Event Notification Report for August 17, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/16/2000 - 08/17/2000 ** EVENT NUMBERS ** 37173 37214 37223 37229 37230 37231 37232 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37173 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 07/17/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 23:18[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 07/17/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:35[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/16/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MICHAEL PARKER R3 | | DOCKET: 0707002 |M. WAYNE HODGES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JEFF CASTLE | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01, 24 HOUR REPORT - | | | | At 1335 on 07/17/00, it was discovered that an NCSA mass control was lost in | | a compressor seal can storage area in the X-330 building. Two seal cans were | | identified to contain more items than specifically permitted by | | NCSA-0330_003.A02 requirement #4 which states: "Only one seal set shall be | | in each seal can." One seal can was discovered to contain two seal sets and | | a second seal can was discovered to contain one seal with several (3 or 4) | | additional seal parts. This deficiency was discovered during recovery | | activities for NCS event report PTS-00-065 (NRC Event Number #37172) | | involving a spacing violation of NCSA-0330_003.A02, requirement #8. | | | | This event resulted in the loss of one control (mass) of the double | | criticality control principle. NCS interaction and enrichment control was | | maintained throughout this event. | | | | NCSA-0330_003.A02 requirement #4 compliance was restored at 1415 when the | | extra seal and seal parts were stored individually in seal cans under NCS | | Engineering guidance. Complete compliance with NCSA-0330_003.A02 (refer to | | NCS event #PTS-00-065) was established at 1705. | | | | SAFETY SIGNIFICANCE OF EVENT: | | | | The safety significance of this event is low. NCSE-0330_003.101 analyzes | | greater than safe mass in a group of seal cans. In this analysis it states | | that with an enrichment limit of 15% U-235, the amount of uranium in a seal | | can would have to be exceeded by 4.6 times the normal amount to reach the | | minimum critical mass. In this event two seal cans were found to be double | | loaded. Assuming that both overloaded seal cans were next to each other, | | the mass in the cans is less than the minimum critical mass. Note: these | | cans were found because the group they were in was being moved to correct a | | spacing violation between two other seal can groups. The overloaded seal | | cans were not directly involved in the spacing violation. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED [BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR]: | | | | For a criticality to occur, the seal cans would have to have more than a | | double batch and the enrichment exceed 15% U-235. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, (GEOMETRY, CONCENTRATION, ETC): | | | | The controlled parameters in this case are mass, enrichment and | | interaction. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | The total amount of uranium in the 47 seal cans involved (including the two | | overloaded cans) is estimated to be 1715 grams uranium or 257.3 grams of | | U-235. The maximum enrichment for this NCSA is limited to 15% U-235 and the | | form of the material is dry UO2F2. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | The NCS mass control was lost in this case. Only one seal is allowed to be | | placed In a seal can. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | At 1415, NCSA-0330_ 003.A02 compliance was restored. The extra seal parts | | were removed and stored individually in separate seal storage cans. | | | | The NRC Resident Inspector and the DOE Site Representative were notified of | | this event. | | | | PTS-2000-03534 PR-PTS-00-066 | | | | * * * UPDATE AT 1252 ON 8/2/00, BY SISLER RECEIVED BY WEAVER * * * | | | | On 8/2/00 at 0035 hours maintenance personnel performing walkdown | | verifications for NRC Event PTS-00-066 discovered a seal can containing | | several pieces of seals that were more than volume of one seal. Compliance | | was re-established at 0250hrs under NCS Engineering guidance. The various | | seal parts were separated into three seal cans and properly stored per the | | NCSA. At the time of this Update, a 100% Walkdown of all Seal Cans in | | storage is in progress. | | | | The licensee notified the NRC resident inspector. The operations center | | notified the RDO(Creed); EO (Hickey) | | | | * * * UPDATE ON 8/16/00 @ 0756 BY VANDERPOOL TO GOULD * * * | | | | On 8/15/00 @ 2150 hours maintenance personnel performing walkdown | | verification for NRC Event PTS.00-066 discovered a seal can containing | | several pieces of seals that involved more volume than that of one seal. | | Compliance was re-established at 0032 hours on 08/16/00 under NCS | | Engineering guidance. The various seal parts were separated into the | | appropriate seal cans and properly stored per the NCSA. At the time of this | | update, a 100% walkdown of all seal cans In storage Is in progress. | | | | The NRC Resident Inspector was notified along with the DOE Representative. | | | | The Reg 3 RDO(Jacobson) and NMSS EO(Piccone) were notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37214 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 08/08/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 21:35[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/08/2000| +------------------------------------------------+EVENT TIME: 18:44[EDT]| | NRC NOTIFIED BY: FREDERICK SMITH |LAST UPDATE DATE: 08/16/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 99 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOSTART OF ANNULUS EXHAUST GAS TREATMENT SYSTEM FAN DURING TESTING | | | | "During performance of surveillance testing, the lifting of an incorrect | | lead caused a low flow condition on the in service AEGTS fan. This caused | | the auto start of the standby AEGTS fan. No low flow alarm was received on | | the in service fan, but the system functioned properly." