Event Notification Report for May 17, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/16/2000 - 05/17/2000 ** EVENT NUMBERS ** 36961 37001 37007 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36961 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 05/03/2000| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 12:40[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 05/03/2000| +------------------------------------------------+EVENT TIME: 10:45[CDT]| | NRC NOTIFIED BY: DON POPP |LAST UPDATE DATE: 05/16/2000| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 1 HOUR SECURITY REPORT | | | | Unescorted protected area access granted inappropriately. Immediate | | compensatory measures taken. | | | | The licensee will notify the NRC Resident Inspector. | | | | Contact the Headquarters Operations Center for additional details | | | | * * * RETRACTION ON 05/16/00 AT 1128 ET BY BRAIN KOPETSKI TAKEN BY MACKINNON | | * * * | | | | After further review of this event and conversations with NRC Region 3 this | | event is being retracted. The event is being made a loggable because the | | person's access denial would not have in itself been enough to deny | | access. R3DO (John Madera) notified. | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37001 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 05/15/2000| | UNIT: [1] [] [] STATE: CA |NOTIFICATION TIME: 04:04[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/15/2000| +------------------------------------------------+EVENT TIME: 00:43[PDT]| | NRC NOTIFIED BY: STEVE HACKLEMAN |LAST UPDATE DATE: 05/16/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |CHARLES CAIN R4 | |10 CFR SECTION: |JOSE CALVO NRR | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED |JOSEPH GIITTER IRO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION |EACHES FEMA | |AESF 50.72(b)(2)(ii) ESF ACTUATION |JOSEPH HIMES RCT | |NOCM COMM ASST BRIEF | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DUE TO AUXILIARY TRANSFORMER EXPLOSION & FIRE; LOSS OF OFFSITE | | POWER - | | | | At 0043 PDT on 05/15/00, the licensee declared an Unusual Event due to | | auxiliary transformer #1-1 exploding and catching on fire. This resulted in | | the loss of offsite power and an automatic trip of Unit 1. The licensee | | called the offsite fire department and they responded to the plant. | | Auxiliary transformer #1-1 is located outside the turbine building (north | | end). | | | | Three of three Unit 1 emergency diesel generators started and loaded and are | | supplying emergency power to vital Unit 1 buses. Auxiliary transformer #1-1 | | supplies backup power to Unit 1 emergency buses. The Unit 1 12 KV buses are | | energized. Unit 1 reactor coolant pumps are running providing forced | | circulation. | | | | Unit 1 automatically tripped from 100% power. All control rods inserted | | completely. Steam is being dumped to the atmosphere. Unit 1 has no steam | | generator tube leaks and no fuel leaks. The auxiliary feedwater system | | automatically started, as expected. A #1-2 steam generator code safety | | valve failed open for about 25 - 30 minutes about 30 minutes after the | | reactor trip. The valve is now closed. There was no safety injection | | actuation. | | | | Unit 1 is stable in Mode 3 (Hot Standby). | | | | This event had no effect on Unit 2 which is stable at 100% power. | | | | The licensee notified state and local officials and the NRC Resident | | Inspector. | | | | At 0143 PDT, the fire is out. No personnel were injured. | | | | At 0405 CDT, NRC Region 4 entered the Monitoring Phase of Normal NRC | | Response Mode. | | | | * * * UPDATE AT 0726 ON 05/15/00 FROM MARK LEMKE TO JOLLIFFE * * * | | | | The licensee determined that an electrical fault on the low voltage side of | | auxiliary transformer #1-1 caused extensive damage to the 12 KV buswork and | | nearby buswork used to supply the Unit 1 4 KV buses from offsite power | | following a plant shutdown. Auxiliary transformer #1-1 did not explode and | | is intact. | | | | The licensee also determined that there was not a failure of a main steam | | code safety valve. However, following closure of the main steam isolation | | valves, a code safety valve on the #1-2 steam generator did lift and did not | | fully reseat. Plant operators took manual action to lower steam generator | | pressure, causing the valve to reseat. There was no release of radiation | | from the plant. | | | | The California Department of Forestry responded to the site. | | | | The licensee is continuing to investigate the cause of this explosion and | | has issued a press release. | | | | * * * AT 0900 ON 05/15/00 COMMISSIONERS' ASSISTANTS BRIEFING * * * | | | | IRO (Frank Congel, Joe Giitter); NRR Projects (Steve Dembek); OPA (Bill | | Beecher); OSP (Cardelia Maupin); IP (Howard Faulkner); CA (Tom Combs); | | Chairman Meserve Asst (Mike Tschiltz); Comm Dicus Asst (Joe Olencz); Comm | | McGaffigan Asst (Jeff Sharkey); Comm Diaz Asst (Tony Hsia); Comm Merrifield | | Asst (John Thoma); NRR (Ed Goodwin); R4 (Elmo Collins [Briefer], Bill Jones, | | et al). | | | | * * * UPDATE AT 1358 EDT ON 5/16/00 BY D. PETERSON TO FANGIE JONES * * * | | | | The licensee terminated the Unusual Event at 0959 PDT. Offsite power has | | been restored to the 4 KV vital busses. The diesel generators have been | | shutdown. The RCS temperature is 380 �F and pressure is 920 psig. The | | plant will continue to Cold Shutdown after chemistry hold is complete. | | | | The licensee notified the NRC Resident Inspector. The NRC Headquarters | | Operation Officer notified the R4DO (Bill Jones), IRO (Joseph Giitter), NRR | | (William Beckner), EDO Office (Mark Satorius), PAO (Sue Gagner), FEMA | | (Austin). | | | | NRC Region 4 exited the Monitoring Phase of Normal Mode at 1414 EDT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37007 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 05/16/2000| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 07:28[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 05/15/2000| +------------------------------------------------+EVENT TIME: 09:30[EDT]| | NRC NOTIFIED BY: CHUCK McKINNEY |LAST UPDATE DATE: 05/16/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRIAN BONSER R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR FITNESS FOR DUTY EVENT - | | | | At 0930 on 05/15/00, a licensee supervisor tested positive for alcohol | | during a random drug and alcohol test. The licensee withdrew the employee's | | access authorization to the plant protected area after verification of the | | positive test. The licensee is determining further corrective actions. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021