Event Notification Report for June 5, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/02/2000 - 06/05/2000 ** EVENT NUMBERS ** 36964 37046 37048 37049 37050 37051 37052 37053 37054 37055 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36964 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GEOTECH ENVIRONMENTAL, INC |NOTIFICATION DATE: 05/03/2000| |LICENSEE: GEOTECH ENVIRONMENTAL, INC |NOTIFICATION TIME: 15:24[EDT]| | CITY: MAPLE SHADE REGION: 1 |EVENT DATE: 05/03/2000| | COUNTY: STATE: NJ |EVENT TIME: 08:00[EDT]| |LICENSE#: 29-28286-02 AGREEMENT: N |LAST UPDATE DATE: 06/02/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |NIEL DELLA GRECA R1 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CARL DINICOLANTONIO | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN TROXLER MOISTURE DENSITY GAUGE | | | | On April 27, 2000, a technician was involved in an automobile accident in | | Philadelphia, PA. At that time, the gauge was stored in the trunk of the | | vehicle. When police arrived on the scene, the technician was arrested. | | The technician informed the police that the gauge was in the trunk and | | showed the gauge to the police officers. After the technician was | | arrested, the vehicle was stolen. The vehicle was recovered on April 29, | | 2000. The gauge was not in the trunk when the vehicle was recovered. The | | device contained 8 mCi of Cs-137 and 40 mCi of Am-241. | | | | * * * UPDATE AT 1402 ON 06/02/00 BY CLAIRE PANICO TO JOLLIFFE * * * | | | | The stolen Troxler moisture density gauge was found in a waste management | | recycling facility in Philadelphia. The undamaged gauge has been returned | | to Geotech Environmental, Inc. | | | | George Pangburn, NRC Region 1 has been notified. NRC Region 1 issued | | PNO-I-00-013A. | | | | The NRC Operations Officer Notified R1DO Dick Barkley and NMSS EO Brian | | Smith. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37046 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 05/31/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 18:04[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 05/31/2000| +------------------------------------------------+EVENT TIME: 13:30[CDT]| | NRC NOTIFIED BY: COVEYOU |LAST UPDATE DATE: 06/02/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SHEAR R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 97 Power Operation |97 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED A 7 DAY LCO DUE TO HPCS BEING DECLARED INOPERABLE. | | | | While performing monthly surveillance start LOS-DG-M3, for the High-Pressure | | Core Spray (HPCS) systems Emergency Diesel Generator, the Diesel | | automatically tripped off on an over-speed signal. The Diesel was being | | started from an idle condition while an operator was attempting to maintain | | speed between 400 and 500 rpm. The Diesel does not appear to have been | | damaged but remains shutdown and unavailable for on-going investigation of | | the failure. The High-Pressure Core Spray system is inoperable but available | | from normal power source only. The failure mechanism is being investigated | | and corrective actions will be performed. | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATE AT 2211 ON 06/01/00 BY SHANE MARIK TO JOLLIFFE * * * | | | | | | The licensee investigation has determined that the cause of the event was | | due to operator overcompensation of the engine governor during the start | | that resulted in the EDG accelerating to the overspeed setpoint and tripping | | on overspeed. The operator performing the slow (idle) start in accordance | | with the monthly Technical | | Specification surveillance procedure was a trainee under supervision by a | | qualified operator. The EDG was already inoperable for the performance of | | the monthly surveillance test that verifies operability of the EDG to start | | and carry full load for at least 60 minutes. During inspection, no | | mechanical or electrical malfunctions were | | found associated with governor settings, the start circuitry, the engine | | fuel racks, or fuel injector linkages. The fuel rack and associated fuel | | injector linkages were then verified to have freedom of movement without | | binding. A subsequent fast start was performed (same as an automatic start) | | that verified that the EDG did not have a malfunction that would cause it to | | trip on overspeed. The EDG would have satisfied its intended safety | | function when in standby (no operator interface is required for the | | governor/fuel rack control. except for surveillance testing). Therefore, | | the overspeed trip of the High Pressure Core Spray System EDG is not | | reportable as a | | condition that alone could have prevented fulfillment of a safety function. | | | | Since the failure occurred after the EDG was inoperable due to not being | | lined up for standby operation (removed from service as part of a planned | | evolution in accordance with an approved procedure), the start was a slow | | start controlled by an operator and restoration of the EDG was less than 12 | | hours and well within the 14 day Technical Specification allowed outage | | time. The licensee has determined that this event is not reportable to the | | NRC, and desires to retract this event notification. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R3DO Bruce Jorgensen. