Event Notification Report for July 14, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/13/2000 - 07/14/2000 ** EVENT NUMBERS ** 37138 37165 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37138 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 06/30/2000| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 15:43[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 06/13/2000| +------------------------------------------------+EVENT TIME: 14:00[EDT]| | NRC NOTIFIED BY: MARK MAGNUSON |LAST UPDATE DATE: 07/13/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |SCOTT MORRIS R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT OUTSIDE OF DESIGN BASIS | | | | "On 6/13/00, Vermont Yankee (VY) discovered that a turbine building to | | radwaste hallway door had been breached open for maintenance activities | | without proper engineering review. The condition has been corrected. | | | | "The door serves as a high energy line break (HELB) barrier such that a HELB | | in the turbine building would not propagate into the radwaste hallway and | | cause subsequent failure of masonry block wall between the hallway and the | | main plant switchgear rooms. Redundant equipment in the switchgear rooms is | | not qualified for operation in the environment postulated by the TB HELB. | | | | "VY review has determined that a compensatory measure to close the door in | | the event of a HELB that had been established at the time of the maintenance | | activities would not have provided adequate protection against the | | postulated HELB. | | | | "Based on the above, this condition is reportable in accordance with 10 CFR | | 50.72(b)(1)(ii)(B) as a condition found during operation that results in a | | condition that is outside the design basis of the plant." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * RETRACTED AT 1831 EDT ON 7/13/00 BY MARK MAGNUSON TO FANGIE JONES * * | | * | | | | "On June 30, 2000 Vermont Yankee reported that a planned compensatory | | measure associated with a breached door would not have been adequate to | | protect plant equipment in the unlikely event of a high energy line break in | | the turbine building. The condition was reported under 10 CFR | | 50.72(b)(1)(ii)(B) as a condition that was outside the design basis. The | | associated NRC event number is 37138. | | | | "Vermont Yankee has since determined that the door had not been tied open | | for a period of time greater than the 24 hours allowed by VY technical | | specifications for equipment that may have been affected by the high energy | | line break. In addition, VY assessment has concluded that redundant | | equipment would not have been challenged and that the overall risk of the | | short term event was minimal. | | | | "Based on this information, the 50.72 ENS notification is retracted." | | | | The licensee notified the NRC Resident Inspector. The NRC Operations | | Officer notified the R1DO (Richard Conte). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37165 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 07/13/2000| | UNIT: [1] [2] [] STATE: MD |NOTIFICATION TIME: 16:43[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 07/13/2000| +------------------------------------------------+EVENT TIME: 16:00[EDT]| | NRC NOTIFIED BY: TIM RITI |LAST UPDATE DATE: 07/13/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL ROOM RADIATION SIGNAL DISCOVERED NOT TO FUNCTION AS DESIGNED DURING | | LOSS OF OFFSITE POWER | | | | The licensee discovered that the control room radiation signal would not | | function as designed during the loss of offsite power. They have taken | | manual action per technical specifications to insure proper action during | | the loss of offsite power. A written LER will be submitted within 30 days. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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