Event Notification Report for May 12, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/11/2000 - 05/12/2000 ** EVENT NUMBERS ** 36989 36990 36991 36992 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36989 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/11/2000| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 09:29[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/11/2000| +------------------------------------------------+EVENT TIME: 01:00[EDT]| | NRC NOTIFIED BY: G. FIEDLER |LAST UPDATE DATE: 05/11/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN APPARENT LIGHTNING STRIKE CAUSED THE LOSS OF ALL EMERGENCY SIRENS. | | | | An apparent lightning strike caused the loss of all Emergency Sirens. | | Emergency Sirens were discovered inoperable at 0815 ET. Both repeaters for | | the Emergency Sirens were found inoperable. Emergency Sirens were returned | | to service at 0840 ET when one of the repeaters was restored to service. | | The licensee will inform state and local officials of the loss of their | | Emergency Sirens. | | | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36990 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 05/11/2000| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 12:27[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/11/2000| +------------------------------------------------+EVENT TIME: 08:18[CDT]| | NRC NOTIFIED BY: TURNER |LAST UPDATE DATE: 05/11/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD A REACTOR WATER CLEANUP ( RWCU) ISOLATION WHILE THEY WERE | | PLACING A DEMINERALIZER FILTER IN SERVICE. | | | | "While placing Reactor Water Cleanup Demin "B" in service following a | | precoat, received Division 2 isolation on sustained High Differential flow | | of 55 gpm for 45 seconds. The following valves received closed signals | | G33-F001, RWCU PUMPS INBD SUCTION VALVE, G33-F040, RWCU RETURN INBOARD ISOL. | | VALVE, G33-F053, RWCU PUMPS INBD DISCH VALVE, G33-F02, RWCU INBD DRAIN VAL. | | The Systems responded as designed with all valves closed and the Reactor | | Water Cleanup Pumps tripped. Note: G33-F028 RWCU INBD DRAIN VAL was already | | closed. | | | | "The isolation appears to be valid. The cause of the isolation appears to be | | that valves used to flush a strainer were not full closed, causing flow to | | the Backwash Receiving Tank where it was fully contained. The valves were | | locally visibly verified closed, but the valves were actually 1/2 open. | | Local position indications for both valves appeared to be defective. The | | plant is stable and plans for restoration of the RWCU system are in | | progress." | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36991 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WAYNE CTY ENG TESTING OFFICE |NOTIFICATION DATE: 05/11/2000| |LICENSEE: WAYNE CTY ENG TESTING OFFICE |NOTIFICATION TIME: 15:00[EDT]| | CITY: DETROIT REGION: 3 |EVENT DATE: 05/11/2000| | COUNTY: STATE: MI |EVENT TIME: 14:00[EDT]| |LICENSE#: 21-13687-01 AGREEMENT: N |LAST UPDATE DATE: 05/11/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MELVYN LEACH R3 | | |DON COOL NMSS | +------------------------------------------------+BRENT CLAYTON R3 | | NRC NOTIFIED BY: FAKHOURY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | WAYNE COUNTY ENGINEERING REPORTED DAMAGE TO CPN DENSITY GAUGE. | | | | THE GAUGE WAS BEING USED IN DETROIT, MI. AT A ROAD MAINTENANCE SITE WHEN IT | | WAS RUN OVER BY A CAR. THERE WAS NO MAJOR DAMAGE OR CRACKS TO THE | | DEVICE(CPN MODEL MC3-82 PORTABLE) WHICH CONTAINED 10 MILLICURIE OF CS-137 | | AND 50 MILLICURIE OF AMERICIUM-241/BERYLLIUM. NO LEAKAGE WAS DETECTED WHEN | | THEY MADE A SURVEY. THE DEVICE, WHICH HAD A SLIGHT DENT AND BENT ROD WAS | | PLACED BACK INTO ITS BOX AND WILL BE TAKEN TO THEIR FACILITY FOR STORAGE. | | THE MANUFACTURER WILL BE CONTACTED TOMORROW. WAYNE COUNTY ENGINEERING | | CONTACTED NRC REGION 3 (SIMMONS). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36992 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 05/11/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 16:41[EDT]| | RXTYPE: [1] GE-2 |EVENT DATE: 05/11/2000| +------------------------------------------------+EVENT TIME: 16:40[EDT]| | NRC NOTIFIED BY: DEMONCH |LAST UPDATE DATE: 05/11/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE IDENTIFIED A DEGRADED FIRE BARRIER BETWEEN THE 4160 C AND D | | VAULTS. | | | | The licensee identified the wall protecting the C & D 4160 vaults/rooms from | | each other as a 3 hour rated fire barrier. It has been determined that the | | wall as is does not meet the requirement for a 3 hour rating. Structural | | steel for the wall does not have the required thickness of "Pyrocrete 102" | | to provide a 3 hour rating. The wall is considered functional given the low | | fire loading in each room and the presence of automatic fire detection and | | manual suppression. They have commenced an hourly watch for the effected | | area. | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021