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * RETRACTION ON 08/16/00 AT 1435 ET BY KEN RUSSELL TAKEN BY MACKINNON * | | * * | | | | The low flow signal which started the Annulus Exhaust Gas Treatment System | | fan is not an ESF signal. Therefore, this event is being retracted since | | the autostart did not occur based on a valid ESF signal. R3DO (John | | Jacobson) notified. | | | | The NRC Resident Inspector was notified of the retraction by the licensee. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37223 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 08/14/2000| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 07:42[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/14/2000| +------------------------------------------------+EVENT TIME: 06:58[EDT]| | NRC NOTIFIED BY: WESLEY HILL |LAST UPDATE DATE: 08/16/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANNE BOLAND R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH TRAINS OF HIGH PRESSURE INJECTION DECLARED INOPERABLE | | | | The licensee, in the process of a routine train swap between the 1B nuclear | | volume control (NV) pump and the 1A NV pump, the 1B discharge check valve | | did not fully seat. Flow from the 1A NV pump was being returned through the | | 1B NV pump to the suction header. This could have affected the capability | | of both of the NV pumps to perform their required actions in the event that | | high head injection to the reactor coolant system was needed. Both pumps | | were declared inoperable at 0658 EDT which made the high head injection | | system inoperable. The discharge valve on the 1B NV pump was shut at 0710 | | EDT to restore the 1A NV pump to operable. | | | | The method to be used to restore the 1B NV pump to operable is being | | considered. | | | | The licensee intends to notify the NRC Resident Inspector. | | | | * * * RETRACTION ON 08/16/00 AT 1711 ET BY T. HEAFNER TAKEN BY MACKINNON * | | * * | | | | "Subsequent to the report, further evaluation determined that the calculated | | back flow through the 1B NV pump would not have prevented proper starting | | and operation of that pump. Consequently, that pump was capable of | | performing it's safety function. With one NV pump operable, there is | | sufficient injection flow capacity to the reactor coolant system during the | | event. In addition, for the short time that the 1A NV pump was inoperable, | | it was not required to assume a single failure of the 1B NV pump during an | | event. Consequently, McGuire Nuclear Station was not outside it's design | | basis and Event Report 37223 is retracted." NRC R2DO (Paul Fredrickson) | | notified. | | | | The NRC Resident Inspector was notified of this event retraction by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37229 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 08/16/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 02:15[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/16/2000| +------------------------------------------------+EVENT TIME: 00:30[EDT]| | NRC NOTIFIED BY: PAUL UNDERWOOD |LAST UPDATE DATE: 08/16/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PAUL FREDRICKSON R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 DECLARED HIGH PRESSURE COOLANT INJECTION (HPCI) INOPERABLE DUE TO A | | FAILURE DURING SURVEILLANCE TESTING | | | | "While performing weekly exercise per Operating Order 00-01-0200S, High | | Pressure Coolant Injection turbine stop valve failed to close when trip | | solenoid pushbutton was depressed. | | | | "High Pressure Coolant Injection was declared inoperable. | | | | "Cause of turbine stop valve failure to close is under investigation." | | | | With HPCI inoperable, Unit 1 entered a 14 day LCO Action Statement. Both | | Maintenance and Engineering are evaluating corrective actions. The licensee | | will inform the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37230 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NORTH CAROLINA DIV OF RAD PROTECTIO |NOTIFICATION DATE: 08/16/2000| |LICENSEE: QUALITY NDE/JANX |NOTIFICATION TIME: 11:26[EDT]| | CITY: ROARING RIVER REGION: 2 |EVENT DATE: 08/16/2000| | COUNTY: STATE: NC |EVENT TIME: 10:00[EDT]| |LICENSE#: 0851117-1 AGREEMENT: Y |LAST UPDATE DATE: 08/16/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PAUL FREDRICKSON R2 | | |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ALBRIGHT | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | The North Carolina Division of Radiation Protection reported a radiography | | camera with a disconnected source.. | | | | The state discovered, while reviewing records, they had mis-filed an | | incident report from a licensee reporting a source had disconnected on a | | Source Production and Equipment Co. (SPEC) model #150 serial #316 | | radiography camera. This occurred when Quality NDE(currently Janx) was | | performing work in Roaring