Event Notification Report for August 7, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/04/2000 - 08/07/2000 ** EVENT NUMBERS ** 37197 37208 37209 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37197 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NATIONAL INST OF STANDARDS & TECH |NOTIFICATION DATE: 07/28/2000| |LICENSEE: NATIONAL INST OF STANDARDS & TECH |NOTIFICATION TIME: 14:29[EDT]| | CITY: GAITHERSBURG REGION: 1 |EVENT DATE: 07/10/2000| | COUNTY: STATE: MD |EVENT TIME: [EDT]| |LICENSE#: SNM-362 AGREEMENT: Y |LAST UPDATE DATE: 08/04/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MOHAMED SHANBAKY R1 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM O'REAR | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIALLY LEAKING SOURCE | | | | A 5mCi Sr-90 source in the form of a brachytherapy seed used for | | investigational purposes may be leaking. There is no known personnel | | exposure or spread of contamination involved. The source was manufactured | | by Novoste which is located in GA . The evaluation will continue to | | determine whether the source is actually leaking. | | | | * * * UPDATE ON 08/04/00 AT 1459 ET BY JIM O'REAR TAKEN BY MACKINNON * * * | | | | Up on further investigation it was determined that the brachytherapy seed | | was damaged by NIST personnel during calibration work. The seed was | | packaged up and returned to AEA Technologies located in Massachusetts. NRC | | Region 1, John McGrath, was informed of this update by NIST. NRC R1DO (Jack | | McFadden) and NMSS EO (John Hickey) notified. | | | | Correction To Initial Report: The brachytherapy seed was manufactured by | | AEA Technologies for Novoste. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37208 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 08/05/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 08:07[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/05/2000| +------------------------------------------------+EVENT TIME: 04:28[EDT]| | NRC NOTIFIED BY: STUART BYRD |LAST UPDATE DATE: 08/05/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEORGE BELISLE R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A MINIMAL AMOUNT OF WATER IN THE REACTOR CORE ISOLATION COOLING | | OIL SYSTEM | | | | The following text is a portion of a facsimile received from the licensee: | | | | "EVENT: The Unit 2 the Reactor Core Isolation Cooling (RCIC) system was | | discovered to have a minimal amount of water in the oil system. Following | | investigation of the event and replacement of the oil, the RCIC turbine was | | successfully manually started and operated normally. During a subsequent | | automatic start for post-maintenance test requirements, the turbine tripped | | on high exhaust pressure apparently caused by the governor system's slow | | response time. Investigation of the turbine control system is continuing." | | | | "CORRECTIVE ACTION(S): Continue the investigation to determine the root | | cause of the water in the oil system and the response of the governor | | control system." | | | | "INITIAL SAFETY SIGNIFICANCE EVALUATION: Minimal. The High Pressure | | Coolant Injection System, Automatic [Depressurization] System, Low Pressure | | Core Spray, and the Low Pressure Coolant Injection System were operable | | throughout the event." | | | | The licensee stated that, as a result of this issue, the unit is currently | | in a 14-day limiting condition for operation in accordance with Technical | | Specification 3.5.2. The licensee also stated that all other systems | | functioned as required. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37209 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 08/05/2000| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 21:45[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 08/05/2000| +------------------------------------------------+EVENT TIME: 20:54[EDT]| | NRC NOTIFIED BY: J SCHORK |LAST UPDATE DATE: 08/05/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK MCFADDEN R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DURING TESTING ONE CUBICLE OF THE CONTROL BUILDING ENVELOPE, THE 1D 4160 | | VOLT SWITCHGEAR ROOM WAS FOUND TO BE SLIGHTLY NEGATIVE IN PRESSURE. | | | | "At 2054 hours on Saturday, August 5, 2000-AmerGen identified a condition | | that is outside the design basis at TMI Unit 1. Functional testing of the | | TMI-1 Control Building Envelope {CBE} was in process to verify that the | | design basis of the Control Building Emergency Ventilation System had been | | maintained following plant | | modifications to improve the reliability of the system. Results of the | | Functional testing found that one cubicle of the Control Building Envelope, | | the 1D 4160 Volt Switchgear room, located on the 338' elevation of the | | Control Tower, 1 floor below the Control Room, was slightly negative in | | regards to internal atmospheric pressure as compared to outside air | | pressure. The TMI-1 UFSAR, Update 15 states in section 7.4.5.2.1 in part: | | | | " ....A positive pressure of > or equal to 0.10 inches w.g. {water gauge} is | | not a criterion for the entire CBE. The pressure requirement in the cubicles | | of the CBE, other than the Main Control Room, is that they are maintained at | | a positive pressure with respect to the areas outside the CBE. | | | | "The functional testing found that the ID 4160 Switchgear room was | | approximately 0.04 inches w.g. negative in regards to areas outside the CBE. | | Subsequent adjustments to the Control Building Emergency Ventilation System | | restored the area to a positive pressure in regards to areas outside the | | CBE. Additional evaluation and testing is in progress to determine the root | | cause of the event. | | | | "The potential consequences of the condition found are believed to be | | minimal. No actual in-leakage pathway was identified and if the Control | | Building Emergency Ventilation System been called upon to operate in the | | re-circulation mode and had in-leakage occurred, the air in-leakage would | | have been filtered by the CBEVS | | charcoal filters prior to supply to the Control Room. Thus, the dose | | consequences to the operators would have been very minimal due to the low | | amount of in-leakage and filtration prior to supply to the control room." | | | | A follow up 30 day LER will be submitted. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021