Event Notification Report for June 22, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/21/2000 - 06/22/2000 ** EVENT NUMBERS ** 37051 37060 37098 37099 37100 37101 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37051 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 06/02/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 19:24[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 06/02/2000| +------------------------------------------------+EVENT TIME: 17:21[EDT]| | NRC NOTIFIED BY: TOM CHWALEK |LAST UPDATE DATE: 06/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING SYSTEM INOPERABLE DUE TO A FAULTY LEVEL | | SWITCH - | | | | At 1721 on 06/02/00, Nine Mile Point Unit 2 received a Reactor Core | | Isolation Cooling (RCIC) System high point vent low level annunciator alarm. | | This alarm came in and cleared repeatedly. The licensee declared the RCIC | | System inoperable but functional and entered Technical Specification 3.7.4 | | which requires the RCIC System to be restored to operable status within 14 | | days. The licensee closed the RCIC System turbine trip throttle valve, | | #2ICS*MOV150 in accordance with the annunciator response procedure. The | | licensee then performed the RCIC System fill and vent procedure | | #N2-OSP-ICS-M001 satisfactorily with a solid stream of water being vented | | and no evidence of air in the system. The high point vent low level | | annunciator alarm remained in solid following the fill and vent procedure. | | The licensee suspects that a faulty high point vent level switch is the | | problem and prepared a Problem Identification to repair the switch. The | | licensee has returned the RCIC System to available status (but still | | inoperable) and is reviewing compensatory actions for the faulty level | | switch to support the return of the RCIC System to operable status. | | | | This event has no effect on Unit 1 which is at 100% power. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | * * * RETRACTED AT 1446 EDT ON 6/21/00 BY MATT WALDECKER TO FANGIE JONES * * | | * | | | | "On June 2, 2000 at 1721 hours, the reactor core isolation cooling system | | was declared inoperable when a high point vent level low annunciator alarmed | | and cleared repeatedly. The reactor core isolation cooling trip throttle | | valve was closed in accordance with the annunciator response procedure. | | | | "Subsequent review has determined that the high point vent level low | | annunciator alarming and clearing repeatedly was due to a failed level | | switch. Correct high point vent water level was verified utilizing an | | approved operating procedure. 50.72(b)(2)(iii) and 50.73(a)(2)(v) reporting | | criteria covers an event or condition where structures, components, or | | trains of a safety system could have failed to perform their safety function | | because of equipment failures. The failure of the high point level switch | | does not constitute an event or condition which rendered the Reactor Core | | Isolation Cooling System incapable of performing its safety function. In | | addition, the level switch is only used to warn the operators of decreasing | | water inventory in the reactor core isolation cooling discharge line. No | | credit is taken for the level switch in any safety analyses and does not | | directly control the removal of residual heat (the safety function) from the | | Reactor Vessel. Therefore, this event is not reportable. | | | | "The operator action to close the reactor core isolation cooling trip | | throttle valve in accordance with the annunciator response procedure does | | not constitute an event or condition as discussed in the NUREG-1022. | | Therefore, notification of this event is being retracted." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Robert Summers) | | was notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37060 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 06/06/2000| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 06:02[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 06/06/2000| +------------------------------------------------+EVENT TIME: 02:36[CDT]| | NRC NOTIFIED BY: JOHN VAN SICKEL |LAST UPDATE DATE: 06/21/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |JOHN JACOBSON R3 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECONDARY CONTAINMENT DECLARED INOPERABLE DUE TO LOSS OF WATER SEAL CAUSED | | BY