Event Notification Report for August 10, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/09/2000 - 08/10/2000 ** EVENT NUMBERS ** 36578 37192 37215 37216 37217 37218 37219 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36578 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 01/10/2000| |LICENSEE: PETRA TECHNOLOGIES, INC. |NOTIFICATION TIME: 17:10[EST]| | CITY: HOUSTON REGION: 4 |EVENT DATE: 01/10/2000| | COUNTY: HARRIS STATE: TX |EVENT TIME: [CST]| |LICENSE#: L05233 (TX) AGREEMENT: Y |LAST UPDATE DATE: 08/09/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JEFF SHACKELFORD R4 | | |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES OGDEN (VIA FAX) | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING STOLEN TROXLER 3430 MOISTURE DENSITY GAUGE | | | | "Troxler Model 3430, Serial # 27239, stolen January 9/10, 2000, from 605 | | East Safari Parkway, D-2, Mesquite, Texas. The gauge contained two | | radioactive sources: 8 millicurie (nominal activity) Cs-137 source, Serial # | | 750-976 and 40 millicurie (nominal activity) Am-241:Be source, Serial # | | 47-23865. Stolen from a parked Ford Ranger pickup truck belonging to the | | machines operator during the hours of darkness January 9/10, 2000. Gauge had | | been locked in the pickup's cab and covered by a jacket or blanket. Listed | | as Texas Incident 7561 Texas Licensee L05233 is based in Houston and had | | been performing work at a jobsite in East Fort Worth. Reported as missing | | to the Mesquite Fire Department January 10, 2000. Further details pending | | contact with company R.S.O." | | | | * * * UPDATE 1632 8/9/2000 FROM OGDEN (VIA FAX) INPUT BY STRANSKY * * * | | | | "Troxler Model 3430 was discovered in a garbage truck that set off radiation | | monitors at a local Dallas-Fort Worth landfill. The gauge was discovered in | | the back of the garbage truck operated by Duncan Disposal, 1220 Dowdy Ferry | | Road, Hutchins, Texas. It is believed that the gauge was picked up from | | apartment dumpsters located in the City of Seagoville. | | | | "The gauge is Serial Number: 27239 which was stolen in Mesquite, Texas on | | the evening of January 9/10, 2000. The gauge appears to be undamaged but is | | not in its transportation case which was taken during the theft. The Texas | | Licensee from whom the gauge was stolen is Petra Technologies Incorporated, | | Texas License # L05233. This licensee is currently in the process of | | revocation for failure to pay fees. All known phone numbers for the firm | | have been disconnected, therefore, and no one has yet been contacted within | | the firm. | | | | "Troxler both in North Carolina and in Arlington have been notified. | | | | "Texas Department of Health, Region 3 (Arlington) Bureau of Radiation | | Control personnel have picked-up the gauge from the disposal firm and have | | it secured at regional headquarters. The gauge appears to be intact. The | | gauge will be leak tested by Troxler's Arlington location." | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37192 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 07/27/2000| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 13:54[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 07/27/2000| +------------------------------------------------+EVENT TIME: 09:02[CDT]| | NRC NOTIFIED BY: VERNON CARLSON |LAST UPDATE DATE: 08/09/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BILL JONES R4 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL LOSS OF SAFETY FUNCTION RELATED TO CONTROL ROOM CHILLED WATER | | SYSTEM | | | | "While alternating Divisions of Control Room Chilled water to perform post | | maintenance testing on HVK-CHL1B the 'B' chiller tripped. When actions | | were taken to restart the 'A' chiller the breaker for the service water | | recirc valve SWP-MOV 27A tripped. The breaker was reset and the chiller was | | started. Due to the indeterminate nature of the breaker trip on the valve, | | the 'A' chiller was declared Inoperable. The 'C' & 'D' chillers were | | already Inoperable due to non-related existing conditions. This places the | | unit in Action 'B' of Tech Spec 3.7.3. We are conservatively reporting | | this pending the investigation of the condition and it's affect on the | | system response to postulated events to determine if the safety function was | | truly lost. System is currently operating and maintaining normal control | | room temperature." | | | | The licensee will inform the NRC Resident Inspector. | | | | * * * UPDATE AT 0924 ON 8/9/00, REPORTED BY NORTHRUP, RECEIVED BY WEAVER * * | | * | | | | The event occurred when the control building chilled water system was being | | shifted from Division I to Division II. The "A" chiller subsystem (Division | | I) had been operating normally for approximately one week, and was to be | | shut down to allow shut down of the "B" chiller subsystem (Division II). | | The "C" and "D" chillers were already inoperable for reasons unrelated to | | this event. | | | | During the transition to the "B" chiller, it failed to start. The "A" | | chiller did not immediately restart due to the configuration of its support | | systems at this point in the transition. Operator actions were promptly | | taken to restart the "A" chiller. Approximately nine minutes elapsed | | from the initial shutdown of the "A" chiller until it was restored to | | service. | | | | During the event, the "A" chiller was capable of performing its safety | | function with reasonable operator actions. This event had no bearing on the | | previous operability of the "A" chiller. | | | | Based on the above information, this event did not result in a loss of | | safety function. This event notification is retracted. | | | | The licensee informed the NRC resident inspector. The Operations Center | | notified the R4DO(Kennedy). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37215 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 08/09/2000| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 10:32[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 08/09/2000| +------------------------------------------------+EVENT TIME: 10:28[EDT]| | NRC NOTIFIED BY: DENNIS BEMIS |LAST UPDATE DATE: 08/09/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE DOERFLEIN R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION - AIRCRAFT WARNING LIGHTS | | | | The licensee notified the Federal Aviation Administration that the aircraft | | warning lights on the containment would be without power during planned | | maintenance. The maintenance is expected to last less than one hour. The | | licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37216 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 08/09/2000| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 11:22[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/09/2000| +------------------------------------------------+EVENT TIME: 09:07[CDT]| | NRC NOTIFIED BY: PAT MINAHAN |LAST UPDATE DATE: 08/09/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KRISS KENNEDY R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION - FISH KILL | | | | The licensee reported finding 300 dead shad to the Texas Parks and Wildlife | | Department. The shad were observed in the Circ water discharge. This | | condition is believed to be the result of local weather and not due to a | | spill or plant related event. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37217 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. AIR FORCE |NOTIFICATION DATE: 08/09/2000| |LICENSEE: U.S. AIR FORCE |NOTIFICATION TIME: 16:35[EDT]| | CITY: REGION: 4 |EVENT DATE: 08/08/2000| | COUNTY: LINCOLN STATE: NV |EVENT TIME: 16:30[PDT]| |LICENSE#: 422353901-AF AGREEMENT: Y |LAST UPDATE DATE: 08/09/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KRISS KENNEDY R4 | | |C.W. (BILL) REAMER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MARK WROBEL | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TWO AM-241 SOURCES LOST IN CRASH OF AIRCRAFT | | | | On 8/8/00, at approximately 1630 PDT, an F-16 crashed on a mountain north of | | Glendale, NV. The aircraft was equipped with a LANTIRN pod, which contains | | two 4 �Ci Am-241 sources (registry number NR-0136-S-0208-5; Amersham model | | AMM.7). The crash occurred approximately 5,000 feet up the side of a | | mountain that is approximately 7,000 feet high in a very remote location. | | The Air Force incident investigation team has not yet accessed the crash | | site. Wreckage is reported to be spread along a 1,000 foot distance. The | | licensee will make reasonable efforts to retrieve the sources. | | | | The licensee has already contacted NRC Region IV (Gaines) regarding this | | event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37218 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 08/09/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 19:06[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/09/2000| +------------------------------------------------+EVENT TIME: 17:51[EDT]| | NRC NOTIFIED BY: JOHN GARECHT |LAST UPDATE DATE: 08/09/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP | | | | Salem Unit 1 experienced an automatic reactor trip due to unknown causes. | | The first out annunciator was "Power Range Negative Flux Rate Hi." All | | control rods inserted following the trip and all systems functioned as | | expected. The auxiliary feedwater system automatically started as expected. | | The unit is stable in Hot Standby with decay heat being exhausted to the | | main condenser via the steam dumps. | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37219 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/10/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 01:55[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/09/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:20[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/10/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |RONALD GARDNER R3 | | DOCKET: 0707002 |C.W. (BILL) REAMER NMSS | +------------------------------------------------+FRANK CONGEL IRO | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BULLETIN 91-01 24 HOUR REPORT | | | | At 1520 hours on 8/9/00, it was discovered that a Nuclear Criticality Safety | | Approval (NCSA) non-compliance had occurred in the X-705 decontamination | | facility. During a routine walk-through by the NRC Resident Inspector, two | | (2) violations of the X-705 Inadvertent Containers NCSA, NCSA-0705_076, were | | noted. The conditions noted were as a follows: | | | | - An open plastic bag containing used personal protective clothing (PPE) was | | discovered lying in the Tunnel Basement. | | - A shelving unit, adjacent to the Microfiltration system was found to | | contain cardboard boxes, loosely wrapped in plastic. | | | | Both of these areas are covered by the controls of NCSA-0705_076. It was | | determined that these arrays had the potential to collect an unsafe | | configuration of Uranium-bearing material. | | | | This event resulted in the loss of one control (geometry/volume) of the | | double contingency control principle. The physical integrity of all nearby | | systems containing uranium-bearing material was maintained throughout this | | event. | | | | NCSA-0705_076 compliance was restored at 1620 hours when the on duty NCS | | engineer authorized the removal of these items from there respective areas. | | | | The licensee informed the NRC resident inspector that this report would be | | made. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021