Event Notification Report for September 7, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/06/2000 - 09/07/2000 ** EVENT NUMBERS ** 37253 37289 37293 37294 37295 37296 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37253 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 08/24/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 05:27[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 08/24/2000| +------------------------------------------------+EVENT TIME: 04:35[EDT]| | NRC NOTIFIED BY: SQUIRES |LAST UPDATE DATE: 09/06/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHRISTOPHER CAHILL R1 | |10 CFR SECTION: |CHARLES MILLER IRO | |AINT 50.72(b)(1)(vi) INTERNAL THREAT |TAD MARSH NRR | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |53 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SMOKE AND SMALL FLAMES FROM "B" REACTOR FEED PUMP (RFP) OUTBOARD BEARING. | | FIRE LESS THAN 15 MINUTES. | | | | Control room plant received a high bearing temperature alarm from the "B" | | RFP. Plant personnel were dispatched to investigate. Smoke and small flames | | were seen around the outboard bearing of "B" RFP. Onsite fire brigade was | | dispatched to extinguish the fire. Fire brigade was unsuccessful in | | extinguishing the fire using carbon dioxide. Fire was extinguished using a | | fire hose. No other electrical systems were wetted by the fire hose. | | Reactor power was reduced from 100% to approximately 53% power at which time | | the "B" RFP was taken out service. A reflash fire watch is stationed at the | | "B" RFP. Lagging has been removed from the RFP and the lagging where the | | smoke and fire issued from is oil soaked. Investigation of fire is in | | progress. Unnecessary personnel were evacuated from the area of the fire. | | "B" RFP is located in the Turbine Building lower level (252'). All | | Emergency Core Cooling Systems are fully operable except for HPCI (see event | | # 37252). Offsite electrical grid is stable. No offsite site help was | | needed. Fire lasted from 0435 ET until 0449 ET. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * RETRACTED AT 1348 EDT ON 9/6/00 BY BOB STEIGERWALD TO FANGIE JONES * * | | * | | | | "This notification retracts an earlier report made on 08/24/00, at 05:27 | | (EDT), per 10CFR50.72(b)(1)(vi). A fire was reported at the outboard bearing | | of the 'B' Reactor Feed Pump. The fire was minor in nature, limited to the | | 'B' feed pump room, extinguished within 15 minutes of discovery, and did not | | hamper the ability of personnel to perform safety-related activities | | affecting plant safety. Reactor power was reduced and the 'B' feed pump was | | removed from service. Therefore, this event notification is being | | retracted." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Anthony | | Dimitriadis) was notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37289 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 09/05/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 05:42[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/05/2000| +------------------------------------------------+EVENT TIME: 02:00[EDT]| | NRC NOTIFIED BY: R.T. ELLIOT |LAST UPDATE DATE: 09/06/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | "2B" AUXILIARY FEEDWATER (CA) PUMP RAN 2 HOURS AND 55 MINUTES BEFORE BEING | | DISCOVERED IT WAS OPERATING. STEAM GENERATORS WERE ISOLATED FROM THE AFW | | SYSTEM. | | | | At 0200 ET the "B" Train of the Solid State Protection System (SSPS) was | | deenergized for part of their refueling outage maintenance. When the SSPS | | was deenergized the blocks for the Main Feedwater Pump blocks cleared, which | | resulted in an automatic start signal to the "2B" AFW pump. The on shift | | reactor operator did not notice the "2B" AFW pump run light was on until | | 0455 ET due to refueling outage maintenance activities in Control Room. The | | "2B" AFW pump recirculated water to the Upper Surge Tank since the Steam | | Generators were isolated. No damage occurred to the AFW pump. The licensee | | is investigating this event. | | | | The NRC Resident Inspector will be notified of this event. | | | | * * * RETRACTED AT 1630 EDT ON 9/6/00 BY LARRY TUMBLESON TO FANGIE JONES * * | | * | | | | "Further investigation has determined that, prior to and during the | | automatic start, the 2B CA Pump had been properly removed from service. This | | was accomplished when valves that isolate flow from the pump to the Unit 2 | | Steam Generators were closed as a result of planned Unit 2 shutdown | | operations using plant procedures. In addition, the automatic start of the | | 2B CA Pump was not the result of a valid ESF actuation intended to mitigate | | the consequences of an event. Instead, the ESF actuation signal which | | started the pump upon reset of the SSPS relay was present because the MFP's | | were already off as a result of planned refueling outage shutdown | | operations. | | | | "Based upon the above, the September 5, 2000, automatic start of the 2B CA | | Pump occurred as a result of an invalid ESF actuation signal received while | | the pump was properly removed from service. Consequently, this is not | | reportable under the requirements of 10 CFR 50.72(b)(2)(ii) - Actuation of | | An Engineered Safety Feature (ESF) and NRC Notification 37289 is retracted. | | | | "The Resident Inspector has been notified." | | | | The R2DO (Mark Lessor) has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37293 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 09/06/2000| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 12:13[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/06/2000| +------------------------------------------------+EVENT TIME: 08:45[CDT]| | NRC