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Alert

Due to a lapse in appropriations, the NRC has ceased normal operations. However, excepted and exempted activities necessary to maintain critical health and safety functions—as well as essential progress on designated critical activities, including those specified in Executive Order 14300—will continue, consistent with the OMB-Approved NRC Lapse Plan.

Event Notification Report for August 9, 2000

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           08/08/2000 - 08/09/2000

                              ** EVENT NUMBERS **

37212  37213  37214  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37212       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PEACH BOTTOM             REGION:  1  |NOTIFICATION DATE: 08/08/2000|
|    UNIT:  [] [3] []                 STATE:  PA |NOTIFICATION TIME: 01:24[EDT]|
|   RXTYPE: [2] GE-4,[3] GE-4                    |EVENT DATE:        08/07/2000|
+------------------------------------------------+EVENT TIME:        21:26[EDT]|
| NRC NOTIFIED BY:  WINGFIELD                    |LAST UPDATE DATE:  08/08/2000|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LAWRENCE DOERFLEIN   R1      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|3     A/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR SCRAM FROM 100% POWER ON A FALSE LOW REACTOR WATER LEVEL INDICATION  |
|                                                                              |
| The Unit experienced an automatic reactor scram when an instrument line      |
| "root" valve failed causing a water leak which resulted in a false low       |
| reactor water level signal indication to be sensed by the RPS.  The water    |
| leak was immediately isolated by the ESF actuation of the Excess Flow Check  |
| Valve in the same reactor instrumentation line.  All rods fully inserted, no |
| ECCS injection occurred,  no relief valves lifted and all safety systems     |
| responded correctly.  The plant also had actuation of the Primary            |
| Containment Isolation System following the reactor scram.                    |
|                                                                              |
| The NRC Resident Inspector will be notified.                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37213       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CLINTON                  REGION:  3  |NOTIFICATION DATE: 08/08/2000|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 10:42[EDT]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        08/08/2000|
+------------------------------------------------+EVENT TIME:        08:39[CDT]|
| NRC NOTIFIED BY:  SCHOTTEL                     |LAST UPDATE DATE:  08/08/2000|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD GARDNER       R3      |
|10 CFR SECTION:                                 |                             |
|AENS 50.72(b)(1)(v)      ENS INOPERABLE         |                             |
|AARC 50.72(b)(1)(v)      OTHER ASMT/COMM INOP   |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PLANT HAS LOST ENS, STATE NOTIFICATION PHONE LINES AND LOCAL COMMERCIAL      |
| PHONE LINES.                                                                 |
|                                                                              |
| THE ENS LINES, DIRECT LINES TO THE STATE, AND LOCAL COMMERCIAL LINES HAVE    |
| BEEN CUT RESULTING IN THE LOSS OF THE USE OF THESE PHONE SYSTEMS.  HOWEVER,  |
| THEY DO HAVE OPERABLE FOREIGN EXCHANGE B/U PHONES AVAILABLE, SO THAT         |
| EMERGENCY RESPONSE CAPABILITY IS NOT AFFECTED.  THE TELEPHONE COMPANY IS     |
| AWARE OF THE PROBLEM AND IS CURRENTLY WORKING ON IT.  THE LICENSEE ALSO HAS  |
| A SATELLITE PHONE AVAILABLE                                                  |
|                                                                              |
| THE NRC RESIDENT INSPECTOR AND THE STATE HAVE BEEN INFORMED.                 |
|                                                                              |
| * * * UPDATE 1453 8/8/2000 FROM SCHOTTEL TAKEN BY STRANSKY * * *             |
|                                                                              |
| All telephone lines have been restored. The NRC resident inspector has been  |
| informed. Notified R3DO (Gardner).                                           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37214       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PERRY                    REGION:  3  |NOTIFICATION DATE: 08/08/2000|
|    UNIT:  [1] [] []                 STATE:  OH |NOTIFICATION TIME: 21:35[EDT]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        08/08/2000|
+------------------------------------------------+EVENT TIME:        18:44[EDT]|
| NRC NOTIFIED BY:  FREDERICK SMITH              |LAST UPDATE DATE:  08/08/2000|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD GARDNER       R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       99       Power Operation  |99       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOSTART OF ANNULUS EXHAUST GAS TREATMENT SYSTEM FAN DURING TESTING         |
|                                                                              |
| "During performance of surveillance testing, the lifting of an incorrect     |
| lead caused a low flow condition on the in service AEGTS fan. This caused    |
| the auto start of the standby AEGTS fan. No low flow alarm was received on   |
| the in service fan, but the system functioned properly."                     |
|                                                                              |
| The NRC resident inspector has been informed of this event by the licensee.  |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Wednesday, March 24, 2021

Page Last Reviewed/Updated Wednesday, March 24, 2021