Event Notification Report for June 23, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/22/2000 - 06/23/2000 ** EVENT NUMBERS ** 37031 37095 37102 37103 37104 37105 37106 37107 37108 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37031 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 05/25/2000| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 09:21[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/25/2000| +------------------------------------------------+EVENT TIME: 08:32[EDT]| | NRC NOTIFIED BY: KEVIN PHILLIPS |LAST UPDATE DATE: 06/22/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK LESSER R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUXILIARY BUILDING FILTERED EXHAUST MAY NOT HAVE BEEN ABLE TO PERFORM ITS | | DESIGN FUNCTION | | | | The licensee discovered both doors on the vestibule to the '1A' Centrifugal | | Charging Pump Room not fully closed, this may have prevented the Auxiliary | | Building filtered exhaust system from maintaining a negative pressure in | | that room. This would render both trains of Auxiliary Building exhaust | | inoperable per Technical Specifications 3.7.12 and would require entry into | | Technical Specification 3.0.3. The doors were closed on discovery which | | returned the unit to compliance with Technical Specifications. | | | | The licensee will followup with an investigation into when and how the doors | | came to be open. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE ON 6/22/00 @ 1610 BY BURGESS TO GOULD * * * RETRACTION | | | | After further engineering evaluation, it has been determined that the plant | | was not outside the design basis during this event. Therefore, this | | notification is being retracted. | | | | The NRC Resident Inspector will be notified by the licensee. | | | | The Reg 2 RDO (Landis) was informed by the NRC Operations Officer. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37095 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 06/19/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 16:22[EDT]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 06/19/2000| +------------------------------------------------+EVENT TIME: 15:25[EDT]| | NRC NOTIFIED BY: CRAIG GILLIG |LAST UPDATE DATE: 06/22/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SHUTDOWN REQUIRED BY TECH SPEC 3.0.3 DUE TO FAILED VALVE TESTING | | | | The licensee was conducting Instrument and Control testing under DB-MI-03211 | | which failed to produce the expected response for solenoid SP6A2 on valve | | SP6A, Steam Generator Main Feedwater Valve. The problem is with the | | solenoid or associated limit switch. Due to a lack of specific Technical | | Specification guidance, 3.0.3 has been entered which requires the plant to | | initiate action to place the plant in a mode in which the specification does | | not apply. It is expected that the plant will be able to repair and test | | prior to a full plant shutdown. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1710 EST ON 6/19/00 BY CRAIG GILLIG TO FANGIE JONES * * * | | | | The licensee determined the problem was with the limit switch, has exited | | the tech spec required shutdown, and is returning to full power from 96%. | | | | The licensee intends to notify the NRC Resident Inspector. The R3DO (Roger | | Lanksbury) has been notified. | | | | * * * UPDATE ON 6/22/00 @ 1334 BY WOLF TO GOULD * * * RETRACTION | | | | The suspect limit switch for solenoid valve SVSP6A2 has been adjusted and | | satisfactorily tested via Surveillance Test DB-MI-03211. This testing | | confirmed that the problem was only with the limit switch. The solenoid | | valve and associated Steam Generator Main Feedwater Control Valve SPGA | | remained operable during this event. Therefore, the plant was not in the | | Action Statement for Technical Specification 3.0.3, and no plant shutdown | | was required. Therefore, the licensee desires to retract this event. | | | | The NRC Resident Inspector has been notified of the retraction by the | | licensee. | | | | The Reg 3 RDO (Lanksbury) was informed by the NRC Operations Officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37102 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 06/22/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 09:57[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 06/22/2000| +------------------------------------------------+EVENT TIME: 07:28[CDT]| | NRC NOTIFIED BY: JOHN WASHKO |LAST UPDATE DATE: 06/22/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 98 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUTO REACTOR SCRAM FROM 98% POWER CAUSED BY LOSS OF REACTOR FEEDWATER PUMP | | - | | | | At 0728 CDT on 06/22/00, LaSalle Unit 2 experienced an automatic reactor | | scram from 98% power due to low reactor vessel water level (+12.5 inches, | | Level 3). Normal reactor vessel water level is +36 inches. The low reactor | | vessel water level was caused by a loss of the #2A turbine driven reactor | | feedwater pump for unknown reasons. The lowest reactor vessel water level | | reached was -23 inches on the wide range recorders. All control rods | | inserted completely. Steam is being dumped to the main condenser. No | | emergency core cooling system actuations occurred or were required during | | the transient. All systems operated as designed with the exception of the | | Unit 2 station air compressor, which went into a surge condition. The air | | compressor has been secured and the Unit 0 station air compressor was | | started to pick up the additional load. Unit 2 is stable in Condition 3 | | (Hot Shutdown) with reactor vessel water level and pressure being maintained | | in their normal bands. The licensee is investigating the cause of the #2A | | reactor feedwater pump loss. | | | | This event had no effect on Unit 1 which is at 100% power. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37103 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OHIO BUREAU OF RADIATION PROTECTION |NOTIFICATION DATE: 06/22/2000| |LICENSEE: DAVID V. LEWIN CORPORATION |NOTIFICATION TIME: 11:18[EDT]| | CITY: TWINSBURG REGION: 3 |EVENT DATE: 06/21/2000| | COUNTY: STATE: OH |EVENT TIME: 10:00[EDT]| |LICENSE#: 31-210180022 AGREEMENT: Y |LAST UPDATE DATE: 06/22/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROGER LANKSBURY R3 | | |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MIKE SNEE | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - DAMAGED CPN PORTABLE MOISTURE DENSITY GAUGE | | | | At 1000 on 06/21/00, a CPN portable moisture density gauge belonging to | | David V. Lewin Corporation, Cleveland, OH, was damaged at a construction | | site at State Route 91 a mile north of Twinsburg, OH. The gauge had been | | struck by a backhoe while the Cs-137 source was extended from the gauge. | | The gauge is a CPN model MC3 containing a 10 mCi Cs-137 source and a 50 mCi | | Am-241 source. The gauge was damaged in a way that prevented the Cs-137 | | source from being secured in the safe position. The licensee contacted CTS, | | license #03225230000, a licensed gauge repair facility for advice. Ohio | | Department of Health inspectors were dispatched to the site to monitor the | | recovery. | | | | CTS recommended that the guide tube be cut which would allow the Cs-137 | | source to be retracted into the safe position. The guide tube was cut and | | the source was secured in the safe position. The source was not damaged and | | no contamination was detected. Dose rates with the source extended were 350 | | mrem/hr. | | | | The gauge was taken back to the David V. Lewin Corporation and will be | | shipped to CTS for evaluation and possible repair. The licensee will issue | | a report to the Ohio Department of Health within 30 days. | | | | Ohio Report #00-019. | | | | Mike Snee notified NRC Region 3 Jim Lynch. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37104 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GEORGE WASHINGTON UNIV. HOSPITAL |NOTIFICATION DATE: 06/22/2000| |LICENSEE: GEORGE WASHINGTON UNIV. HOSPITAL |NOTIFICATION TIME: 16:51[EDT]| | CITY: WASHINGTON REGION: 1 |EVENT DATE: 06/14/2000| | COUNTY: STATE: DC |EVENT TIME: 14:30[EDT]| |LICENSE#: 08-00216-22 AGREEMENT: N |LAST UPDATE DATE: 06/22/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROBERT SUMMERS R1 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: JOHNSON | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | GEORGE WASHINGTON UNIVERSITY HOSPITAL REPORTED AN UNDERTREATMENT DURING | | BRACHYTHERAPY. | | | | THE HOSPITAL REPORTED THAT A FEMALE PATIENT WAS BEING TREATED WITH CESIUM | | 137 SEEDS IN THE FIRST OF A TWO PHASE TREATMENT SEQUENCE WITH EACH | | DELIVERING APPROXIMATELY 1,680 RADS. DURING THIS TREATMENT THE DEVICE THAT | | CONTAINED THE SEEDS SLIPPED OUT OF THE AREA BEING TREATED. IT IS NOT KNOWN | | WHEN THIS ACTUALLY OCCURRED, BUT THE UNDERTREATMENT COULD HAVE LASTED | | BETWEEN 3.25 - 6 HOURS. THEY ARE ESTIMATING THAT THE PATIENT MAY HAVE ONLY | | RECEIVED 1,478.5 RADS. A CORRECTION FOR THIS UNDERTREATMENT CAN BE DONE | | DURING THE SECOND PHASE. THERE ALSO MAY HAVE BEEN OTHER AREAS NOT DESTINED | | FOR TREATMENT THAT WERE EXPOSED TO THE RADIATION WHEN THE DEVICE SLIPPED. | | THE PATIENT HAS BEEN REEXAMINED A WEEK FOLLOWING THIS MISADMINISTRATION AND | | NO ADVERSE AFFECTS WERE DETERMINED. A SECOND FOLLOWUP EXAMINATION WILL BE | | DONE WITHIN A WEEK. THE PATIENT WAS INFORMED AND THE ATTENDING PHYSICIAN | | WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37105 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 06/22/2000| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 17:26[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 06/22/2000| +------------------------------------------------+EVENT TIME: 15:13[CDT]| | NRC NOTIFIED BY: GILMORE |LAST UPDATE DATE: 06/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOE TAPIA R4 | |10 CFR SECTION: |FRANK CONGEL IRO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE ISSUED THE FOLLOWING PRESS RELEASE REGARDING A FIRE IN A PLANT | | SUPPORT BUILDING: | | | | "BURLINGTON, KS - A small, localized fire occurred early this afternoon at | | Wolf Creek Generating Station. The fire was contained in the welding area of | | a support building about 150 yards from where electricity is generated. The | | fire appears to have originated from an equipment malfunction. | | | | No injuries were reported. | | | | The plant's fire brigade responded and with assistance from the Coffey | | County Fire Department, quickly extinguished the fire. The fire was | | extinguished at about 1:41 p.m. | | | | The equipment, a plasma-arc cutter, is used to cut