Event Notification Report for August 9, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/08/2000 - 08/09/2000 ** EVENT NUMBERS ** 37212 37213 37214 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37212 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 08/08/2000| | UNIT: [] [3] [] STATE: PA |NOTIFICATION TIME: 01:24[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 08/07/2000| +------------------------------------------------+EVENT TIME: 21:26[EDT]| | NRC NOTIFIED BY: WINGFIELD |LAST UPDATE DATE: 08/08/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE DOERFLEIN R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM FROM 100% POWER ON A FALSE LOW REACTOR WATER LEVEL INDICATION | | | | The Unit experienced an automatic reactor scram when an instrument line | | "root" valve failed causing a water leak which resulted in a false low | | reactor water level signal indication to be sensed by the RPS. The water | | leak was immediately isolated by the ESF actuation of the Excess Flow Check | | Valve in the same reactor instrumentation line. All rods fully inserted, no | | ECCS injection occurred, no relief valves lifted and all safety systems | | responded correctly. The plant also had actuation of the Primary | | Containment Isolation System following the reactor scram. | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37213 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 08/08/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 10:42[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/08/2000| +------------------------------------------------+EVENT TIME: 08:39[CDT]| | NRC NOTIFIED BY: SCHOTTEL |LAST UPDATE DATE: 08/08/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AENS 50.72(b)(1)(v) ENS INOPERABLE | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAS LOST ENS, STATE NOTIFICATION PHONE LINES AND LOCAL COMMERCIAL | | PHONE LINES. | | | | THE ENS LINES, DIRECT LINES TO THE STATE, AND LOCAL COMMERCIAL LINES HAVE | | BEEN CUT RESULTING IN THE LOSS OF THE USE OF THESE PHONE SYSTEMS. HOWEVER, | | THEY DO HAVE OPERABLE FOREIGN EXCHANGE B/U PHONES AVAILABLE, SO THAT | | EMERGENCY RESPONSE CAPABILITY IS NOT AFFECTED. THE TELEPHONE COMPANY IS | | AWARE OF THE PROBLEM AND IS CURRENTLY WORKING ON IT. THE LICENSEE ALSO HAS | | A SATELLITE PHONE AVAILABLE | | | | THE NRC RESIDENT INSPECTOR AND THE STATE HAVE BEEN INFORMED. | | | | * * * UPDATE 1453 8/8/2000 FROM SCHOTTEL TAKEN BY STRANSKY * * * | | | | All telephone lines have been restored. The NRC resident inspector has been | | informed. Notified R3DO (Gardner). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37214 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 08/08/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 21:35[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/08/2000| +------------------------------------------------+EVENT TIME: 18:44[EDT]| | NRC NOTIFIED BY: FREDERICK SMITH |LAST UPDATE DATE: 08/08/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 99 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOSTART OF ANNULUS EXHAUST GAS TREATMENT SYSTEM FAN DURING TESTING | | | | "During performance of surveillance testing, the lifting of an incorrect | | lead caused a low flow condition on the in service AEGTS fan. This caused | | the auto start of the standby AEGTS fan. No low flow alarm was received on | | the in service fan, but the system functioned properly." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021