Event Notification Report for September 5, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/01/2000 - 09/05/2000 ** EVENT NUMBERS ** 37281 37282 37283 37284 37285 37286 37287 37288 37289 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37281 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 08/31/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 21:32[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/31/2000| +------------------------------------------------+EVENT TIME: 17:47[CDT]| | NRC NOTIFIED BY: TIEDEMANN |LAST UPDATE DATE: 09/01/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED 72 HOUR LCO ACTION STATEMENT WHEN DIVISION III DIESEL | | GENERATOR WAS DECLARED INOPERABLE | | | | During performance of Fire Protection Surveillance 9337.81 (performs a | | functional check of the Division III Diesel Generator (DG) Carbon Dioxide | | (CO2) system operation), the Division III DG ventilation system tripped | | during restoration. Electrical Maintenance personnel were performing a | | functional check of the Division III DG room thermal detectors when the | | panel reset push button was depressed. The anticipated resets did not occur | | and the decision was made to restore the system to a safe condition. During | | restoration, a sticking relay prevented restoration of the Division III DG | | ventilation system. The relay has been reset and the ventilation system | | restored. | | | | Division III DG was declared INOPERABLE at 1747 and the plant entered LCO | | 3.8.1. | | Action B.1- Perform 9082.01 within 1 hour and every 8 hours thereafter. | | Action B.2- Declare required features supported by Division Ill DG inop when | | the redundant required features are inop, within 4 hours. | | Action B.3.1- Determine Operable DG are not inop due to common cause failure | | within 24 hours - This action -completed. | | Action B.4- Restore Div 3 DG to Operable within 72 hrs. | | Division Ill DG was declared OPERABLE at 1813 and the LCO was exited. | | | | The NRC Resident Inspector was notified.. | | | | * * * UPDATE ON 09/01/00 @ 1400 BY SHELTON TO GOULD * * * | | | | The time the diesel became inoperable was 1420 but it was not declared | | inoperable until 1747. This event is being reported pursuant to 10CFR50.72 | | (b)(2)(iii)(D) as a condition that alone could have prevented the | | fulfillment of the High Pressure Core Spray (HPCS) system, a single-train | | safety system needed to mitigate the consequences of an accident, since the | | Div. 3 DG is an essential support system for the HPCS system needed to | | mitigate a small break LOCA concurrent with a loss of offsite power. | | | | The NRC Resident Inspector will be notified. | | | | The Reg 3 RDO (Leach) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37282 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ENGELHARDT & ASSOCIATES |NOTIFICATION DATE: 09/01/2000| |LICENSEE: ENGELHARDT & ASSOCIATES |NOTIFICATION TIME: 10:09[EDT]| | CITY: MADISON REGION: 3 |EVENT DATE: 06/12/2000| | COUNTY: STATE: WI |EVENT TIME: [CDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 09/01/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MELVYN LEACH R3 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SUSAN ENGELHARDT | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAE1 20.2202(b)(1) PERS OVEREXPOSURE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN EMPLOYEE OF A RADIATION CONSULTING FIRM MAY HAVE RECEIVED A PERSONNEL | | OVEREXPOSURE | | | | ENGELHARDT & ASSOCIATES, INC. WAS HIRED BY SOUTHEAST MISSOURI STATE | | UNIVERSITY LOCATED IN CAPE GIRARDEAU, MO. TO ASSESS AND UPGRADE THE | | UNIVERSITY'S RADIATION SAFETY PROGRAM. SEVERAL YEARS BEFORE THE UNIVERSITY | | INFORMED THE NRC THAT A COUPLE OF AMERICIUM-241 SOURCES HAD BEEN REMOVED. | | DURING AN NRC RIII INSPECTION LATE LAST YEAR, THE SOURCES WERE FOUND ON | | CAMPUS. DURING THE CONSULTANTS ASSESSMENT, HE DISCOVERED THAT ONE OF THE | | SOURCES HAD BEEN SPILLED (LIQUID FORM) CAUSING A LARGER PROBLEM THAN | | INITIALLY BELIEVED. THE EMPLOYEE'S UPTAKE WAS DETERMINED BY ARGONNE | | NATIONAL LAB TO BE ON THE ORDER OF 9 REM CUMULATIVE DOSE EQUIVALENT. NRC | | REGION III (WRIGHT, JORGENSEN) WAS INFORMED BY ENGELHARDT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37283 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 09/01/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 12:20[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/01/2000| +------------------------------------------------+EVENT TIME: 11:30[EDT]| | NRC NOTIFIED BY: UNDERWOOD |LAST UPDATE DATE: 09/01/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD CLOSURE OF THE POST ACCIDENT SAMPLING SYSTEM INBOARD PRIMARY | | CONTAINMENT ISOLATION VALVE | | | | During performance of Reactor Building Isolation LSFT (34SV-SUV-027-1S), | | 1E41-F122, Post Accident Sampling System Inboard PCIV, failed closed between | | approximately 1145 and 1230 on 08/31/00. 