Event Notification Report for May 25, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/24/2000 - 05/25/2000 ** EVENT NUMBERS ** 37024 37025 37026 37027 37028 37029 37030 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37024 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA DEPT OF HEALTH SERVICES |NOTIFICATION DATE: 05/24/2000| |LICENSEE: STERIGENICS INTERNATIONAL |NOTIFICATION TIME: 13:10[EDT]| | CITY: HAYWARD REGION: 4 |EVENT DATE: 05/23/2000| | COUNTY: STATE: CA |EVENT TIME: 12:29[PDT]| |LICENSE#: 6268-01 AGREEMENT: Y |LAST UPDATE DATE: 05/24/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CLAUDE JOHNSON R4 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PENDERGAST | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE RADIOLOGICAL HEALTH BRANCH OF THE CALIFORNIA DEPARTMENT OF HEALTH | | SERVICES WAS NOTIFIED BY STERIGENICS INTERNATIONAL THAT THEY HAD A CABLE JAM | | ON THEIR SOURCE HOIST ARRAY. | | | | THIS OCCURRED ON THEIR 600,000 CURIE POOL IRRADIATOR WHILE THEY WERE | | LOWERING THE SOURCE ARRAY INTO THE SHIELDED POSITION AND THE SOURCE HOIST | | CABLE JAMMED DUE TO A FRAY ON THE CABLE. THEY LOOSENED THE SHIELDING AROUND | | THE SOURCE HOIST CABLE AND THAT ALLOWED THE SOURCES TO BE RETURNED TO THE | | SAFE POSITION. THERE WERE NO OVEREXPOSURES AND NO ABNORMAL RADIATION | | LEVELS. THE PLANT WAS SHUTDOWN UNTIL MAINTENANCE WAS COMPLETED THIS MORNING | | @ 6:00. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37025 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 05/24/2000| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 14:45[EDT]| | RXTYPE: [3] CE |EVENT DATE: 05/24/2000| +------------------------------------------------+EVENT TIME: 12:50[CDT]| | NRC NOTIFIED BY: SCOTT |LAST UPDATE DATE: 05/24/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF COMPROMISE OF CLASSIFIED DOCUMENTS/SAFEGUARDS INFORMATION. | | | | IMMEDIATE COMPENSATORY MEASURES TAKEN UPON DISCOVERY. | | | | REFER HOO LOG FOR ADDITIONAL DETAILS. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37026 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 05/24/2000| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 15:48[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 05/24/2000| +------------------------------------------------+EVENT TIME: 14:08[CDT]| | NRC NOTIFIED BY: ROBBINS |LAST UPDATE DATE: 05/24/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEOFFREY WRIGHT R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF VENTILATION TO PAB BATTERY AND INVERTER ROOMS DURING AN APPENDIX R | | FIRE | | | | DURING THE FINAL REVIEW OF THE NEW APPENDIX R REBASELINE PROJECT IT WAS | | DISCOVERED THAT VENTILATION TO THE PAB BATTERY AND INVERTER ROOMS WOULD BE | | LOST FOR GREATER THAN 2 HOURS FOR AN APPENDIX R FIRE. FIRE ROUNDS IN THE | | AFFECTED AREAS HAVE BEEN STARTED AND PROCEDURE REVISIONS ARE IN PROGRESS TO | | ESTABLISH PORTABLE VENTILATION AS NEEDED. | | | | THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37027 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 05/24/2000| | UNIT: [] [] [3] STATE: AL |NOTIFICATION TIME: 15:50[EDT]| | RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 05/24/2000| +------------------------------------------------+EVENT TIME: 13:54[CDT]| | NRC NOTIFIED BY: GOLDEN |LAST UPDATE DATE: 05/24/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK LESSER R2 | |10 CFR SECTION: |JOHN HANNON NRR | |ACCS 50.72(b)(1)(iv) ECCS INJECTION |JOSEPH GIITTER IRO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 A/R Y 100 Power Operation |0 Hot Standby | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD A REACTOR SCRAM FROM 100% POWER DUE TO LOW REACTOR WATER | | LEVEL | | | | At 13:54 CDT, unit 3 reactor scrammed due to low reactor water level. All | | rods fully inserted into the core. The expected groups 2, 3, 6 and 8 | | isolations were received. Both recirc pumps tripped, all Standby Gas | | Treatment trains started and the 'A' CREV started. The expected Refuel zone | | and unit 3 reactor zone isolations were received. Both the HPCI system and | | the RCIC system automatically initiated and injected due to low level | | following the scram. The actual signal perturbation that caused the reactor | | trip on low water level is still being investigated. Currently the plant is | | in a stable condition in mode 3 with investigations in progress. No relief | | valves lifted and HPCI was secured within the first 5 minutes and RCIC | | secured a few minutes later. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37028 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WASHINGTON DEPARTMENT OF HEALTH |NOTIFICATION DATE: 05/24/2000| |LICENSEE: ANVIL CORPORATION |NOTIFICATION TIME: 18:05[EDT]| | CITY: BELLINGHAM REGION: 4 |EVENT DATE: 05/11/2000| | COUNTY: STATE: WA |EVENT TIME: 00:00[PDT]| |LICENSE#: WN-IR031-1 AGREEMENT: Y |LAST UPDATE DATE: 05/24/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CLAUDE JOHNSON R4 | | |WAYNE HODGES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: FRAZEE | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Licensee had a source disconnect occur due to a mechanical failure of the | | drive cable connector. | | | | A source disconnect attributable to mechanical failure of the drive cable | | connector occurred during use of a cobalt 60 radiographic exposure device on | | May 11. Radiography is routinely conducted by this licensee in