NOTIFIED BY: W. MOOKHOEK |LAST UPDATE DATE: 09/06/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VITAL BUS SUPPLY BREAKER FOUND TO HAVE IMPROPER TRIP SETTING AFFECTING | | OPERABILITY | | | | "On August 29, 2000, at 0038 CDT, Unit 2 experienced a loss of power to | | Class 1 E 480v motor control center (MCC) E2C1. The power loss resulted in a | | loss of normal letdown in the Chemical Volume Control System and loss of | | other safety related loads. The MCC was re-energized at 0108 CDT and plant | | systems were restored to normal. | | | | "An investigation found the long time overload settings for the feeder | | breaker to MCC E2C1 to be one-half of the required values. The condition had | | existed since October 23, 1999, when the breaker was placed in service. At | | 0845 on September 6, 2000, this condition was determined to be reportable | | after completion an engineering evaluation. The engineering evaluation | | determined that the breaker had a high potential for opening under accident | | conditions because of the improper settings. The condition was corrected on | | August 29, 2000, at 1806 CDT. The corresponding breakers in the other ESF | | trains and in Unit 1 were found to have the correct settings. | | | | "Some safety related equipment powered from the MCC was determined to have | | been inoperable since October 23, 1999, because opening of the breaker would | | have interrupted the equipment's ability to perform its | | design function. The duration of inoperability exceeded the Technical | | Specification allowed outage time for some systems, which include: | | - 1 of 3 trains of Essential Chilled Water (TS 3/4.7.14): inoperable | | essential chilled water pump 21C | | - 1 of 3 trains of Control Room Envelope HVAC (TS 3/4.7.7): inoperable | | makeup fan 21C | | - 1 of 3 Standby Diesel Generators (TS 3/4.8.1): inoperable emergency supply | | fan 21C (support system for SDG 23) | | | | "This condition is reportable under 10CFR50.73(a)(2)(i)(B) and notification | | is required within 24 hours by Section 2G of the Unit 2 Operating License | | (NPF-80)" | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37294 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: PHILIP MORRIS |NOTIFICATION DATE: 09/06/2000| |LICENSEE: PHILIP MORRIS |NOTIFICATION TIME: 15:42[EDT]| | CITY: RICHMOND REGION: 2 |EVENT DATE: 06/01/2000| | COUNTY: STATE: VA |EVENT TIME: [EDT]| |LICENSE#: 45-00385-06 AGREEMENT: N |LAST UPDATE DATE: 09/06/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MARK LESSER R2 | | |E. WILLIAM BRACH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DONALD IRWIN | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |IBBF 30.50(b)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SHUTTER ON SCANNER DISABLED ON CONVEYOR LINE | | | | A small piece of lead fell off the inside of a shield for a sealed beam | | source which prohibited the full closure of the shutter on the source. | | There was no exposure to personnel and repairs will be made by Philip | | Morris. This was discovered on 6/1/00 during a normal inventory of sources. | | It wasn't known to be reportable until today. The scanner is used to | | monitor cartons for missing packs of cigarettes. It is manufactured by | | Industrial Dynamics, model FT14, with two 100 mCi Am-241 sources. | | | | The company also notified NRC Region 2 (Orysia Bailey) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37295 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: R.D. ZANDE & ASSOCIATES |NOTIFICATION DATE: 09/06/2000| |LICENSEE: R.D. ZANDE & ASSOCIATES |NOTIFICATION TIME: 15:45[EDT]| | CITY: KYSER REGION: 2 |EVENT DATE: 09/06/2000| | COUNTY: GRANT STATE: WV |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 09/06/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MARK LESSER R2 | | |GARY SHEAR R3 | +------------------------------------------------+E. WILLIAM BRACH NMSS | | NRC NOTIFIED BY: JOE STOCK | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TROXLER GAUGE DAMAGED BY TRUCK RUNNING OVER IT | | | | R.D. Zande and Associates (of Columbus, OH) was conducting a back scatter | | test on asphalt on State Route 220 in Kyser, WV when an asphalt truck backed | | over it. The gauge is a Troxler Model 3411 with a cesium source. The case | | was damaged , case cracked, and the extension rods were damaged. The source | | was extended at the time and not believed to be damaged. The source was | | recovered into the shielded position. The gauge will be transported to | | Cline Technical Services in Amanda, Ohio, will be wipe tested there and | | final disposition of the gauge will be determined. | | | | The company has contacted NRC Region 3 (John Madera and Sam Mulea). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37296 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 09/06/2000| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 18:38[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 09/06/2000| +------------------------------------------------+EVENT TIME: 16:21[CDT]| | NRC NOTIFIED BY: ERNEST MATHES |LAST UPDATE DATE: 09/06/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DURING SURVEILLANCE AN AUTOMATIC ISOLATION SIGNAL WAS GENERATED DUE TO | | MISSED SWITCH POSITIONING | | | | "Reactor Core Isolation Cooling (RCIC) system isolated during performance of | | Annual Leak Detection surveillance (06-IC-A-1003-02). Investigation | | revealed leak detection switches not in bypass during test. System | | responded as designed. ES1-F064 (Mn Steam isolation) and trip Throttle | | valve closed. System restored to standby." | | | | The licensee determined there was a missed step in the surveillance | | procedure. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021