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Event Notification Report for July 13, 2000

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           07/12/2000 - 07/13/2000

                              ** EVENT NUMBERS **

37163  37164  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37163       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LASALLE                  REGION:  3  |NOTIFICATION DATE: 07/11/2000|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 21:40[EDT]|
|   RXTYPE: [1] GE-5,[2] GE-5                    |EVENT DATE:        07/11/2000|
+------------------------------------------------+EVENT TIME:        19:50[CDT]|
| NRC NOTIFIED BY:  RUSSELL BENNETT              |LAST UPDATE DATE:  07/12/2000|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |BRUCE JORGENSEN      R3      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT OUTSIDE DESIGN BASIS DUE TO 10 CFR PART 50, APPENDIX R ISSUE            |
|                                                                              |
| "At approximately 1610 on 7/11/2000, it was identified by plant walkdown     |
| that in electrical switchgear Bus 142Y (1AP06B) cubicle 4 (for the Unit 1 B  |
| Residual Heat Removal pump) that an unsealed borehole of approximately three |
| (3) inches in diameter existed. This borehole is located in the floor        |
| separating the Unit 1 Division 2 Switchgear room from the Unit 1 Division 1  |
| switchgear room. The borehole is located in a three (3) hour rated fire      |
| barrier that is required by Administrative Technical Requirement 3/4.7.6     |
| (Fire Rated Assemblies). This has been considered an event that is outside   |
| the design basis due to required design basis protective features for safe   |
| shutdown trains as described in 10 CFR 50, Appendix R and Final Safety       |
| Analysis Report [being] lacking. Compensatory measures (fire watches) have   |
| been established per Administrative Technical Specifications and plans for   |
| repairs are in progress."                                                    |
|                                                                              |
| The NRC resident inspector has been notified of this event by the licensee.  |
|                                                                              |
| * * * UPDATE 1155 7/12/00 FROM ROCKY HASTY TAKEN BY BOB STRANSKY * * *       |
|                                                                              |
| "Additionally, on 7/7/2000, another unsealed borehole of 2.75 inches in      |
| diameter was identified in non-safety Switchgear bus 152 (1AP02B) cubicle 4. |
| Both boreholes are located in the floor separating the Unit 1 Division 1     |
| switchgear room from the Unit 1 Division 2 Switchgear room. Both boreholes   |
| are in a three (3) hour rated fire barrier that is required by               |
| Administrative Technical Requirement 3/4.7.6 (Fire Rated Assemblies). This   |
| has been considered an event that is outside the design basis due to         |
| required design basis protective features for safe shutdown trains as        |
| described in 10 CFR 50, Appendix R and Final Safety Analysis Report (FSAR)   |
| [being] lacking."                                                            |
|                                                                              |
| The NRC resident inspector has been informed of this update. Notified R3DO   |
| (Jorgensen).                                                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   37164       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  LAW ENG. AND ENV. SERVICES           |NOTIFICATION DATE: 07/12/2000|
|LICENSEE:  LAW ENG. AND ENV. SERVICES           |NOTIFICATION TIME: 12:39[EDT]|
|    CITY:  ALPHERETTA               REGION:  2  |EVENT DATE:        07/11/2000|
|  COUNTY:                            STATE:  GA |EVENT TIME:             [EDT]|
|LICENSE#:  45-21498-01           AGREEMENT:  Y  |LAST UPDATE DATE:  07/12/2000|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |THOMAS DECKER        R2      |
|                                                |DONALD COOL          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DAVID RUMWILL                |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAB1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MISSING MOISTURE/DENSITY GAUGE                                               |
|                                                                              |
| The licensee reported that a Troxler Model 3411 nuclear moisture/density     |
| gauge containing 8 mCi of Cs-137 and 40 mCi of Am-241/Be (S/N 18561) was     |
| missing from the Sterling, VA area. A company employee, who resides in West  |
| Virginia, was scheduled to bring the gauge to a job site in the northern VA  |
| area on 7/11/2000, but failed to show up. Neither the individual, the        |
| company vehicle that he was using, nor the gauge can be located. The company |
| last had contact with the employee on 7/7/2000. The licensee did not believe |
| that the individual was a disgruntled employee. The licensee has contacted   |
| local law enforcement agencies regarding the missing individual and gauge.   |
+------------------------------------------------------------------------------+


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