Event Notification Report for July 13, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/12/2000 - 07/13/2000 ** EVENT NUMBERS ** 37163 37164 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37163 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 07/11/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 21:40[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 07/11/2000| +------------------------------------------------+EVENT TIME: 19:50[CDT]| | NRC NOTIFIED BY: RUSSELL BENNETT |LAST UPDATE DATE: 07/12/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT OUTSIDE DESIGN BASIS DUE TO 10 CFR PART 50, APPENDIX R ISSUE | | | | "At approximately 1610 on 7/11/2000, it was identified by plant walkdown | | that in electrical switchgear Bus 142Y (1AP06B) cubicle 4 (for the Unit 1 B | | Residual Heat Removal pump) that an unsealed borehole of approximately three | | (3) inches in diameter existed. This borehole is located in the floor | | separating the Unit 1 Division 2 Switchgear room from the Unit 1 Division 1 | | switchgear room. The borehole is located in a three (3) hour rated fire | | barrier that is required by Administrative Technical Requirement 3/4.7.6 | | (Fire Rated Assemblies). This has been considered an event that is outside | | the design basis due to required design basis protective features for safe | | shutdown trains as described in 10 CFR 50, Appendix R and Final Safety | | Analysis Report [being] lacking. Compensatory measures (fire watches) have | | been established per Administrative Technical Specifications and plans for | | repairs are in progress." | | | | The NRC resident inspector has been notified of this event by the licensee. | | | | * * * UPDATE 1155 7/12/00 FROM ROCKY HASTY TAKEN BY BOB STRANSKY * * * | | | | "Additionally, on 7/7/2000, another unsealed borehole of 2.75 inches in | | diameter was identified in non-safety Switchgear bus 152 (1AP02B) cubicle 4. | | Both boreholes are located in the floor separating the Unit 1 Division 1 | | switchgear room from the Unit 1 Division 2 Switchgear room. Both boreholes | | are in a three (3) hour rated fire barrier that is required by | | Administrative Technical Requirement 3/4.7.6 (Fire Rated Assemblies). This | | has been considered an event that is outside the design basis due to | | required design basis protective features for safe shutdown trains as | | described in 10 CFR 50, Appendix R and Final Safety Analysis Report (FSAR) | | [being] lacking." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Jorgensen). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37164 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: LAW ENG. AND ENV. SERVICES |NOTIFICATION DATE: 07/12/2000| |LICENSEE: LAW ENG. AND ENV. SERVICES |NOTIFICATION TIME: 12:39[EDT]| | CITY: ALPHERETTA REGION: 2 |EVENT DATE: 07/11/2000| | COUNTY: STATE: GA |EVENT TIME: [EDT]| |LICENSE#: 45-21498-01 AGREEMENT: Y |LAST UPDATE DATE: 07/12/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS DECKER R2 | | |DONALD COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DAVID RUMWILL | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING MOISTURE/DENSITY GAUGE | | | | The licensee reported that a Troxler Model 3411 nuclear moisture/density | | gauge containing 8 mCi of Cs-137 and 40 mCi of Am-241/Be (S/N 18561) was | | missing from the Sterling, VA area. A company employee, who resides in West | | Virginia, was scheduled to bring the gauge to a job site in the northern VA | | area on 7/11/2000, but failed to show up. Neither the individual, the | | company vehicle that he was using, nor the gauge can be located. The company | | last had contact with the employee on 7/7/2000. The licensee did not believe | | that the individual was a disgruntled employee. The licensee has contacted | | local law enforcement agencies regarding the missing individual and gauge. | +------------------------------------------------------------------------------+
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