated and it was determined that the | | design basis thyroid dose of 30 rem to the control room operators would be | | exceeded during post-accident conditions. | | | | "A Follow-Up Assessment of Operability (similar to a Justification for | | Continued Operation) was prepared to allow continued plant operation in this | | condition. The operability determination, which was based upon an | | evaluation of control room dose for several accident scenarios, concluded | | that the as-found inleakage did not render the control room emergency | | filtration system inoperable (based upon 10CFR50, Appendix A, GDC 19). In | | addition, a follow-up interim compensatory measure to reduce the calculated | | control room thyroid dose below the 30 rem limit includes administration of | | potassium iodide in accordance with requirements contained in abnormal | | operating procedures. Final resolution of this issue will be addressed by | | implementation of alternative source term methodology at WNP-2 and as part | | of the proposed Technical Specification amendment request. A feasibility | | study, using alternative source term methodology, has shown that inleakage | | rates well in excess of 83 � 37 cfm (approximately 300 cfm) would result in | | control room doses below the regulatory limit. This is a design basis | | analysis issue and no plant hardware changes are required in the resolution | | of the problem. We are continuing to follow the NRC-industry initiative | | efforts to resolve generic issues related to control room habitability." | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37316 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF VIRGINIA HOSPITAL |NOTIFICATION DATE: 09/13/2000| |LICENSEE: UNIVERSITY OF VIRGINIA HOSPITAL |NOTIFICATION TIME: 16:39[EDT]| | CITY: CHARLOTTESVILLE REGION: 2 |EVENT DATE: 09/07/2000| | COUNTY: STATE: VA |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 09/13/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |STEPHEN CAHILL R2 | | |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PICCOLO | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE UNIVERSITY OF VIRGINIA HOSPITAL REPORTED A MEDICAL MISADMINISTRATION | | DURING BRACHYTHERAPY. | | | | A patient being treated for cervical cancer was given a higher dose (8 gray) | | instead of the prescribed dose (5 gray) due to human error resulting in the | | wrong dwell times being used. It appears there will be no adverse affects | | to the patient. The patient and the referring physician will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37317 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 09/13/2000| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 17:51[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 09/13/2000| +------------------------------------------------+EVENT TIME: 16:36[EDT]| | NRC NOTIFIED BY: MAY |LAST UPDATE DATE: 09/13/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES TRAPP R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM FROM 77% POWER FOLLOWING LOSS OF CONDENSER VACUUM | | | | This occurred when the plant lost condenser vacuum after the steam jet air | | ejector valves closed. This valve closure was the result of a blown valve | | indication light bulb being changed. The reactor was manually scrammed | | from 77% power when the vacuum reached 6.5" Hg and decreasing. After the | | reactor scram the reactor vessel water level dipped below 127"(as low as | | 121") initiating groups 2, 3, 4 and 5 isolations and start of the standby | | gas treatment system. All rods fully inserted, no ECCS injection occurred | | and no relief valves lifted. | | | | The NRC Resident Inspector will be informed | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37318 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ARIZONA RADIATION REGULATORY AGENCY |NOTIFICATION DATE: 09/13/2000| |LICENSEE: UNIVERSITY OF ARIZONA |NOTIFICATION TIME: 18:40[EDT]| | CITY: TUCSON REGION: 4 |EVENT DATE: 07/22/2000| | COUNTY: STATE: AZ |EVENT TIME: [MST]| |LICENSE#: 10-024 AGREEMENT: Y |LAST UPDATE DATE: 09/13/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GARY SANBORN R4 | | |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: GODWIN (VIA FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TRITIUM RELEASE FROM THE UNIVERSITY OF ARIZONA | | | | At approximately 10:30 AM, September 6, 2000, the Agency was advised by the | | Radiation Safety Officer of the University that a laboratory had reported | | approximately 100 microcuries of tritium had been picked up by the custodial | | staff. The University Radiation Control office commenced an investigation of | | the problem and on September 7, 2000 reported that approximately 31 | | millicuries of tritium may have been lost out of a fume hood stack. This | | release was confirmed on September 11, 2000. The release occurred around | | July 22 - 30, 2000. | | | | The University and the Agency continue to investigate this event. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021