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37048 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TRI STATE CONSULTANTS |NOTIFICATION DATE: 06/02/2000| |LICENSEE: TRI STATE CONSULTANTS |NOTIFICATION TIME: 07:26[EDT]| | CITY: FLINT REGION: 3 |EVENT DATE: 06/01/2000| | COUNTY: STATE: MI |EVENT TIME: 14:30[EDT]| |LICENSE#: 37-19640-01 AGREEMENT: N |LAST UPDATE DATE: 06/02/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE JORGENSEN R3 | | |SCOTT MOORE NMSS | +------------------------------------------------+RICHARD BARKLEY R1 | | NRC NOTIFIED BY: PAT DURKIN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |IBBF 30.50(b)(2)(ii) EQUIP DISABLED/FAILS | | |IBAE 30.50(b)(1)(iii) ACCESS DENIED OTHER | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SOURCE ASSEMBLY, CONTAINING 24 CURIES OF IRIDIUM-192, BECAME DETACHED FROM | | ITS DRIVE ASSEMBLY | | | | While checking a radiographic exposure device manufactured by AEA | | Technology, the source assembly became detached from its drive mechanism. | | The licensee was checking the swage end, the locking mechanism, of the | | exposure assemble when the assembly failed. The swage connection had a crack | | and this caused the swage connection to fail, becoming detached. The | | Assistant Radiation Safety Officer (ARSO) cleared the room and made several | | trips into the room to place lead shielding over the source assembly. After | | the source assembly was covered with lead, the ARSO took radiation surveys | | around the room to make sure radiation levels were within acceptable limits. | | The ARSO spent the night guarding the entrance to the room to prevent anyone | | from entering. AEA Technology was notified of this event on 06/01/00 and | | they are sending a retrieval team out on 06/02/00 to retrieve the source. | | The source model number is 424-9. | | | | The ARSO was the only one to be exposed and he received 78 millirems as | | indicated by his pocket dosimeter. | | | | The source, Iridium-192, was originally manufactured on 12/17/99 with a | | strength of 114.5 curies. The present strength of the Iridium-192 source is | | 24 curies (half life of Iridium-192 is 74.2 days). | | | | Tri State Consultants' main office is located in Pittsburgh, PA. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37049 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 06/02/2000| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 11:57[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 06/02/2000| +------------------------------------------------+EVENT TIME: 04:15[CDT]| | NRC NOTIFIED BY: PAT McKENNA |LAST UPDATE DATE: 06/02/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |ADEG 50.72(b)(1)(ii) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OUTSIDE CONTAINMENT ISOLATION VALVE INOPERABLE DUE TO INCOMPLETE PLANT | | MODIFICATION | | | | At 0415 CDT on 06/02/00, I&C technicians began to perform tech spec | | surveillance test #ISF-SB-OA30A to test the operability of 'A' train steam | | line isolation valve slave relay #K-634. In establishing the initial | | conditions at step 4.2 of the test procedure, solid state protection system | | white light #26 was not illuminated as required by the procedure. The | | procedure was exited at that time and the control room crew was informed of | | the finding. | | | | The control room crew replaced the light bulb and the light still did not | | illuminate. Another light bulb, known to be good, was then installed in the | | light socket. The light still did not illuminate. The Shift Supervisor | | contacted the System Engineer at approximately 0530 CDT when the engineer | | arrived onsite, and requested that the engineer investigate what the white | | light indicated when the light was not illuminated. | | | | After review of the system schematics, the engineer found that there was the | | possibility of outside containment isolation valve #EGHV-0061 being | | INOPERABLE if relay #K-802 did not function properly. (Reference electrical | | drawing #E-23EG09A.) This situation was reported to the control room crew. | | | | The Shift Supervisor declared valve #EGHV-0061 INOPERABLE using the time of | | discovery at 0415 CDT and closed the valve and deenergized power to the | | valve per Tech Spec action statement 3.6.3.A at 0800 CDT. Equipment out of | | service log entry #7986 was made. | | | | I&C technicians were dispatched to support troubleshooting efforts. After | | some initial troubleshooting, some results did not agree with the drawing. | | The engineer noted the drawing showed that the circuitry had recently been | | changed by Plant Modification #CMP 98-1020. The drawing had been updated on | | 04/07/00. | | | | The engineer called the Construction Supervisor of the plant modification | | installation. The supervisor reviewed the modification package and found a | | connection between a terminal block at the motor control center for valve | | #EGHV-0061 and the solid state protection system cabinet #SB030A had not | | been performed. This made containment isolation valve #EGHV-0061 INOPERABLE | | because it would not close on a phase B containment isolation signal. The | | control room crew was notified of this finding. This finding meant that the | | valve had been INOPERABLE since the installation of the plant modification | | on 04/06/00. | | | | The Construction Supervisor initiated field change notice #FCN-11 to plant | | modification package #MP 98-1020 and initiated work document #W657017 to | | correct the circuitry wiring. Retest documents #R657017A and #R6S70173 was | | also initiated for post maintenance testing of the circuit. | | | | The licensee determined that this event was reportable to the NRC at 1030 | | CDT. