Event Notification Report for June 7, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/06/2000 - 06/07/2000 ** EVENT NUMBERS ** 37002 37060 37061 37062 37063 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37002 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WNP-2 REGION: 4 |NOTIFICATION DATE: 05/15/2000| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 11:47[EDT]| | RXTYPE: [2] GE-5 |EVENT DATE: 05/15/2000| +------------------------------------------------+EVENT TIME: 04:48[PDT]| | NRC NOTIFIED BY: J.W. GASTON |LAST UPDATE DATE: 06/06/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BILL JONES R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 62 Power Operation |62 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OUTBOARD MAIN STEAM ISOLATION (MSIV) VALVE FOUND CLOSED. | | | | At 0448 PDT on 05/15/00, the outboard main steam isolation valve # | | MSIV-V-28A was found in the closed position (green indicating light on). | | Follow-up verification of the 'A' main steam line flow (0%) and the plant | | computer valve position verified that the valve was closed. The plant | | computer indicated that the valve closed at 0254 PDT and it was discovered | | closed at 0448 PDT. No work was being performed on the main steam system or | | in the area of the main steam system when the valve closed. The plant | | computer indicated that the valve had fast closed. The plant entered the | | Limiting Condition of Operation for Primary Containment Isolation Valve and | | placed the control switch for the MSIV in the closed position. There was no | | valid ESF Actuation signal that caused the valve closure. The plant was | | operating at 62% power and did not experience a transient as a result of the | | MSIV closure (no flux tilt). Licensee investigation into the cause of the | | closure is continuing. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE ON 6/6/00 @ 1155 BY MCBRIDE TO GOULD * * * RETRACTION | | | | The event notification report associated with the above event is hereby | | retracted. The event and conditions associated with the event do not meet | | NUREG 1022, Rev. 1, reporting criteria. Only a single component, MSIV-V-28A, | | actuated (closed). The single component (MSIV) is not sufficient to mitigate | | the consequences of single events. There was not a manual or automatic ESE | | system actuation. An ESF signal (valid or invalid) was not generated. | | Therefore, in accordance with the statements of considerations for NUREG | | 1022, Rev. 1,( 10CFR50.72(b)(2)(ii), there was not a sufficient number of | | channels (zero) in a multichannel ESF actuation system to meet the | | definition of actuation of enough channels to complete the minimum actuation | | logic for a train or the system. For these reasons, this event does not meet | | the reporting criteria of 10CFR50.72(b)(2)(ii) and is hereby retracted. | | | | The NRC Resident Inspector was notified. The Reg 4 RDO (Pellet) was | | notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37060 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 06/06/2000| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 06:02[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 06/06/2000| +------------------------------------------------+EVENT TIME: 02:36[CDT]| | NRC NOTIFIED BY: JOHN VAN SICKEL |LAST UPDATE DATE: 06/06/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |JOHN JACOBSON R3 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECONDARY CONTAINMENT DECLARED INOPERABLE DUE TO LOSS OF WATER SEAL CAUSED | | BY PIPE CORROSION | | | | "A 4 inch diameter floor drain outlet pipe inside the Standby Gas Treatment | | Sump was identified by Operating personnel to be corroded through near the | | wall of the sump. This piping is designed to act as a Secondary Containment | | boundary which is used to form a loop seal between the Reactor Building and | | the SBGT room. Normally, the piping would come out from the wall and make a | | 90 degree turn to near the bottom of the sump, and open under water. | | However, with the erosion occurring near the wall of the sump, a breech of | | secondary containment exists. Due to the amount of corrosion, the opening | | was estimated to be 12.57 square inches. Additionally, damaged seals on two | | other doors (#225 and #128) located on airlocks associated with Secondary | | Containment accounted for another 7 square inches, for a total of 19.57 | | square inches. Openings in excess of 12.7 square inches in this | | configuration have not been tested/evaluated. Therefore, Secondary | | Containment was considered inoperable. Operations entered Technical | | Specification LCO 3.6.4.1, condition A, for Secondary Containment inoperable | | in Mode 1 at 0236[CDT]. Required action A.1 is to restore Secondary | | Containment to operable status in 4 hours. | | | | "Operations took actions to prohibit access through the two seal damaged | | doors/airlocks by posting them to prevent access. Once administrative | | control of the doors was established, the known opening in secondary | | containment was reduced to the corroded pipe in the SBGT sump, or 12.57 | | square inches. This is less than the 12.7 square inches allowed. Technical | | Specification LCO 3.6.4.1, condition A, was exited at 0258[CDT]." | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37061 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 06/06/2000| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 12:47[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 06/06/2000| +------------------------------------------------+EVENT TIME: 10:20[EDT]| | NRC NOTIFIED BY: DENNIS MAY |LAST UPDATE DATE: 06/06/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE | | | | After completion of HPCI pump surveillance testing, a check for freedom of | | movement and proper reset action of the overspeed trip tappet was performed. | | As a result of this check, an adjustment was found to be necessary for the | | turbine stop valve reset time. Attempts to make this adjustment resulted in | | inoperability of the reset function of the overspeed trip. HPCI was | | declared inoperable and Technical Specification limiting condition for | | operation 3.5E(3) was entered. HPCI will still start if called upon but if | | it trips on overspeed HPCI will become inoperable. | | | | Reactor Core Isolation Cooling, Emergency Diesel Generators, and all other | | Emergency Core Cooling Systems are fully operable if needed. The electrical | | grid is stabile. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37062 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SOUTH COAST MEDICAL CENTER |NOTIFICATION DATE: 06/06/2000| |LICENSEE: SOUTH COAST MEDICAL CENTER |NOTIFICATION TIME: 19:04[EDT]| | CITY: LAGUNA BEACH REGION: 4 |EVENT DATE: 06/06/2000| | COUNTY: STATE: CA |EVENT TIME: 14:30[PDT]| |LICENSE#: 0920-30 AGREEMENT: Y |LAST UPDATE DATE: 06/06/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN PELLET R4 | | |WILLIAM BRACH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOSE BRUNO | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAAA 20.1906(d) SURFACE CONT/ EXT RAD | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | WIPE TEST OF PACKAGE EXTERIOR RESULTED IN A COUNT LEVEL OF 4442 DPM | | | | A package containing technetium - 99m (NaTcO4) delivered by NYCOMED Amersham | | to South Coast Medical Center was found to have surface contamination level | | above the 22 DPM per square centimeter limit. The wipe of the outer surface | | of the package (metal canister) was placed in a well counter and the counter | | indicated the that total count on the wipe was 4442 +/-149 DPM. The outer | | dimensions of the metal canister are 15 centimeters by 25 centimeters by 29 | | centimeters. The licensee will contact NYCOMED Amersham located in Anaheim, | | CA, and ask them to pickup the package. The package was not opened. | | Activity of the technetium-99m (NaTcO4) was originally 25 millicuries and | | the quantity is 2.4838 milliliters. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37063 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 06/07/2000| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 01:32[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 06/06/2000| +------------------------------------------------+EVENT TIME: 23:10[CDT]| | NRC NOTIFIED BY: RUITER |LAST UPDATE DATE: 06/07/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 35 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD A MANUAL REACTOR TRIP FROM 35% POWER. | | | | At 2243 on 06/06/2000 an alarm for high reactor coolant pump "A" bearing | | water temperature came in on the plant process computer. At 2310 the | | reactor coolant pump "A" bearing water temperature exceeded 225�F and a | | manual reactor trip was initiated and the "A" reactor coolant pump was | | secured. Following the reactor trip all three auxiliary feed water pumps | | started and equipment response was as expected. All rods fully inserted and | | no safety relief valves lifted. Currently the turbine driven aux feed is | | secured, but the motor driven aux feed is still operating. They are | | investigating if the cause was a temperature indicating problem or a bearing | | failure. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021