Event Notification Report for May 11, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/10/2000 - 05/11/2000 ** EVENT NUMBERS ** 36921 36987 36988 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36921 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 04/23/2000| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 06:49[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/23/2000| +------------------------------------------------+EVENT TIME: 03:35[EDT]| | NRC NOTIFIED BY: BRIAN MOTZ |LAST UPDATE DATE: 05/10/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK RING R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 TRAIN 'B' ESSENTIAL SERVICE WATER PUMP STARTED AUTOMATICALLY | | | | While setting up for testing the Solid State Protection System (SSPS) on | | Unit 2, the clearance permit did not anticipate the start of the Unit 1 | | train 'B' Essential Service Water (ESW) Pump. | | | | "To perform maintenance on the SSPS, a clearance to deenergize the SSPS | | cabinets in Unit 2 was written. The Unit 2 SSPS was in inhibit at this | | time. During the deenergization per this clearance, an automatic start of | | the Unit 1 East ESW Pump occurred. The ESW Pump autostart was not | | anticipated or described in the clearance. | | | | "A Safety Injection (SI) signal through SSPS in either Unit 1 or Unit 2 will | | cause the ESW Pumps in both units to autostart for the train effected. | | Similarly, the removal of power from the control room instrumentation | | distribution circuit, which is what occurred here, will cause the autostart | | of the ESW pumps. | | | | "There were no adverse consequences as a result of the auto pump start and | | the actuation was per the system design. No SI signal was generated." | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1822 ON 5/10/00 BY WOODS RECEIVED BY WEAVER * * * | | | | "The original report was made regarding an automatic start of the Unit 1 | | East Essential Service Water (ESW) Pump during maintenance, and was | | conservatively reported as an automatic actuation of an Engineered Safety | | Feature (ESF). Subsequent reviews of the pump start event and the | | reportability requirements of 10 CFR 50.72 and 50.73 have confirmed that | | this event is not reportable. | | | | "In the case of the start of the 1 E ESW Pump, the ESF actuation slave relay | | never was actuated, but was deenergized and would not have actuated. No | | other portion of the associated ESF actuation circuitry was completed. | | Additionally, the ESW pump was not manually started in an emergency response | | to plant conditions that would have required the pump to be operating. | | | | "NUREG-1022, Revision 1, Event Reporting Guidelines: 10CFR50.72 and 50.73, | | Part 3.3.2, Actuation Of An Engineered Safety Feature Or The RPS, provides | | guidance for the reporting requirements of an ESF actuation event as listed | | in 10 CFR 50.72 and 50.73. The NUREG states that actuation of certain | | single ESF components of complex systems need not be reported. Single | | components of complex systems, by themselves, usually do not mitigate the | | consequences of significant events. | | | | "Based on the facts that this event was an inadvertent start of a single | | component that would not mitigate the consequences of a significant event, | | and that the minimum amount of ESF actuation logic, i.e., the slave relay, | | did not actuate, the event is not reportable under 10 CFR 50.72 or 50.73. | | Therefore, the 4 hour non-emergency report, event number 36921, is being | | retracted." | | | | The licensee informed the NRC resident inspector of this report. The | | Operations Center notified the R3DO (CLAYTON). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36987 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 05/09/2000| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 21:19[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 05/09/2000| +------------------------------------------------+EVENT TIME: 20:39[EDT]| | NRC NOTIFIED BY: DAVID COSEO |LAST UPDATE DATE: 05/10/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | COMPENSATORY MEASURES TEMPORARILY SUSPENDED DUE TO INCLEMENT WEATHER. | | CONTACT THE OPERATIONS CENTER FOR ADDITIONAL DETAILS. | | | | * * * Updated on 5/10/00 to reflect correct reactor mode of cold shutdown | | vice hot shutdown * * * | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36988 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF CONNECTICUTT |NOTIFICATION DATE: 05/10/2000| |LICENSEE: UNIVERSITY OF CONNECTICUTT |NOTIFICATION TIME: 11:56[EDT]| | CITY: STORRS REGION: 1 |EVENT DATE: 05/05/2000| | COUNTY: STATE: CT |EVENT TIME: 09:30[EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 05/10/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN ROGGE R1 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KEN PRICE | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE LOSS OF A TRITIATED EXIT SIGN | | | | During final walkthrough for renovation of the Waring Chemistry Building, | | one tritiated exit sign appears to be missing. Eleven signs were collected, | | but there appeared to be a "spot" on the wall at one exit where it appears a | | sign had hung. A search was conducted of the building without finding any | | indication of the sign. There is no inventory of the signs so there is no | | positive way of determining that a sign is actually missing. The sign would | | by a model 101 by Shield Source Incorporated if it matches the rest of the | | signs. The sign contained 7 curies of tritium on 1/93 and would contain | | about 5 curies now. The university plans to send out a flyer looking for | | the sign and provide warning of the hazards involved. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021