Event Notification Report for August 22, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/21/2000 - 08/22/2000 ** EVENT NUMBERS ** 37208 37235 37241 37242 37243 37244 37245 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37208 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 08/05/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 08:07[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/05/2000| +------------------------------------------------+EVENT TIME: 04:28[EDT]| | NRC NOTIFIED BY: STUART BYRD |LAST UPDATE DATE: 08/21/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEORGE BELISLE R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A MINIMAL AMOUNT OF WATER IN THE REACTOR CORE ISOLATION COOLING | | OIL SYSTEM | | | | The following text is a portion of a facsimile received from the licensee: | | | | "EVENT: The Unit 2 the Reactor Core Isolation Cooling (RCIC) system was | | discovered to have a minimal amount of water in the oil system. Following | | investigation of the event and replacement of the oil, the RCIC turbine was | | successfully manually started and operated normally. During a subsequent | | automatic start for post-maintenance test requirements, the turbine tripped | | on high exhaust pressure apparently caused by the governor system's slow | | response time. Investigation of the turbine control system is continuing." | | | | "CORRECTIVE ACTION(S): Continue the investigation to determine the root | | cause of the water in the oil system and the response of the governor | | control system." | | | | "INITIAL SAFETY SIGNIFICANCE EVALUATION: Minimal. The High Pressure | | Coolant Injection System, Automatic [Depressurization] System, Low Pressure | | Core Spray, and the Low Pressure Coolant Injection System were operable | | throughout the event." | | | | The licensee stated that, as a result of this issue, the unit is currently | | in a 14-day limiting condition for operation in accordance with Technical | | Specification 3.5.2. The licensee also stated that all other systems | | functioned as required. | | | | The licensee notified the NRC resident inspector. | | | | | | * * * UPDATE ON 8/21/00 @ 1050 BY ELBERFELD TO GOULD * * * RETRACTION | | | | Upon further investigation, it has been determined that the condition | | resulting in the RCIC turbine trip developed during the period of time that | | the system was inoperable for maintenance, and that there was no loss of | | safety function. | | | | After the notification was made it was determined that the trip of the RCIC | | turbine was caused by the presence of air in the control system for the | | governor valve positioning servo. The presence of air delayed the closing of | | the governor valve during the RCIC turbine start sequence, allowing the | | turbine speed to increase, thus increasing turbine exhaust pressure above | | the trip setpoint. The presence of air was introduced by the maintenance | | activities associated with changing the turbine lube oil. An acknowledged | | industry expert was consulted and confirmed that one controlled manual start | | would not be considered adequate to remove air from the governor control | | system even with a substantial run duration. Experience has shown that | | multiple starts, at least 2 to 3 governor valve strokes, may be needed to | | remove the air that can cause abnormal turbine starts. | | | | Review of the "as found" condition of the RCIC system and the RCIC system | | performance before and after the turbine trip indicates that the RCIC system | | would have successfully performed its intended functions prior to being | | taken out of service for maintenance on August 4, 2000. This is based on | | the following. | | | | * The system quick started and ran successfully on August 2, 2000, prior to | | the oil sample being taken that contained the water. | | * The presence of water in the lube oil did not cause the turbine trip and | | did not have an adverse impact on short-term system operability. | | * Both turbine trips during the quick-starts were the result of minimal | | governor valve stroking after the lube oil changes introduced air into the | | governor valve control system. | | * The RCIC turbine was able to achieve a quick-start without tripping, | | during the performance of OPT-10.1.1 on August 7, 2000, after the governor | | valve had been stroked twice (i.e., the controlled manual start and a failed | | quick-start). | | | | This event is being retracted by the licensee. | | | | The NRC Resident Inspector was notified by the licensee. The R2DO (Paul | | Fredrickson) was notified by the NRC Operations Officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37235 