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Due to a lapse in appropriations, the NRC has ceased normal operations. However, excepted and exempted activities necessary to maintain critical health and safety functions—as well as essential progress on designated critical activities, including those specified in Executive Order 14300—will continue, consistent with the OMB-Approved NRC Lapse Plan.

Event Notification Report for July 5, 2000

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           07/03/2000 - 07/05/2000

                              ** EVENT NUMBERS **

37140  37141  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37140       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FITZPATRICK              REGION:  1  |NOTIFICATION DATE: 07/03/2000|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 11:10[EDT]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        07/03/2000|
+------------------------------------------------+EVENT TIME:        10:20[EDT]|
| NRC NOTIFIED BY:  BERNARD HORNING              |LAST UPDATE DATE:  07/03/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |STEVEN DENNIS        R1      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOSS OF THE 'A' REACTOR PROTECTION SYSTEM BUS CAUSING MULTIPLE AUTOMATIC     |
| ACTIONS                                                                      |
|                                                                              |
| The unit experienced a loss of 'A' reactor protection system (RPS) bus.  RPS |
| motor generator output breakers opened and deenergized the bus, this caused  |
| the 'A' standby gas treatment to automatically start.  Also the 'A'          |
| hydrogen/oxygen monitor isolation valves closed, reactor building            |
| ventilation isolated, and the reactor water cleanup system tripped due to    |
| isolation valve closure.                                                     |
|                                                                              |
| This trip appears to be "identical" to a trip reported on 6/26/00, event     |
| #37119.                                                                      |
|                                                                              |
| The licensee has energized the 'A' RPS bus and returned all systems to       |
| normal operation with the exception of reactor water cleanup, which is being |
| restored.                                                                    |
|                                                                              |
| The licensee has notified the NRC Resident Inspector.                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37141       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUSQUEHANNA              REGION:  1  |NOTIFICATION DATE: 07/04/2000|
|    UNIT:  [] [2] []                 STATE:  PA |NOTIFICATION TIME: 14:13[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        07/04/2000|
+------------------------------------------------+EVENT TIME:        11:54[EDT]|
| NRC NOTIFIED BY:  FITCH                        |LAST UPDATE DATE:  07/04/2000|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |STEVEN DENNIS        R1      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE PLANT HAD ESF ACTUATIONS DUE TO LOSS OF THE "B" RPS BUS.                 |
|                                                                              |
| "While operating at 100% power, Susquehanna Unit 2, experienced ESF          |
| actuations for containment isolations as a result of an unexpected loss of   |
| "B" RPS Bus caused by a trip of the RPS MG Set Output Breaker.  All          |
| containment isolations associated with a loss of "B" RPS Bus actuated and    |
| went to completion. "B" RPS power was swapped to the alternate power supply  |
| and affected systems restored to normal configuration."                      |
|                                                                              |
| The actuations received were cooling water to recirc pump isolation, RWCU    |
| isolation, containment sampling isolation, reactor building secondary        |
| containment isolations and coolant sampling isolations.  They also had       |
| standby gas treatment initiation.  The cause of the trip of the MG set is    |
| being investigated.                                                          |
|                                                                              |
| The NRC Resident Inspector was notified.                                     |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021

Page Last Reviewed/Updated Thursday, March 25, 2021