Event Notification Report for July 5, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/03/2000 - 07/05/2000 ** EVENT NUMBERS ** 37140 37141 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37140 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 07/03/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 11:10[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 07/03/2000| +------------------------------------------------+EVENT TIME: 10:20[EDT]| | NRC NOTIFIED BY: BERNARD HORNING |LAST UPDATE DATE: 07/03/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVEN DENNIS R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF THE 'A' REACTOR PROTECTION SYSTEM BUS CAUSING MULTIPLE AUTOMATIC | | ACTIONS | | | | The unit experienced a loss of 'A' reactor protection system (RPS) bus. RPS | | motor generator output breakers opened and deenergized the bus, this caused | | the 'A' standby gas treatment to automatically start. Also the 'A' | | hydrogen/oxygen monitor isolation valves closed, reactor building | | ventilation isolated, and the reactor water cleanup system tripped due to | | isolation valve closure. | | | | This trip appears to be "identical" to a trip reported on 6/26/00, event | | #37119. | | | | The licensee has energized the 'A' RPS bus and returned all systems to | | normal operation with the exception of reactor water cleanup, which is being | | restored. | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37141 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 07/04/2000| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 14:13[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 07/04/2000| +------------------------------------------------+EVENT TIME: 11:54[EDT]| | NRC NOTIFIED BY: FITCH |LAST UPDATE DATE: 07/04/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVEN DENNIS R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD ESF ACTUATIONS DUE TO LOSS OF THE "B" RPS BUS. | | | | "While operating at 100% power, Susquehanna Unit 2, experienced ESF | | actuations for containment isolations as a result of an unexpected loss of | | "B" RPS Bus caused by a trip of the RPS MG Set Output Breaker. All | | containment isolations associated with a loss of "B" RPS Bus actuated and | | went to completion. "B" RPS power was swapped to the alternate power supply | | and affected systems restored to normal configuration." | | | | The actuations received were cooling water to recirc pump isolation, RWCU | | isolation, containment sampling isolation, reactor building secondary | | containment isolations and coolant sampling isolations. They also had | | standby gas treatment initiation. The cause of the trip of the MG set is | | being investigated. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021