PIPE CORROSION | | | | "A 4 inch diameter floor drain outlet pipe inside the Standby Gas Treatment | | Sump was identified by Operating personnel to be corroded through near the | | wall of the sump. This piping is designed to act as a Secondary Containment | | boundary which is used to form a loop seal between the Reactor Building and | | the SBGT room. Normally, the piping would come out from the wall and make a | | 90 degree turn to near the bottom of the sump, and open under water. | | However, with the erosion occurring near the wall of the sump, a breech of | | secondary containment exists. Due to the amount of corrosion, the opening | | was estimated to be 12.57 square inches. Additionally, damaged seals on two | | other doors (#225 and #128) located on airlocks associated with Secondary | | Containment accounted for another 7 square inches, for a total of 19.57 | | square inches. Openings in excess of 12.7 square inches in this | | configuration have not been tested/evaluated. Therefore, Secondary | | Containment was considered inoperable. Operations entered Technical | | Specification LCO 3.6.4.1, condition A, for Secondary Containment inoperable | | in Mode 1 at 0236[CDT]. Required action A.1 is to restore Secondary | | Containment to operable status in 4 hours. | | | | "Operations took actions to prohibit access through the two seal damaged | | doors/airlocks by posting them to prevent access. Once administrative | | control of the doors was established, the known opening in secondary | | containment was reduced to the corroded pipe in the SBGT sump, or 12.57 | | square inches. This is less than the 12.7 square inches allowed. Technical | | Specification LCO 3.6.4.1, condition A, was exited at 0258[CDT]." | | The licensee informed the NRC Resident Inspector. | | | | * * * UPDATE AT 0903 ON 06/21/00 BY BOB NURRELL TO JOLLIFFE * * * | | | | Upon further engineering review, the licensee has determined that during | | this event, secondary containment was operable based on the actual measured | | opening size (2.25 square inches). Therefore, since secondary containment | | was not inoperable, this event is not reportable under the specified | | criterion and no other criteria apply and thus, the licensee desires to | | retract this event. The licensee notified the NRC Resident Inspector. | | The NRC Operations Officer notified the R3DO Roger Lanksbury. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37098 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ROBINSON REGION: 2 |NOTIFICATION DATE: 06/21/2000| | UNIT: [2] [] [] STATE: SC |NOTIFICATION TIME: 05:08[EDT]| | RXTYPE: [2] W-3-LP |EVENT DATE: 06/21/2000| +------------------------------------------------+EVENT TIME: 02:57[EDT]| | NRC NOTIFIED BY: AL GARROU |LAST UPDATE DATE: 06/21/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KERRY LANDIS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 M/R Y 68 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - MANUAL REACTOR TRIP FROM 68% POWER DUE TO UNISOLABLE EHC SYSTEM OIL LEAK | | - | | | | At 0257 on 06/21/00, control room operators manually tripped the plant from | | 68% power due to an unisolable electrohydraulic control (EHC) system oil | | leak which caused main turbine control valve oscillations. Two control rod | | bottom lights, shutdown bank 'A' and control bank 'C' did not illuminate; | | however, the control rod position indications showed that all control rods | | were fully inserted into the core. The auxiliary feedwater system | | actuated, as expected. Steam is being dumped to the main condenser. The | | plant is stable in Mode 3 (Hot Standby). | | | | The licensee is repairing the oil leak and investigating the problem with | | the control rod bottom lights. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37099 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NC DIVISION OF RADIATION PROTECTION |NOTIFICATION DATE: 06/21/2000| |LICENSEE: APA CONSTRUCTION COMPANY |NOTIFICATION TIME: 10:28[EDT]| | CITY: SILER CITY REGION: 2 |EVENT DATE: 06/20/2000| | COUNTY: STATE: NC |EVENT TIME: 15:10[EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 06/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KERRY LANDIS R2 | | |BOB AYRES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: LEE COX, NC DRP | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - TROXLER MOISTURE DENSITY GAUGE RUN OVER BY A TRUCK - | | | | A truck owned by APA Construction Company backed over a Troxler Moisture | | Density Gauge, Model #4640, Serial #1717, at State Road 1554, Siler City, | | NC. The gauge sources, 8 millicuries Cs-137 and 40 millicuries Am-241-Be, | | were not damaged and are in their shielded position. The gauge appeared to | | be functioning properly. The licensee plans to send the gauge to Troxler | | for inspection/repair. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37100 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: DNX TRANSGENIC SCIENCES |NOTIFICATION DATE: 06/21/2000| |LICENSEE: DNX TRANSGENIC SCIENCES |NOTIFICATION TIME: 10:35[EDT]| | CITY: CRANBURY REGION: 1 |EVENT DATE: 06/07/2000| | COUNTY: STATE: NJ |EVENT TIME: 11:00[EDT]| |LICENSE#: 29-30350-01 AGREEMENT: N |LAST UPDATE DATE: 06/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROBERT SUMMERS R1 | | |BOB AYRES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE D'IPPOLITO, RSO | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - LOSS OF LICENSED MATERIAL - | | | | On 06/02/00, one vial of 500 �Ci of [alpha-32] deoxycytidine 5'-Triphosphate | | (dCTP) was received at DNX Transgenic Sciences, Cranbury, NJ. The | | concentration of the material was 10 �Ci/�l. Upon arrival, this vial was | | designated as vial #153. At 1130 on 06/07/00, Roland Felkner, a DNX | | Transgenic Sciences research associate, was planning to remove 50 �Ci of | | material from this vial to do a DNA labeling experiment. However, he | | discovered that there was no material in the vial. According to the isotope | | inventory log of vial #153, there should have been 150 �Ci of the 500 �Ci | | still available in the vial. Upon investigation, it was determined that 200 | | �Ci, rather than 150 �Ci, was actually missing. This error is attributed to | | a computational mistake made in the log by another research associate. | | | | Joe D'Ippolito, DNX Transgenic Sciences Radiation Safety Officer (RSO), | | interviewed lab personnel, conducted a survey of the lab area and performed | | an internal investigation to locate the missing material. There was no | | indication of radiation exposure to lab personnel. Based on the results of | | the investigation, the RSO and members of the DNX Transgenic Sciences | | Radiation Safety Committee believe that less material had been sent in vial | | #153 by their supplier, NEN Life Science Product, than was reported on the | | vial label. | | | | The RSO is continuing his investigation and will determine corrective | | actions. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37101 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 06/21/2000| |LICENSEE: PROFESSIONAL ENGINEERING & INSPECTION|NOTIFICATION TIME: 11:01[EDT]| | CITY: PLANTATION REGION: 2 |EVENT DATE: 06/21/2000| | COUNTY: STATE: FL |EVENT TIME: 06:30[EDT]| |LICENSE#: 2113-1 AGREEMENT: Y |LAST UPDATE DATE: 06/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KERRY LANDIS R2 | | |BOB AYRES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLEY ADAMS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING A STOLEN TROXLER GAUGE OWNED BY | | PROFESSIONAL ENGINEERING & INSPECTION COMPANY, INC. (PEICO) LOCATED IN | | PLANTATION, FLORIDA | | | | The following text is a portion of a facsimile received from the Florida | | Bureau of Radiation Control about the theft of a Troxler Soil/Moisture | | Density Gauge, Model #3440, Serial #13201, Isotope(s): Cs-137 (8.0 mCi); | | Am-241:Be (40 mCi): | | | | "Licensee: Professional Engineering & Inspection Company, Inc. (PEICO) | | | | "Incident Location: 1385 S.W. 19th St., Miami, Florida 33145 | | | | "Incident Description: Licensee reported that a gauge was stolen from a | | technician's home at approximately 6:30 am.. The technician had come to work | | and noted that his first job was later in the morning, so he returned home | | for breakfast. When he came out of his home he noticed that the container, | | gauge and the securing cable and lock were missing. The keys were not | | stolen. The Miami Police Department and the Florida Bureau of Radiation | | Control are investigating. | | | | "Miami PD case #173-1159Z | | | | "Office: Environmental Radiation Control | | | | "Date: Time Investigated: 21-June-00; 0930" | | | | Call the NRC operations officer for contact information. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021