metal such as stainless | | steel. Workers were cutting one and one-half inch stainless when the fire | | started. | | | | Wolf Creek Nuclear Operating Corporation operates Wolf Creek Generating | | Station near Burlington, Kan. | | Wolf Creek is owned by Kansas City Power & Light Company; KGE, a Western | | Resources Company; and | | Kansas Electric Power Cooperative, inc. The plant is in Coffey County, | | Kansas, about four miles northeast of | | Burlington. The plant is 55 miles south of Topeka, 90 miles southwest of | | Kansas City, and 120 miles northeast | | of Wichita." | | | | The fire lasted for approximately 20 minutes (1321-1341 CDT) and the only | | damage was to the piece of equipment. | | | | The NRC Resident Inspector was notified by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37106 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/22/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:43[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/22/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 11:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/22/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |ROGER LANKSBURY R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HALCOMB | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | At 1100 hours on 06/22/00, it was determined by the Plant Shift | | Superintendent, Engineering, and Nuclear Regulatory Affairs that Criticality | | Accident Alarm System Technical Safety Requirement (TSR) required actions | | were not entered as required. The concern was whether a TSR Limiting | | Condition for Operation (LCO) should be entered prior to performing Safety | | Analysis Review required horns and light testing. | | | | All previous testing has correctly been accomplished under site operability | | procedures, even though no LCO actions were initiated due to taking credit | | for the nitrogen system. The issue was raised due to the fact that when the | | cascade strombos horns are sounding, the nitrogen horns could not be heard | | to meet required LCO requirements. Currently, all plant site Criticality | | Accident Alarm Systems are fully operable. | | | | This condition is reportable to the NRC per 10CFR76.120(c) "Safety Equipment | | Failure/Actuation". The equipment is required by a TSR to be available and | | operable and no redundant equipment is available and operable to perform the | | required safety function. | | | | The DOE Site Representative and NRC Resident Inspector were notified by the | | licensee.. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37107 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 06/22/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 18:07[EDT]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 06/22/2000| +------------------------------------------------+EVENT TIME: 14:07[CDT]| | NRC NOTIFIED BY: BORING |LAST UPDATE DATE: 06/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT ENTERED A 14 DAY LCO ACTION STATEMENT DUE TO HIGH PRESSURE COOLANT | | INJECTION (HPCI) SYSTEM BEING DECLARED INOPERABLE. | | | | During routine surveillance testing of the Containment Cooling Water System, | | required system flow through the HPCI Room Cooler could not be obtained due | | to leakage past 2-3999-252 check valve. | | | | With the HPCI Room Cooler inoperable, the HPCI System was declared | | INOPERABLE, a 14 day LCO Action Statement was entered, and an action request | | for repair of the 2-3999-252 valve was submitted. | | | | The NRC Resident Inspector was notified by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37108 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 06/22/2000| | UNIT: [] [2] [3] STATE: CA |NOTIFICATION TIME: 21:40[EDT]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 06/22/2000| +------------------------------------------------+EVENT TIME: 16:16[PDT]| | NRC NOTIFIED BY: WILLIAMS |LAST UPDATE DATE: 06/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOE TAPIA R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AT 1616 PDT ON 06/22/00, THE LICENSEE NOTIFIED THE CALIFORNIA OFFICE OF | | EMERGENCY SERVICES AND THE SAN DIEGO DEPARTMENT OF ENVIRONMENTAL HEALTH OF A | | SODIUM HYPOCHLORIDE LEAK. | | | | At 0830 PDT on 06/22/00, a 3 to 5 gpm leak occurred from the Unit 2 sodium | | hypochloride storage tank. As a precaution, the licensee evacuated | | nonessential personnel from the area of the leak. The spilled liquid was | | fully contained by a berm around the tank. This event did not pose a threat | | to the nuclear power plant or hamper site personnel in the performance of | | duties necessary for safe plant operation. Even though there was no threat | | to control room personnel and plant conditions did not require it, at 1005 | | PDT, operators manually initiated Toxic Gas Isolation Signal (TGIS) as a | | precautionary measure in response to changing wind direction. (TGIS is | | designed to terminate the supply of outside air to the control room and | | initiate operation of the control room emergency HVAC system to minimize | | operator exposure.) All system components operated as expected. | | | | The event was terminated at approximately 1145 PDT. There were no | | injuries. | | | | The NRC Resident Inspector will be informed by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021