1E41-H22 was verified to be open at | | approximately 1145 following completion of channel A performance test | | (section 7.2). After returning from lunch break, operators observed | | 1E41-F122 closed and could not be reopened with control switch. | | | | The isolation has not been reset and they have also isolated the outboard | | valve by TS requirement. Investigation into cause of closure is continuing. | | | | During discussions with Nuclear Safety and Compliance Department at 1130 on | | 09/01/00 it was determined that this PCIV failing closed was a reportable | | ESF actuation. | | | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37284 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 09/01/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 18:49[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 09/01/2000| +------------------------------------------------+EVENT TIME: 14:19[CDT]| | NRC NOTIFIED BY: HOPMAN |LAST UPDATE DATE: 09/01/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING SYSTEM RECEIVED AN ISOLATION SIGNAL DURING | | MAINTENANCE. | | | | Unit 2 was operating at 100% power. The Reactor Core Isolation Cooling | | System was removed from service for scheduled maintenance. Following valve | | packing adjustment, the Reactor Core Isolation Cooling system steam supply | | outboard isolation valve was opened per approved procedure. Approximately | | 10 seconds after the Reactor Core Isolation Cooling system steam inboard | | isolation bypass valve was throttled open for warming. "Division 2 Reactor | | Core isolation Cooling system steam line DP hi" and "Reactor Core Isolation | | Cooling system Steam Line/Turbine isolation" alarms were received. The | | Reactor Core Isolation Cooling system steam inboard isolation bypass valve | | automatically closed due to an isolation signal. The Reactor Core Isolation | | Cooling system remains isolated by the inboard isolation valves. The cause | | of the isolation signal is unknown at this time. An investigation is in | | progress to determine the cause of the isolation and initiate actions to | | restore the Reactor Core Isolation Cooling system to an operable and | | available status and exit the LCO action statement. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37285 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 09/01/2000| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 21:08[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 09/01/2000| +------------------------------------------------+EVENT TIME: 19:40[EDT]| | NRC NOTIFIED BY: MCDONNELL |LAST UPDATE DATE: 09/01/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETE ESELGROTH R1 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION DECLARED INOPERABLE PLACING THE PLANT IN A | | 14 DAY LCO ACTION STATEMENT. | | | | During the performance of 8.5.4.1 (HPCI operability test), HPCI failed to | | meet acceptance criteria. The HPCI pump failed to meet the required flow, | | pressure and rpm requirements. Troubleshooting of the problem is in | | progress to make HPCI operable within the 14 day LCO action statement | | requirement. | | | | The NRC Resident Inspector was informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37286 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 09/03/2000| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 15:49[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 09/03/2000| +------------------------------------------------+EVENT TIME: 15:10[EDT]| | NRC NOTIFIED BY: DAVE OWEN |LAST UPDATE DATE: 09/03/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |PETE ESELGROTH R1 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC |JOSEPH GIITTER IRO | | |CALDWELL FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT - FIRE IN CONTAINMENT | | | | The licensee declared an unusual event at 1510 because of a fire in | | containment that lasted more than 15 minutes. A fire was reported at 1440 | | in a tarp that was being used in containment. The tarp is believed to have | | been ignited by some cutting or grinding going on in the vicinity. The | | licensee called for assistance from the local fire department, but they | | extinguished the fire before the fire company could assist. The fire was | | reported out at 1509. The unusual event was terminated at 1615. | | | | The reactor is defueled with all fuel having been moved to the spent fuel | | pool. No radioactivity was released. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37287 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 09/04/2000| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 15:00[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 09/04/2000| +------------------------------------------------+EVENT TIME: 11:32[CDT]| | NRC NOTIFIED BY: JIM GILMORE |LAST UPDATE DATE: 09/04/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVE LOVELESS R4 | |10 CFR SECTION: |STUART RICHARDS NRR | |ARPS 50.72(b)(2)(ii) RPS ACTUATION |VICTOR DRICKS PAO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP DUE TO FIRE IN UNIT AUXILIARY TRANSFORMER | | | | At about 1132 CDT a fire was reported in the unit auxiliary transformer, | | alarms were received in the control room with a unit trip, all rods fully | | inserted. The on-site fire brigade and the off-site fire department were | | called to respond. The fire was extinguished by installed fire suppression | | equipment and declared out at 1143 CDT. The fire is being investigated by | | fire protection personnel. The off-site fire department was released. | | | | The plant is stable in Hot Standby at normal temperature and pressure. Heat | | removal is via the main condensers with steam generator level being | | maintained by auxiliary feedwater. | | | | The auxiliary feedwater system, both turbine and motor driven, started | | automatically on low steam generator level as expected with this event. All | | safety equipment performed as designed. | | | | Concurrent with the reactor trip, the 'C' and 'D' reactor coolant pumps | | tripped along with other loads due to one (PA02) of the two non-vital busses | | not automatically transferring as expected to off-site power. The bus is | | presently energized by off-site power and the 'D' reactor coolant pump was | | restarted. The actual cause of the problem is being investigating. | | | | One of the reactor coolant system power operated relief valve opened and | | closed one time due the transient of the 'D' reactor coolant pump trip and | | subsequent loss of pressurizer spray. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37288 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 09/04/2000| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 15:30[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/04/2000| +------------------------------------------------+EVENT TIME: 14:16[EDT]| | NRC NOTIFIED BY: ANDY DISMUKE |LAST UPDATE DATE: 09/04/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INADVERTENT DEENERGIZATION OF THE '2A' RPS MG SET CAUSED GROUP 2 AND 5 | | ISOLATIONS | | | | Plant personnel inadvertently tripped breaker to the '2A' reactor protection | | system motor generator (RPS MG) set resulting in de-energization of the '2A' | | RPS bus. This resulted in the closure of the inboard Group 2 containment | | isolation valves, the inboard Group 5 reactor water cleanup valve, inboard | | reactor water sample valve, the control room ventilation swapped to the | | pressurization mode of operation, and a half scram in the 'A' RPS channel. | | All actuations have been reset and the '2A' RPS bus is energized from the | | alternate supply while an investigation is being conducted. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37289 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 09/05/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 05:42[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/05/2000| +------------------------------------------------+EVENT TIME: 02:00[EDT]| | NRC NOTIFIED BY: R.T. ELLIOT |LAST UPDATE DATE: 09/05/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | "2B" AUXILIARY FEEDWATER PUMP RAN 2 HOURS AND 55 MINUTES BEFORE IT WAS | | DISCOVERED THAT IT WAS OPERATING. STEAM GENERATORS WERE ISOLATED FROM THE | | AFW SYSTEM. | | | | At 0200 ET the "B" Train of the Solid State Protection System (SSPS) was | | deenergized for part of their refueling outage maintenance. When the SSPS | | was deenergized the blocks for the Main Feedwater Pump blocks clear which | | gave an automatic start signal to the "2B" AFW pump. The on shift reactor | | operator did not notice that the "2B" AFW pump run light was on until 0455 | | ET due to refueling outage maintenance activities in Control Room. "2B" AFW | | pump recirculated water to the Upper Surge Tank since the Steam Generators | | were isolated. NO damage occurred to the AFW pump. The licensee is | | investigating this event. | | | | The NRC Resident Inspector will be notified of this event. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021