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 08/17/2000| | UNIT: [1] [2] [] STATE: MN |NOTIFICATION TIME: 13:34[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 08/16/2000| +------------------------------------------------+EVENT TIME: 11:15[CDT]| | NRC NOTIFIED BY: BRAD ELLISON |LAST UPDATE DATE: 08/21/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING A LARGE FISH KILL | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[The] decision was made today (08/17/00) at 1130 [CDT] to notify offsite | | agencies concerning a large fish kill at Prairie Island. This [was the] | | result of the planned zebra mussel treatment that was taking place at the | | plant." | | | | The licensee stated that the event occurred on 08/16/00 and that the fish | | kill involved approximately 7,500 young fish (mainly catfish and minnows | | approximately 2" to 5" in length). The majority of these fish were | | discovered in the plant's recycle canal. However, a few dead fish were also | | found in the Mississippi River. | | | | The licensee notified both the state and Goodhue County. The licensee also | | plans to notify the NRC resident inspector. In addition, a press release | | may be issued because this may be a media sensitive event. | | | | * * * UPDATE 1145EDT 8/21/00 FROM BILL MATHER TO S. SANDIN * * * | | | | The licensee is correcting this report to read that 75,000 young fish were | | killed. The licensee informed the NRC resident inspector. Notified | | R3DO(Hiland). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37241 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 08/21/2000| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 12:30[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/21/2000| +------------------------------------------------+EVENT TIME: 06:45[CDT]| | NRC NOTIFIED BY: MIKE SCHAEFER |LAST UPDATE DATE: 08/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LARRY YANDELL R4 | |10 CFR SECTION: | | |NLCO TECH SPEC LCO A/S | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - 2 OF 3 TRAINS OF ESSENTIAL CHILLED WATER SYSTEM INOPERABLE; TECH SPEC | | 3.0.3 ENTERED - | | | | At 0645 CDT on 08/21/00 with the 'C' train Essential Chilled Water System | | inoperable for maintenance activities, the 'A' train Essential Chilled Water | | System became inoperable due to an oil leak. This condition of two trains of | | the Essential Chilled Water System being inoperable is not allowed by | | Technical Specification 3.7.14 and required entry into Technical | | Specification 3.0.3. No maintenance work had yet been performed on the 'C' | | train Essential Chilled Water System. At 0754 CDT on 02/21/00, the licensee | | released the equipment clearance tags and restored the 'C' train Essential | | Chilled Water System to operable status and exited Technical Specification | | 3.0.3. | | | | This event is reportable to the NRC in accordance with the requirements of | | 2G of the South Texas Project's Operating License to notify the NRC within | | 24 hours of any violation of Technical Specifications. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37242 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 08/21/2000| | UNIT: [1] [2] [] STATE: MN |NOTIFICATION TIME: 14:54[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 08/21/2000| +------------------------------------------------+EVENT TIME: 13:15[CDT]| | NRC NOTIFIED BY: BILL MATHER |LAST UPDATE DATE: 08/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - WESTINGHOUSE ANALYSIS OF UNBORATED SFP NOT WITHIN NRC APPROVED DESIGN | | CRITERIA - | | | | Westinghouse has notified the Prairie Island Nuclear Plant that the analysis | | for the Spent Fuel Pool (SFP) with zero boron concentration is not within | | the NRC approved design criteria. The current NRC approved analysis for | | unborated water in the SFP states that the Keff should be less than 1.0. | | The Westinghouse analysis assumed a nominal fuel pellet density lower than | | the as-fabricated density. This results in a Keff of 1.00086 in an | | unborated SFP. | | | | Westinghouse reanalyzed the condition using a methodology that takes credit | | for the effect of spacer grids and spacer sleeves. With this factor, the | | analysis concludes that Keff in an unborated SFP would be less than 1.01; | | however, this change to the methodology has not been approved by the NRC. | | | | The approved analysis includes a case that takes credit for 750 ppm borated | | water. Westinghouse has reevaluated this case using higher density fuel | | pellets and concluded the acceptance criteria (Keff < 0.95) is still met. | | | | Prairie Island Plant Technical Specifications require the SFP boron | | concentration