Event Notification Report for May 23, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/22/2000 - 05/23/2000 ** EVENT NUMBERS ** 37015 37016 37017 37018 37019 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37015 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 05/22/2000| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 04:48[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 02:53[EDT]| | NRC NOTIFIED BY: BOB KIDDER |LAST UPDATE DATE: 05/22/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN MADERA R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - ESF ACTUATION OF REACTOR WATER CLEANUP SYSTEM FOR UNKNOWN REASONS - | | | | At 0253 on 05/22/00, the plant experienced an isolation of the Reactor Water | | Cleanup System on a Division 2 isolation signal when the Residual Heat | | Removal heat exchanger vent valve closed unexpectedly. An apparent | | electrical power supply spike to the Division 2 isolation instrumentation | | occurred. No testing or maintenance activities or electrical storms were | | occurring at the time of the isolation. The licensee is investigating the | | cause of the isolation. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37016 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 05/22/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 13:42[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 12:59[EDT]| | NRC NOTIFIED BY: ABRAMSKI |LAST UPDATE DATE: 05/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING (RCIC) SYSTEM MAY NOT BE PROTECTED BY STEAM | | LEAK DETECTION CIRCUITRY. | | | | A LICENSEE ENGINEERING REVIEW IDENTIFIED A SECTION OF RCIC SYSTEM PIPING | | WHICH MAY NOT BE PROTECTED BY THE STEAM LEAK DETECTION CIRCUITRY. | | SPECIFICALLY, THE STEAM SUPPLY ISOLATION SIGNAL MAY NOT ISOLATE A POSTULATED | | CRACKED STEAM SUPPLY LINE PRIOR TO CRACK PROPAGATION AS IN THE DESIGN INTENT | | OF THE STEAM LEAK DETECTION SYSTEM. THE LICENSEE IS CONTINUING WITH ITS | | INVESTIGATION. THE RCIC SYSTEM WAS NOT DECLARED INOPERABLE AND THE LICENSEE | | HAS NOT ENTERED ANY LCO ACTION STATEMENTS. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37017 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 05/22/2000| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 16:27[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 11:53[CDT]| | NRC NOTIFIED BY: LYNCH |LAST UPDATE DATE: 05/22/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSITIVE TEST FOR ALCOHOL | | | | AN ENTERGY EMPLOYEE TESTED POSITIVE FOR ALCOHOL FOLLOWING A FOR-CAUSE TEST. | | UPON NOTIFICATION, THE EMPLOYEE'S PLANT ACCESS AUTHORIZATION WAS SUSPENDED | | AT RIVER BEND STATION PENDING FURTHER INVESTIGATION. | | | | THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37018 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 05/23/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 00:11[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 21:59[CDT]| | NRC NOTIFIED BY: JOHN LECHMAIER |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUTO Rx SCRAM FROM 100% AFTER REPLACEMENT OF MAIN TURBINE CONTROL VALVE | | SOLENOID - | | | | On 05/21/00, the Unit 2 Main Turbine #1 Control Valve Fast Acting Solenoid | | failed its required Tech Spec Surveillance Test. | | | | At 2159 CDT on 05/22/00, during return to service activities following | | replacement of this solenoid, Unit 2 automatically scrammed from 100% power | | due to receipt of an APRM High-High RPS Actuation signal. All control rods | | inserted completely. No safety/relief valves lifted. Steam is being dumped | | to the main condenser. During the transient, reactor vessel water level | | dropped to +8 inches (normal level is +30 inches) and all PCIS Group II | | actuations occurred, as expected. These actuations included Reactor | | Building Ventilation Valves closed, Train 'A' Standby Gas Treatment System | | auto started (Train 'B' SBGT System was inoperable), Control Room | | Ventilation System isolated, and Containment Isolation Valves closed. Quad | | Cities has one Emergency Diesel Generator (EDG) for each unit and a shared | | EDG. The Unit 2 EDG received a spurious auto start signal during the 4 KV | | auxiliary bus power transfer to the reserve transformer. The licensee | | secured the Unit 2 EDG. | | | | Unit 2 is now stable in Condition 3 (Hot Shutdown) with reactor vessel water | | level within its normal band. | | | | This event had no effect on Unit 1 which is at 100% power. | | | | The licensee is investigating the cause of this reactor scram. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37019 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/23/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 02:52[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/22/2000| +------------------------------------------------+EVENT TIME: 23:38[EDT]| | NRC NOTIFIED BY: NICK CONICELLA |LAST UPDATE DATE: 05/23/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 4 Startup |4 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HIGH PRESSURE COOLANT INJECTION SYSTEM AUTO ISOLATED WHILE BRINGING IT ON | | LINE - | | | | At 2338 on 05/22/00, the High Pressure Coolant Injection (HPCI) System | | isolated due to a spurious high steam flow isolation signal. A valid high | | steam line flow condition would normally be indicative of a piping break; | | however, a piping break did not occur. Although the signal was not valid, | | this is nonetheless considered an Engineered Safety Features (ESF) Actuation | | since a containment isolation had occurred. | | | | The Hope Creek reactor was in Operational Condition 2 (Startup) with Reactor | | Coolant System (RCS) pressure at 200 psig and power at about 4%. The HPCI | | System steam line warmup, which is required to place the HPCI System in a | | standby alignment, had just commenced. When shutdown, the HPCI steam line | | is isolated from the reactor by three containment isolation valves. These | | valves are an outboard valve, an inboard valve, and a bypass valve around | | the inboard valve for steam line warm-up purposes. As part of the steam | | line warmup procedure, the outboard valve is fully opened and the inboard | | bypass valve is throttled to slowly heat up and pressurize the steam line. | | Once the steam line is pressurized, the inboard valve is opened. | | | | During the initial phases of the steam line warmup process, a high steam | | line flow signal was generated when the bypass valve was throttled open. | | This occurred due to steam pressure and flow perturbations within the steam | | line. As a result, an isolation signal was generated and the bypass valve | | automatically closed as expected for this isolation signal. Prior to | | resetting the isolation signal, the HPCI steam line was verified to be | | operable. The HPCI System warmup was then recommenced and the HPCI System | | is currently in its standby alignment. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021