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37050 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: KANSAS DEPT OF HEALTH & ENVIRONMENT |NOTIFICATION DATE: 06/02/2000| |LICENSEE: ALLEN COUNTY HOSPITAL, IOLA, KS |NOTIFICATION TIME: 14:31[EDT]| | CITY: IOLA REGION: 4 |EVENT DATE: 06/01/2000| | COUNTY: STATE: KS |EVENT TIME: 16:00[CDT]| |LICENSE#: 19-B366-01 AGREEMENT: Y |LAST UPDATE DATE: 06/02/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GARY SANBORN R4 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TOM CONLEY | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | I-131 OVERDOSE - MEDICAL MISADMINISTRATION/AGREEMENT STATE EVENT - | | | | A female patient at Allen County Hospital, Iola, KS, was given 100 | | microcuries of I-131 for an thyroid uptake measurement during a diagnostic | | study instead of the prescribed 50 microcuries. The cause of this medical | | misadministration event was due to the hospital hot lab delivering two | | capsules of 50 microcuries each; one to be given to the patient and the | | other to be used as a standard. The patient was mistakenly given both | | capsules. This overdose poses no adverse medical effects to the patient. | | The patient's doctor has been informed. The doctor plans to inform the | | patient. The hospital is determining corrective actions. | | (KS Case #KS-00-0011). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37051 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 06/02/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 19:24[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 06/02/2000| +------------------------------------------------+EVENT TIME: 17:21[EDT]| | NRC NOTIFIED BY: TOM CHWALEK |LAST UPDATE DATE: 06/02/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING SYSTEM INOPERABLE DUE TO A FAULTY LEVEL | | SWITCH - | | | | At 1721 on 06/02/00, Nine Mile Point Unit 2 received a Reactor Core | | Isolation Cooling (RCIC) System high point vent low level annunciator alarm. | | This alarm came in and cleared repeatedly. The licensee declared the RCIC | | System inoperable but functional and entered Technical Specification 3.7.4 | | which requires the RCIC System to be restored to operable status within 14 | | days. The licensee closed the RCIC System turbine trip throttle valve, | | #2ICS*MOV150 in accordance with the annunciator response procedure. The | | licensee then performed the RCIC System fill and vent procedure | | #N2-OSP-ICS-M001 satisfactorily with a solid stream of water being vented | | and no evidence of air in the system. The high point vent low level | | annunciator alarm remained in solid following the fill and vent procedure. | | The licensee suspects that a faulty high point vent level switch is the | | problem and prepared a Problem Identification to repair the switch. The | | licensee has returned the RCIC System to available status (but still | | inoperable) and is reviewing compensatory actions for the faulty level | | switch to support the return of the RCIC System to operable status. | | | | This event has no effect on Unit 1 which is at 100% power. | | | | The licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37052 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/03/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:44[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/02/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:30[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/03/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |TONY VEGEL R3 | | DOCKET: 0707002 |TED SHERR NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICK LARSON | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC 91-01 BULLETIN REPORT INVOLVING POTENTIAL LOSS OF CRITICALITY | | CONTROL IN SHUTDOWN CELLS | | | | "On 6/2/00 the Plant Shift superintendent was notified of a potential NCSA | | noncompliance. NCSAs 326_013, NCSA 330_004, and NCSA 333_015 require that | | cells that are shutdown and at a UF6 negative be buffered with dry air or | | nitrogen to maintain moderation control as part of double contingency. For | | cells that have less than a safe mass, procedure guidance allows the cell to | | be maintained less than atmospheric pressure, when not at a UF6 negative. | | Various leaks (either from the dry air system or from wet atmospheric air) | | can enter the cell allowing pressure to increase. This pressure must then be | | evacuated to maintain the cell less than atmospheric pressure. Repeated | | cycles of 'leak up' and evacuation will eventually achieve a UF6 negative | | unknown to operators since there are no periodic sampling requirements. The | | NCS requirement to buffer a cell within eight hours of achieving a UF6 | | negative may then be violated because the state of a UF6 negative is not | | known. | | | | "Presently all cells that are shutdown that have less than a safe mass in | | them are at a UF6 negative, and there is currently no violation of this | | moderation control. However, it cannot be guaranteed that this control was | | not violated during past operations, and is being reported as a loss of one | | control. