Event Notification Report for June 26, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/23/2000 - 06/26/2000 ** EVENT NUMBERS ** 36263 37101 37109 37110 37111 37112 37113 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36263 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SWAGELOK COMPANY |NOTIFICATION DATE: 10/06/1999| |LICENSEE: SWAGELOK COMPANY |NOTIFICATION TIME: 09:48[EDT]| | CITY: Solon REGION: 3 |EVENT DATE: 10/04/1999| | COUNTY: STATE: OH |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 06/23/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN KINNEMAN R1 | | |BRIAN BONSER R2 | +------------------------------------------------+JOHN JACOBSON R3 | | NRC NOTIFIED BY: BRUCE FLUSCHE (Fax) |KRISS KENNEDY R4 | | HQ OPS OFFICER: LEIGH TROCINE |VERN HODGE NRR | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE 10-CFR-PART-21 REPORT REGARDING A POSSIBLE DEFECT IN A SWAGELOK | | TUBE FITTING | | | | The following text is a portion of a facsimile submitted by Swagelok | | Company: | | | | "This is a preliminary notification of a possible defect in a Swagelok tube | | fitting, part number SS-400-3-4TTM, male branch tee. A drawing of the part | | is included with this notification. We are also notifying each of the | | involved utilities." | | | | "We became aware of this on October 4, 1999." | | | | "The defect is a crack in the seat of the fitting. We are continuing our | | analysis of the part and will provide further details in accordance with NRC | | timetables." | | | | "[The] following are the six utilities to whom we have sold these parts: | | | | Georgia Power [Company], Plant Vogtle, ... , 10 pcs. ... [;] | | Duke Power Company, Oconee Nuclear Station, ... ,100 pcs. ... [;] | | Arizona Public Service Co., Palo Verde Nuclear Generating Station, ... , 15 | | pcs. ... [;] | | North Atlantic Energy Service Co., ... , Seabrook Station, ... ,10 pcs. ... | | [;] | | Virginia Power, Surry Power Station, ... , 3 pcs. ... [; and] | | Omaha Public Power District, Ft. Calhoun Nuclear Station, ... , 10 Pcs. ... | | ." | | | | (Call the NRC operations officer for Swagelok contact information.) | | | | * * * UPDATE AT 1553 EST ON 11/04/99 FROM BRUCE FLUSCHE TO S. SANDIN * * * | | | | The following information was received via fax: | | | | "We are writing further to our preliminary notification on October 6,1999, | | about a possible defect in a Swagelok tube fitting, part number | | SS-400-3-4TTM, male branch tee. | | | | "The utilities to whom we have sold this are repeated in the appendix to | | this letter. | | | | "As we reported earlier, the defect is a crack in the seat of the fitting. | | This crank resulted from overheating during the resistive type heated | | forging process; it was not a defect in the raw material. The estimated per | | cent of forgings that have this condition is less than 0.03%. | | | | "This forging was processed in December of 1996. Since the middle of 1998 | | we have required liquid penetrant testing on all resistive type heated | | forgings. | | | | "If there are any questions, please do not hesitate to contact us." | | | | The NRC operations officer notified the R1DO (Mohamed Shanbaky), R2DO | | (Pierce Skinner), R3DO (James Creed), and R4DO (Claude Johnson). This | | report was also faxed to NRR Part 21 (Vern Hodge). | | | | ******************** UPDATE AT 0934 ON 12/17/99 FROM BRUCE FLUSCHE TO | | TROCINE ******************** | | | | The following text is a portion of a facsimile submitted by Swagelok | | Company: | | | | "Further to our notice of November 18,1999, on Swagelok part number | | SS-400-3-4TTM, we are providing further information. As earlier reported | | the licensee below was not notified: | | | | Florida Power and Light | | P0. #00029212 | | 5 pcs. SS-400-3-4TTM | | Product ID. R17KLO5O9B" | | | | "The reason for the lack of notification was that the certification had not | | been entered into our database. The associate responsible for entering the | | certifications is no longer with Swagelok, and we have scheduled an audit of | | our database for the time period from June 1997 through July 1999, as we | | believe this is the time period that most needs to be scrutinized." | | | | "Whether further review of the database is necessary will be determined