a shielded | | vault (a permanent radiographic installation). An AEA Technologies Model 676 | | cobalt 60 camera, serial number B105, is generally left set-up between | | shots. The routine daily equipment check includes a visual check to confirm | | that the drive cable and camera are still connected. The last quarterly | | maintenance inspection was at the end of March 2000 and no problems with the | | drive cable connector were noted. However, during the first shot of the day, | | the radiographer noticed that the source did not go out smoothly and then | | failed to retract. The RSO was contacted and after several more attempts to | | retract the source the licensee decided to secure the area and call in the | | manufacturer's retrieval experts. Additional shielding, locks and posting | | were added and a survey of the area including the roof showed no readings | | above 1 mrem per hour. The state Division of Radiation Protection was | | notified and staff observed the retrieval on May 12. Once the source was | | secured, the failed equipment was inspected. No problems were noted with | | the source assembly or the camera. However, the ball fitting at the drive | | cable connector's end had become separated from the cable. AEA Technologies | | took the separated ball and 4 inches of the end of the drive cable back to | | AEA for analysis. | | | | What is the notification or reporting criteria involved? WAC 246-221-250 | | Notification of incidents (equipment failure) | | | | Activity and isotope(s) involved: 71 curies of Cobalt 60. | | | | Overexposures? There were no overexposures (however, retrieval personnel | | received 130 and 65 mrem whole body exposures) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37029 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WASHINGTON DEPARTMENT OF HEALTH |NOTIFICATION DATE: 05/24/2000| |LICENSEE: SPEARS ENGINEERING & TECHNICAL SERVIC|NOTIFICATION TIME: 18:26[EDT]| | CITY: SOUTH SEATTLE REGION: 4 |EVENT DATE: 05/22/2000| | COUNTY: STATE: WA |EVENT TIME: 18:00[PDT]| |LICENSE#: WN-I0357-1 AGREEMENT: Y |LAST UPDATE DATE: 05/24/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CLAUDE JOHNSON R4 | | |WAYNE HODGES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: FRAZEE | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE REPORTED A STOLEN PORTABLE GAUGE. | | | | The licensee reported on May 23 that at approximately 6:00 PM the previous | | evening a Seaman Nuclear C-200 gauge, serial number A-872, with 4.5 | | milligrams of Ra-226 was stolen. The licensee's technician had stopped by a | | friend's house in South Seattle on his way home. While there, his pickup | | truck was stolen from in front of the house. The gauge was locked, in a | | locked transport box, and the box was chained and locked in the bed of the | | truck. The licensee believes the thief wanted only the truck and will | | probably abandon the gauge. The police were notified and the licensee was | | advised to notify the local papers and post a reward. | | | | Overexposures? Unknown | | | | Disposition/recovery: Unknown at this time | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37030 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/24/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 20:27[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/24/2000| +------------------------------------------------+EVENT TIME: 18:04[EDT]| | NRC NOTIFIED BY: SERATA |LAST UPDATE DATE: 05/24/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: |JOSEPH GIITTER IRO | |NINF INFORMATION ONLY |JACK CRLENJAK R1 | | |JOHN HANNON NRR | | |JOHN ZWOLINSKI NRR | | |ROY ZIMMERMAN NRR | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 19 Power Operation |19 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MAIN TRANSFORMER EXPLOSION AND FIRE WITHIN FIVE FEET OF THE TURBINE | | BUILDING. | | | | PRIOR TO THE EVENT, THEY HAD JUST CLOSED THE MAIN TURBINE AND GENERATOR | | OUTPUT BREAKERS SO THAT THE TURBINE WOULD SYNCHRONIZE TO THE GRID. AT 1804 | | A MAIN TURBINE TRIP AND MAIN TRANSFORMER TROUBLE ALARM WAS RECEIVED IN THE | | CONTROL ROOM. SUBSEQUENT TO THE TURBINE TRIP, MAIN GENERATOR TRANSFORMER | | FIRE ALARMS WERE RECEIVED AND VISUAL VERIFICATIONS CONFIRMED A FIRE ON THE | | "C" PHASE OF THE MAIN GENERATOR TRANSFORMER. THE FIRE DELUGE SYSTEM | | ACTIVATED, AND ALTHOUGH EXTERNAL INDICATION THE FIRE HAD CEASED, IT IS | | EXPECTED THAT THE FIRE CONTINUES TO BURN INTERNALLY TO THE TRANSFORMER. ALL | | OFFSITE POWER SOURCES ARE STILL AVAILABLE. NO OFFSITE FIRE ASSISTANCE HAS | | BEEN REQUESTED. THE FIRE HAS BEEN ONGOING INTERNALLY FOR APPROXIMATELY TWO | | HOURS. THEY ARE IN THE PROCESS OF ELECTRICALLY ISOLATING THE TRANSFORMER | | FROM BOTH THE GENERATOR AND THE GRID AND TAGGING IT OUT. DELUGE ACTUATION | | HAS BEEN SECURED AND THEY ARE SPRAYING THE TRANSFORMER WITH FIRE WATER. THEY | | ARE ALSO MAKING PREPARATIONS TO USE A FOAM FIRE SUPPRESSION AGENT. | | | | FURTHER EVALUATION CONTINUES IN REGARD TO THE ENVIRONMENTAL IMPLICATIONS OF | | THE EVENT. SPECIFICALLY, THE ABILITY OF THE PLANT OIL WASTE SYSTEM TO | | PROPERLY PROCESS THE MIXTURE OF WATER AND OIL THAT WERE PRODUCTS OF THE | | COMPONENT FAILURE AND SUBSEQUENT FIRE FIGHTING EFFORTS. | | | | THE LICENSEE WILL KEEP THE NRC INFORMED OF ANY ADVERSE CHANGES. | | | | THE NRC RESIDENT INSPECTOR WILL BE INFORMED. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021