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "The safety significance of this event is low. Only affected cells that when | | shutdown have less than a safe mass of material in them. Failure to | | establish or maintain the buffer as required could result in wet air | | entering a shutdown cell. This would moderate a UO2F2 deposit due to the | | hygroscopic properties of UO2F2. If this unbuffered condition were permitted | | to continue for longer periods, the H/U of the deposit could eventually | | reach a maximum of 4 (the maximum H/U ratio of a deposit exposed to ambient | | cascade building air is 4). However, due to being less than a safe mass, a | | criticality could not occur. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | "For a criticality to occur the mass of the deposit would have to be greater | | than a safe mass, moderation level would have to reach an H/U ratio of 4, | | the deposit would have to be reflected. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | "The controlled parameters for this event are mass and moderation. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | "The highest possible enrichment for event is 20% and the material will be | | at or below a safe mass. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | "The failure in this case is the implementation of the control on | | moderation. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | [Not specified]." | | | | Department Operating Instructions (DOIs) have been issued pending procedural | | revisions to address this deficiency. The NRC Resident Inspector and DOE | | Site Representative have been informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37053 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 06/04/2000| | UNIT: [] [2] [] STATE: CT |NOTIFICATION TIME: 01:28[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 06/04/2000| +------------------------------------------------+EVENT TIME: 00:12[EDT]| | NRC NOTIFIED BY: MIKE CICCONE |LAST UPDATE DATE: 06/04/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 65 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED A REACTOR TRIP ON TURBINE TRIP DURING SURVEILLANCE | | TESTING OF THE TURBINE | | | | AT 0128 EDT ON 6/4/00 WHILE PERFORMING TURBINE SURVEILLANCE PROCEDURE 2651T, | | "POWER LOAD UNBALANCED PUSH-TO-TEST", THE TURBINE TRIPPED UNEXPECTEDLY | | CAUSING A REACTOR TRIP. ALL CONTROL RODS FULLY INSERTED. ALL SYSTEMS | | FUNCTIONED AS REQUIRED. THE MAIN FEEDWATER SYSTEM AND MAIN CONDENSER REMAIN | | IN SERVICE FOR DECAY HEAT REMOVAL . NO PRIMARY OR SECONDARY SAFETIES/PORVs | | LIFTED DURING THE TRANSIENT. ELECTRICAL LOADS TRANSFERRED TO THE RSST | | TRANSFORMER WITH ALL EDGs AVAILABLE IF NEEDED. THERE IS NO SAFETY EQUIPMENT | | OUT OF SERVICE AT THIS TIME. THE LICENSEE NOTIFIED THE NRC RESIDENT | | INSPECTOR AND BOTH STATE AND LOCAL AGENCIES. A PRESS RELEASE IS | | ANTICIPATED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37054 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 06/04/2000| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 06:42[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 06/04/2000| +------------------------------------------------+EVENT TIME: 05:54[EDT]| | NRC NOTIFIED BY: MARIE GILLMAN |LAST UPDATE DATE: 06/04/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 A/R Y 22 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 3 EXPERIENCED A REACTOR TRIP ON LOW STEAM GENERATOR WATER LEVEL | | FOLLOWING A TURBINE TRIP | | | | "[A] plant startup [was] in progress. [The] main turbine generator [was] | | tied to [the] grid at 0452 [EDT]. Power was being raised to 30% power. | | | | "At 22% reactor power while feeding steam generators via manual control of | | [the] feedwater regulatory valves, '33' Steam Generator level reached a high | | level trip point and tripped the turbine. The subsequent shrink in steam | | generator '31' levels resulted in a reactor trip at 0554 [EDT]. | | | | "All plant equipment functioned as required, no malfunctions noted at this | | time. [A] post trip review [is] in progress. ESF Actuation; '31' and '33' | | auxiliary feed pump[s] started." | | | | All rods fully inserted following the trip. There is no safety equipment | | out of service at this time. Offsite power is supplying electrical loads. | | The auxiliary feed pumps and main condenser are removing decay heat. | | | | The licensee informed the NRC Resident Inspector and plans to issue a press | | release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37055 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 06/04/2000| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 15:45[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 06/04/2000| +------------------------------------------------+EVENT TIME: 15:15[EDT]| | NRC NOTIFIED BY: RON CARPINO |LAST UPDATE DATE: 06/04/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N N 0 Startup |0 Startup | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NY STATE DEC TO BE NOTIFIED OF 5 - 15 GALLONS LUBE OIL SPILL INTO PLANT | | DISCHARGE CANAL - | | | | At 1515 on 06/04/00, the licensee notified the DOT National Response Center | | and plans to notify the NY State Department of Environmental Conservation | | (DEC), local officials, and the NRC Resident Inspector that 5 to 15 gallons | | of lube oil had overflowed from the plant oil collection system into the | | plant discharge canal which drains into the Hudson River. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021