Event Notification Report for July 20, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/19/2000 - 07/20/2000 ** EVENT NUMBERS ** 37107 37158 37178 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37107 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 06/22/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 18:07[EDT]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 06/22/2000| +------------------------------------------------+EVENT TIME: 14:07[CDT]| | NRC NOTIFIED BY: BORING |LAST UPDATE DATE: 07/19/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT ENTERED A 14 DAY LCO ACTION STATEMENT DUE TO HIGH PRESSURE COOLANT | | INJECTION (HPCI) SYSTEM BEING DECLARED INOPERABLE. | | | | During routine surveillance testing of the Containment Cooling Water System | | (CCWS), required system flow through the HPCI Room Cooler could not be | | obtained due to leakage past 2-3999-252 check valve. | | | | With the HPCI Room Cooler inoperable, the HPCI System was declared | | INOPERABLE, a 14 day LCO Action Statement was entered, and an action request | | for repair of the 2-3999-252 valve was submitted. | | | | The NRC Resident Inspector was notified by the licensee. | | | | * * * UPDATE AT 1917 ON 07/19/00 BY MARK RUNION TO JOLLIFFE * * * | | | | Upon further review of this event by Dresden Operations and Engineering | | Department personnel, the licensee determined that with the HPCI Room Cooler | | blower available, even without CCWS flow to the HPCI Room Cooler, the HPCI | | System will perform its required function and remain operable. Thus, the | | HPCI System was not inoperable at the time of the notification of this event | | and therefore, this event is not reportable to the NRC. Based on this, the | | licensee desires to retract this event. | | | | The licensee notified the NRC Resident Inspector. The NRC Operations | | Officer notified the R3DO Mike Parker. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37158 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 07/10/2000| | UNIT: [3] [4] [] STATE: FL |NOTIFICATION TIME: 17:28[EDT]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 07/10/2000| +------------------------------------------------+EVENT TIME: 10:38[EDT]| | NRC NOTIFIED BY: JAMES RUSSELL |LAST UPDATE DATE: 07/19/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEORGE BELISLE R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | |4 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY REPORT | | | | A licensed training supervisor tested positive for alcohol use during a | | random drug and alcohol test. The individual's access has been suspended and | | the licensee will review the individual's work for the past 90 days. The NRC | | resident inspector has been informed of this event by the licensee. | | | | * * * RETRACTION ON 07/19/00 AT 1122 ET BY STEWART TAKEN BY MACKINNON * * * | | | | After discussions with NRC Region 2 it was determined that the above | | reported event did not have to be reported and is being withdrawn. The | | individual was not a supervisor at the time of the event. This report will | | be reported on the licensee's Semi - Annual Fitness for Duty Report. NRC | | R2DO (Bonser) notified. | | | | The NRC Resident Inspector was notified of this update by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37178 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 07/20/2000| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 04:28[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 07/20/2000| +------------------------------------------------+EVENT TIME: 03:52[EDT]| | NRC NOTIFIED BY: TESORIERO |LAST UPDATE DATE: 07/20/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GREGORY CRANSTON R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT OUTSIDE OF DESIGN BASIS | | | | "On July 20, 2000 at 0352 hours a Reactor Coolant system leakrate of 0.30 | | gpm was calculated. Currently the Charging and Letdown systems are isolated | | for maintenance. Investigation revealed the leakage being from the Excess | | Letdown system to the systems isolated for maintenance, which are located | | outside Containment. This leakrate exceeds the limit of 0.68 gph outside | | Containment and therefore is a condition outside the design basis of the | | plant. The Control Room Ventilation system is inoperable and a 72 hour | | limiting condition of operation has been entered." | | | | The NRC resident inspector will be informed of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021