to be greater than 1800 ppm. Current SFP boron concentration | | is 3210 ppm. Additional compensatory measures are being evaluated. | | | | Reference: Tech Specs 3.8.E.2.a and 5.6.A.1.b. | | | | The licensee notified state and local officials and the NRC Resident | | Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37243 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 08/21/2000| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 15:52[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 08/21/2000| +------------------------------------------------+EVENT TIME: 14:15[CDT]| | NRC NOTIFIED BY: ROY SCOTT |LAST UPDATE DATE: 08/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(1)(ii)(A) UNANALYZED COND OP | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 96 Power Operation |96 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - 3 OF 3 AFW PUMPS INOPERABLE DUE TO UNDERSIZED PUMP SUCTION STRAINERS - | | | | During an inspection of the 'A' Auxiliary Feedwater (AFW) pump, the licensee | | observed that the length and hole size of the pump suction strainer were | | different than those assumed in a previous operability determination. The | | installed pump strainer is approximately 10 inches long and has 1/16 inch | | diameter holes. The operability determination assumed a 6 inch long | | strainer with 1/8 inch diameter holes. The licensee could not determine | | whether the smaller strainer would plug and therefore, declared the 'A' AFW | | pump inoperable. The licensee inspected the suction strainers of the 'B' | | and 'C' AFW pumps and determined that their suction strainers may be | | identical to the 'A' AFW pump strainer and therefore, declared the 'B' and | | 'C' AFW pumps inoperable. With 3 of 3 AFW pumps inoperable, plant tech | | specs prohibit the licensee from changing plant operating modes. | | | | The licensee plans to remove the suction strainers from all 3 AFW pumps. | | With the 'A' AFW pump strainer removed and the 'A' AFW pump declared | | operable, the plant will be in a 4-hour shutdown LCO with the other AFW | | pumps inoperable. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37244 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 08/21/2000| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 17:53[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/21/2000| +------------------------------------------------+EVENT TIME: 15:31[CDT]| | NRC NOTIFIED BY: MARK BROWNING |LAST UPDATE DATE: 08/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - MANUAL REACTOR SCRAM FROM 100% POWER DUE TO REDUCED MAIN CONDENSER VACUUM | | - | | | | At 1531(CDT) on 08/21/00 with the plant in Operational Condition 1 at 100% | | power, the operating crew inserted a manual reactor scram signal due to the | | inability to maintain main condenser vacuum greater than 25 inches Hg. | | Prior to this condition, the operating crew was responding to a low flow | | condition in the in-service offgas system train in accordance with alarm | | response procedures. While admitting air to the offgas system train as | | directed, a low main condenser vacuum condition occurred, requiring the | | operators to insert a manual reactor scram signal. All control rods | | inserted completely. No safety/relief valves lifted. Steam is being dumped | | to the main condenser. | | | | Subsequent to the reactor scram, a reactor vessel low water level 3 signal | | was received, as expected, which resulted in an ESF isolation of the | | suppression pool cooling system. The suppression pool cooling system was in | | the suppression pool cooling mode at the time of the isolation. The reactor | | vessel water level has been restored to its normal level. Following the | | reactor scram, all systems functioned as expected. The plant is stable in | | Operational Condition 3 (Hot Shutdown). | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37245 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 08/21/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 19:33[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 08/21/2000| +------------------------------------------------+EVENT TIME: 18:00[EDT]| | NRC NOTIFIED BY: KERRY ALLEN |LAST UPDATE DATE: 08/22/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHRISTOPHER CAHILL R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING OIL SPILL ONSITE | | | | "Oil was discovered covering the gravel over an approximate 1 meter diameter | | area. The area was located under vent pipe for the main turbine generator | | air detraining tank on the turbine building roof." | | | | The NRC resident inspector will be notified by the licensee. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021