River, N.C. and while they were retrieving the | | source to its shielded position, the drive cable broke at the gearbox. The | | licensee followed emergency procedures and brought two more radiographers | | to the site and retrieved the source to the shielded position manually. | | Readings of 2mr/hr @ 6" were measured when the source was retracted to the | | shielded position. The source(#EH1804) at the time of the | | incident(01/18/99) measured 25 curies @ Iridium-192 and it was disposed | | 3/99. The individuals involved in the recovery of the source received an | | actual dose of <8 millirem. The licensee had filed this incident report on | | 02/09/99 with the State, which was within the required time. | | | | N.C. incident report #00-33 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37231 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 08/16/2000| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 16:22[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/16/2000| +------------------------------------------------+EVENT TIME: 09:10[CDT]| | NRC NOTIFIED BY: CHARLES BOTTEMILLER |LAST UPDATE DATE: 08/16/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHUCK PAULK R4 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A contract supervisor tested positive for alcohol during random testing. | | His access was immediately suspended. Review of his work determined that | | their was no impact on plant safety. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37232 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 08/16/2000| | UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 17:59[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 08/16/2000| +------------------------------------------------+EVENT TIME: 16:25[CDT]| | NRC NOTIFIED BY: G RHODES |LAST UPDATE DATE: 08/16/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: ALE |PAUL FREDRICKSON R2 | |10 CFR SECTION: |WILLIAM BECKNER NRR | | |FRANK CONGEL IRO | | |BARDEN FEMA | | |YATES DOE | | |LORI THOMAS USDA | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SMOKE SEEN COMING FROM "2C" SERVICE WATER PUMP MOTOR | | | | "2C" Service Water Pump (swing) motor was seen having smoke coming from it. | | On site fire brigade was sent out to the Service Water building and | | extinguished the fire at 1609 CT. The licensee declared an Alert at 1625 CT | | due to the potential of the fire affecting ECCS equipment. No offsite | | assistance was needed and no other equipment onsite was damaged by the fire. | | Service Water Pumps "2A", "2B", "2D", & "2E" remain in service. All | | Emergency Core Cooling Systems are fully operable if needed. | | | | Fire Alarm for Service Water pump was received in control room at 1548 CT. | | A person was immediately dispatched to investigate the alarm. Person | | reported back to control room at 1552 CT that smoke was coming from "2C" | | Service Water motor. Licensee entered AOP 29 (Plant Fire) at 1552 CT. At | | 1555 CT "2C" Service Water Pump tripped for unknown reason. Service Water | | pump flow was degraded for approximately 15 seconds at which time another | | Service Water pump was placed in service. Lowest service water pressure | | reached was 70 psi (min pressure is 60 psi). At 1609 CT report received | | that fire had been extinguished using carbon dioxide. 1616 CT AOP 29 was | | exited. The licensee notified state and local officials of entering Alert | | classification. | | | | The NRC Resident Inspector was in the control room during the event. | | | | NRC Operation Center was notified by Brad Grinstead of the Alabama | | Department of Public Health and by Kerri Seber of the Florida State Warning | | Point of the Farley Unit 2 Alert. | | | | * * * UPDATE ON 08/16/00 AT 1845 ET BY G RHODES TAKEN BY MACKINNON * * * | | | | Alert was terminated at 1736 CT due to fire being out and all systems | | operating properly. | | | | NRC R2DO (Paul Fredrickson), Acting DEDR (Ellis Merschoff), IRO (Frank | | Congel), NRR EO (Bill Beckner), NRC PAO (Bill Beecher), NRR (Roy | | Zimmerman), EDO STAFF (Mark Satorius), NRC RCT (John Jolicoeur), FEMA | | (Belcher), DOE (Yates), USDA (Lori Thomas), EPA Reg IV (Runge), and HHS | | (Burger), notified. | | | | The NRC Resident Inspector was onsite in control room during this event. | | | | * * * UPDATE ON 08/16/00 AT 2031 ET BY G. RHODES TAKEN BY MACKINNON * * * | | | | "At 1625 [CT] FNP staff declared an Alert Emergency classification based on | | criteria found in site procedures. The 2C Service Water Pump motor had | | faulted resulting in a small fire in the Service Water Intake Structure. | | The Site Fire Brigade responded and the fire was extinguished promptly. No | | other equipment was damaged. The FNP Unit 2 Service Water system has 5 | | pumps and requires 2 pumps per train (4 pumps total) to ensure that system | | design functions are met. The 2C Service Water Pump is a swing pump that | | can be aligned to either train. The remaining four Unit 2 Service Water | | pumps are currently operable and in service. | | | | "The FNP staff has assessed this event. No plant personnel were injured and | | only limited damage to plant equipment as described above occurred. There | | was no affect on the health and safety of the general public and no release | | of radiation. The Alert was terminated at 1736 [CT]. Both Units are | | continuing to operate at 100% power." | | | | R2DO (Paul Fredrickson) & IRO (Congel) notified. | | | | The NRC Resident Inspector was notified of this update by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021