Event Notification Report for June 29, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/28/2000 - 06/29/2000 ** EVENT NUMBERS ** 37127 37128 37129 37130 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37127 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 06/28/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 13:19[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 06/28/2000| +------------------------------------------------+EVENT TIME: 12:50[EDT]| | NRC NOTIFIED BY: ROY GILLOW |LAST UPDATE DATE: 06/28/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |SCOTT MORRIS R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MONTHLY SIREN TEST FAILED | | | | On 6/26/00 at 0915 EDT, the offsite emergency siren silent test failed at | | both the Wayne County EOC and the 911 actuation center. Upon arrival of | | maintenance personnel, the test was completed satisfactorily. Root cause | | for the test failure has not been determined. | | | | The licensee was not notified until 1250 EDT on 6/28/00. There is an | | investigation in progress to determine the root cause of the test failure. | | | | | | The licensee notified the NRC Resident Inspector and the local authorities. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37128 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 06/28/2000| | UNIT: [1] [2] [] STATE: TN |NOTIFICATION TIME: 21:08[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/28/2000| +------------------------------------------------+EVENT TIME: 20:20[EDT]| | NRC NOTIFIED BY: CHRIS REEVES |LAST UPDATE DATE: 06/28/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT | | | | SAFEGUARDS SYSTEM DEGRADATION RELATED TO PERIMETER MONITORING. IMMEDIATE | | COMPENSATORY MEASURES NOT FULLY IMPLEMENTED WITHIN THE TIME REQUIRED BY THE | | SECURITY PLAN. COMPENSATORY MEASURES NOW ARE FULLY IMPLEMENTED. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. CONTACT THE | | HEADQUARTERS OPERATIONS OFFICER FOR ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37129 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 06/28/2000| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 22:31[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/28/2000| +------------------------------------------------+EVENT TIME: 22:24[EDT]| | NRC NOTIFIED BY: STEVE CHERBA |LAST UPDATE DATE: 06/28/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 79 Power Operation |79 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 COMMENCED A TECH SPEC REQUIRED SHUTDOWN AFTER TWO IRPIs IN THE SAME | | GROUP WERE DECLARED INOPERABLE | | | | The following information was received by fax: | | | | Notification time: 2231 hrs EDT 6-28-00 | | Event Notification No.: 37129 | | NRC Contact: Steve Sandin | | Cook Caller: SJ Cherba | | Power Level Prior to event: 79.6% | | | | Notification Script: | | | | This is Steve Cherba at the Cook Unit 2 Nuclear Plant making a one hour, | | non-emergency notification for initiation of a nuclear plant shutdown | | required by Technical Specifications in accordance with | | 10CFR50.72(b)(1)(i)(A). The shutdown was initiated to comply with TS 3.0.3 @ | | 2224 hrs EDT on 6-28-00. The TS 3.0.3 one hour limit for initiating a | | shutdown would have expired @ 2228 hrs EDT on 6-28-00. TS 3.0.3 was entered | | when it was discovered that the unit had two Individual Rod Position | | Indicators (IRPIs ) in one group that were INOPERABLE, exceeding the | | allowable actions of TS 3.1.3.2 a., which only allows a maximum of one | | INOPERABLE IRPI per rod group. These IRPIs became INOPERABLE when, without | | any associated rod movement, the indicated rod position drifted above the | | allowable rod deviation limit. Instrument technicians are in the process of | | calibrating these IRPIs and we expect to exit this situation within two | | hours without completing the shutdown. | | | | The control rod IRPIs were H12 & M8, both associated with Control Bank D, | | Group 2. | | | | Post Script to this notification: | | | | The two IRPIs were calibrated for drift caused by the RCS temperature | | increase associated with the unit power increase following the outage and | | are within allowable limits and OPERABLE @ 2250 hrs EDT 6-28-00. The | | shutdown was halted and power stabilized @ 2250 hrs EDT 6-28-00. NRC | | resident personnel were informed of the condition and shutdown at 2230 hrs | | EDT ( J Maynen) & 2240 hrs EDT ( B Bartlett). Power Level when shutdown | | stopped: 78.9%. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37130 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SIEMENS POWER CORPORATION |NOTIFICATION DATE: 06/29/2000| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 00:55[EDT]| | COMMENTS: LEU CONVERSION (UF6 to UO2) |EVENT DATE: 06/28/2000| | FABRICATION & SCRAP RECOVERY |EVENT TIME: 21:15[PDT]| | COMMERICAL LWR FUEL |LAST UPDATE DATE: 06/29/2000| | CITY: RICHLAND REGION: 4 +-----------------------------+ | COUNTY: BENTON STATE: WA |PERSON ORGANIZATION | |LICENSE#: SNM-1227 AGREEMENT: Y |GAIL GOOD R4 | | DOCKET: 07001257 |JOHN HICKEY NMSS | +------------------------------------------------+CHARLES MILLER IRO | | NRC NOTIFIED BY: LOREN MAAS |PETER PRESCOTT RCT | | HQ OPS OFFICER: DOUG WEAVER |GABRINI DOE | +------------------------------------------------+TURMAN NRC | |EMERGENCY CLASS: ALE | | |10 CFR SECTION: | | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ALERT DECLARED - OFFSITE FIRE | | | | RANGE FIRE ON AND ADJACENT TO THE HANFORD NUCLEAR RESERVATION HAS PROMPTED | | BENTON COUNTY EMERGENCY MANAGEMENT, IN CONJUNCTION WITH LOCAL LAW | | ENFORCEMENT, TO REQUIRE A PRECAUTIONARY EVACUATION OF THE HORN RAPIDS | | TRIANGLE INDUSTRIAL AREA IN WHICH THE SIEMENS FUEL FABRICATION PLANT IS | | LOCATED. THE PLANT PRODUCTION HAS BEEN SHUT DOWN. ESSENTIAL PLANT | | PERSONNEL ARE ONSITE. BASED ON DISTANCE AND CURRENT WIND DIRECTION, THE | | PLANT IS NOT THREATENED. | | | | * * * UPDATE AT 0451 ON 6/29/00 BY PROBASCO, RECEIVED BY WEAVER * * * | | | | THE ALERT WAS TERMINATED AT 0150 PDT BECAUSE THE FIRE HAS MOVED FURTHER AWAY | | FROM THE SITE AND IS CONTINUING TO MOVE IN THAT DIRECTION. | | | | NRC NOTIFIED RDO (GOOD); EO (HICKEY); IRO (MILLER); FEMA (STEINDURF); DOE | | (STAMBAUGH); NRC (TURMAN) | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021