on | | the findings of this audit." | | | | The NRC operations officer notified the R1DO (Ruland), R2DO (Boland), R3DO | | (Gardner), and R4DO (Harrell). This report was also faxed to NRR Part 21 | | (Vern Hodge). | | | | * * * UPDATE AT 1100 ON 06/23/00 BY JAMES HANSON TO JOLLIFFE * * * | | | | Swagelok company personnel have determined that five additional | | certifications have been found where it cannot be verified that the | | corresponding licensees have been contacted. This includes licensees for | | the following plants: Susquehanna, North Anna, Duane Arnold, and San | | Onofre. | | | | The NRC Operations Officer notified the R1DO Bob Summers, R2DO Rudy | | Bernhard, R3DO Mike Jordan, R4DO Joe Tapia and NRR Vern Hodge (by fax). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37101 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 06/21/2000| |LICENSEE: PROFESSIONAL ENGINEERING & INSPECTION|NOTIFICATION TIME: 11:01[EDT]| | CITY: PLANTATION REGION: 2 |EVENT DATE: 06/21/2000| | COUNTY: STATE: FL |EVENT TIME: 06:30[EDT]| |LICENSE#: 2113-1 AGREEMENT: Y |LAST UPDATE DATE: 06/23/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KERRY LANDIS R2 | | |BOB AYRES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLEY ADAMS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING A STOLEN TROXLER GAUGE OWNED BY | | PROFESSIONAL ENGINEERING & INSPECTION COMPANY, INC. (PEICO) LOCATED IN | | PLANTATION, FLORIDA | | | | The following text is a portion of a facsimile received from the Florida | | Bureau of Radiation Control about the theft of a Troxler Soil/Moisture | | Density Gauge, Model #3440, Serial #13201, Isotope(s): Cs-137 (8.0 mCi); | | Am-241:Be (40 mCi): | | | | "Licensee: Professional Engineering & Inspection Company, Inc. (PEICO) | | | | "Incident Location: 1385 S.W. 19th St., Miami, Florida 33145 | | | | "Incident Description: Licensee reported that a gauge was stolen from a | | technician's home at approximately 6:30 am.. The technician had come to work | | and noted that his first job was later in the morning, so he returned home | | for breakfast. When he came out of his home he noticed that the container, | | gauge and the securing cable and lock were missing. The keys were not | | stolen. The Miami Police Department and the Florida Bureau of Radiation | | Control are investigating. | | | | "Miami PD case #173-1159Z | | | | "Office: Environmental Radiation Control | | | | "Date: Time Investigated: 21-June-00; 0930" | | | | Call the NRC operations officer for contact information. | | | | * * * UPDATE ON 6/23/00 @ 1323 BY EAKINS TO GOULD * * * | | | | The gauge was found in the early morning on 6/23/00 outside of a locked gate | | to a salvage yard. The gauge appeared to be intact and the licensee has it | | in possession and will conduct a leak test. | | | | Notified Reg 2 RDO(Barnhard) and NMSS EO(Ramsey) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37109 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: US AIR FORCE |NOTIFICATION DATE: 06/23/2000| |LICENSEE: US AIR FORCE |NOTIFICATION TIME: 12:54[EDT]| | CITY: BARKSDALE AFB REGION: 4 |EVENT DATE: 06/23/2000| | COUNTY: STATE: LA |EVENT TIME: 11:00[CDT]| |LICENSE#: 422353901-AF AGREEMENT: Y |LAST UPDATE DATE: 06/23/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOE TAPIA R4 | | |KEVIN RAMSEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WROBEL | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE US AIR FORCE REPORTED 18 LOST/STOLEN LENSATIC COMPASSES. | | | | | | In March, 2000 the Air Force recalled all lensatic compasses NSN | | 6605-00-151-5337 and Barksdale AF Base, La. inadvertently sent 17 of these | | compasses to the Defense Reutilization Management Organization (DRMO) in | | Texarkanna,Tx. DRMO has no record of receiving these 17 compasses from | | Barksdale AFB. Since this time, Barksdale base supply had collected 3 more | | of these compasses and as of 6/3/00 one has been identified as being | | missing. Each of these 18 missing compasses contain 120 millicuries or less | | of tritium. Barksdale base supply is conducting an intense search for these | | compasses. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37110 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 06/23/2000| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 19:33[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 06/23/2000| +------------------------------------------------+EVENT TIME: 16:17[CDT]| | NRC NOTIFIED BY: HAUNER |LAST UPDATE DATE: 06/23/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM FROM 100% POWER DUE TO TURBINE TRIP. | | | | During normal reactor operation at 100% power a turbine trip occurred | | causing a reactor SCRAM. A reactor recirc pump trip initiated and | | functioned normally. Four SRVs and both bypass valves opened to initially | | control reactor pressure. No. 1 bypass valve remained open for subsequent | | pressure control. The reactor vessel level transient (164 to 198 inches) | | resulted in a low level (170 inches) Group 2, 3, and 4 isolations. | | | | Subsequent to the reactor SCRAM, a Reactor Feed Pump and HPCI turbine high | | level trip occurred (HPCI was not running at this time) at 211 inches. | | Operator took action to restore reactor vessel level and restart the 'B' | | reactor feed pump. | | | | The exact cause of the turbine trip is unknown at this time. An | | intermittent 125 VDC Div 1 ground occurred following the SCRAM which is also | | under investigation. | | | | A reactor recirc pump could not be restarted due to a high temperature | | difference and a normal cooldown was initiated to mitigate concerns of | | thermal stratification. | | | | All rods fully inserted and the condenser is being used as the heat sink. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37111 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 06/23/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 20:54[EDT]| | RXTYPE: [1] GE-2 |EVENT DATE: 06/23/2000| +------------------------------------------------+EVENT TIME: 01:00[EDT]| | NRC NOTIFIED BY: BROWN |LAST UPDATE DATE: 06/23/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CURTIS COWGILL R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE NATIONAL MARINE FISHERY SERVICE OF A TRAPPED | | LOGGERHEAD SEA TURTLE. | | | | THE LICENSEE FOUND A LIVE LOGGERHEAD SEA TURTLE AT THE DILUTION STRUCTURE | | INTAKE TRASH BARS, REMOVED AND TRANSPORTED IT TO THE MARINE MAMMAL STRANDING | | CENTER. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37112 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 06/25/2000| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 20:27[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/25/2000| +------------------------------------------------+EVENT TIME: 17:45[CDT]| | NRC NOTIFIED BY: BURKETT |LAST UPDATE DATE: 06/25/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL JORDAN R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT MADE NOTIFICATION TO THE NATIONAL RESPONSE CENTER AND THE ILLINOIS | | EMERGENCY MANAGEMENT AGENCY OF AN OIL SPILL. | | | | These notifications were made due to a small quantity of oil in the runoff | | ditch. The quantity of oil is estimated to be 5 gallons and was due to an | | overflow of their lube oil separator. Cleanup efforts are in progress. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37113 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 06/26/2000| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 01:28[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 06/25/2000| +------------------------------------------------+EVENT TIME: 23:53[CDT]| | NRC NOTIFIED BY: DAVID HANKS |LAST UPDATE DATE: 06/26/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOE TAPIA R4 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF POWER TO AT LEAST 13 OF 43 EVACUATION PUBLIC NOTIFICATION SYSTEM | | SIRENS FOR APPROXIMATELY 20 MINUTES FOLLOWED BY SIRENS FALSELY IN ALARM FOR | | ABOUT 4 MINUTES | | | | Tensas Perish in Louisiana reported a loss of power to evacuation public | | notification system sirens. At least 13 of 43 sirens lost power for | | approximately 20 minutes, and upon restoration, the sirens were in alarm for | | approximately 4 minutes. Local public address station KNOE was notified of | | the false alarm by Tensas Perish. The system has been restored to normal. | | All systems functioned as required once power was restored. | | | | The licensee made applicable local and media notifications and plans to | | notify the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021