Event Notification Report for May 9, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/08/2000 - 05/09/2000 ** EVENT NUMBERS ** 36953 36981 36982 36983 36984 36985 36986 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36953 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 05/02/2000| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 10:59[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 05/02/2000| +------------------------------------------------+EVENT TIME: 07:00[CDT]| | NRC NOTIFIED BY: TOM WEBB |LAST UPDATE DATE: 05/08/2000| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DEFECTIVE STEAM GENERATOR TUBES | | | | Analysis of "B" steam generator eddy current results determined that more | | than 1% of the Westinghouse HEJ sleeve laser weld repaired tubes were | | classified as defective placing the "B" steam generator in the C-3 | | classification per the Kewaunee Technical Specifications. Two tubes of 59 | | inspected contained indications in the weld repaired region. There are 288 | | total tubes in this population. The licensee plans to increase the | | population size to 100%. | | | | The NRC Resident inspector has been notified. | | | | | | * * * UPDATE ON 05/09/00 AT 1153ET BY TOM WEBB TAKEN BY MACKINNON * * * | | | | Analysis of "A" steam generator eddy current results determined that more | | than 1% of the tubes inspected in the hot leg tube sheet crevice region are | | classified as defective, placing steam generator "A" in the C3 category per | | Kewaunee Nuclear Power Plant Technical Specification. Fifteen tubes out of | | 833 inspected were characterized as defective. | | | | No scope expansion is necessary as 100% of the tubes for the hot leg | | tubesheet crevice region have been inspected. | | | | Corrective Action: | | | | 1. Plug or repair defective tubes prior to returning to operation. | | 2. Ensure plugging rate does not result in an unanalyzed condition. | | | | NRC R3DO (Brent Clayton) notified. | | | | The NRC Resident Inspector was notified of this update by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36981 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 05/08/2000| | UNIT: [] [2] [] STATE: CT |NOTIFICATION TIME: 00:44[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 05/08/2000| +------------------------------------------------+EVENT TIME: 00:15[EDT]| | NRC NOTIFIED BY: STEVE MYERS |LAST UPDATE DATE: 05/08/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DIESEL GENERATOR STARTED DURING TESTING | | | | The 'A' emergency diesel generator (EDG ) automatically started due to a bus | | undervoltage signal that was inadvertently caused when a procedural step was | | misinterpreted. The EDG was secured. The licensee has informed the NRC | | resident inspector of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36982 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/08/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 01:37[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/07/2000| +------------------------------------------------+EVENT TIME: 22:43[EDT]| | NRC NOTIFIED BY: NICK CONICELLA |LAST UPDATE DATE: 05/08/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WATER CLEANUP ISOLATION DUE TO INADVERTENT STANDBY LIQUID CONTROL | | SIGNAL | | | | "On 5/7/00 at 2243 hours, a Reactor Water Cleanup System (RWCU) isolation | | occurred due to an inadvertent Standby Liquid Control System (SLC) | | initiation. At the time of the event, Hope Creek was in Operational | | Condition 5, Refueling, with core reload activities recently initiated and | | with all control rods fully inserted. SLC was not required to be operable | | and was removed from service (injection line check valves were closed) when | | the SLC initiation signal occurred. No sodium pentaborate was injected into | | the Reactor Coolant System. Preliminary investigation into the event | | determined that the SLC initiation signal resulted from activities | | supporting required surveillance testing of SLC along with surveillances of | | the Redundant Reactivity Control System (RRCS). The RRCS provides automatic | | SLC initiation. Although the RWCU isolation instrumentation was also not | | required to be operable at the time of the event, it was not removed from | | service. The RWCU isolation due to a SLC initiation signal is an ESF | | actuation. Both SLC pumps actuated as designed in response to the initiation | | signal, however, a crack was observed in a weld in the 'A' SLC injection | | line when the SLC pump was removed from service. Event investigation is | | continuing and repairs to SLC are being initiated. The RWCU isolation signal | | was reset and the RWCU was placed back in service. Core reload activities | | are continuing." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36983 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/08/2000| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 05:25[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/08/2000| +------------------------------------------------+EVENT TIME: 03:56[EDT]| | NRC NOTIFIED BY: RANDY HAISLET |LAST UPDATE DATE: 05/08/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POST-ACCIDENT SAMPLING SYSTEM ISOLATION DURING TAGOUT | | | | While performing a tagout on the 'A' train of the post-accident sampling | | system (PASS) H2/O2 sampling system, solenoid isolation valve SV-5065-20B, | | which is a 'B' train valve, closed unexpectedly. The licensee restored the | | 'A' train of PASS H2/O2 monitoring to service and closed the redundant | | solenoid isolation valve in the 'B' train. The licensee declared valve | | SV-5065-20B inoperable. | | | | After review of system electrical diagrams, the licensee determined that the | | closure of valve SV-5065-20B was appropriate, although its closure was not | | anticipated in the tagout procedure. The NRC resident inspector has been | | informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36984 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/08/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:22[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/05/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 21:30[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/08/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRENT CLAYTON R3 | | DOCKET: 0707001 | | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC WALKER | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY EQUIPMENT FAILURE | | | | At 2130 CDT on 5/05/2000, the C-337 Unit 3 Cell 2 Freezer/Sublimer A-valve | | failed to open while in TSR mode F/S 3 which requires operability of the | | A-valve in order for the valve to open if required to do so upon actuation | | of the Freezer/Sublimer High-High Weight Trip System. An operator was | | attempting to place the Freezer/Sublimer into mode F/S 2 which does not | | require operability of the High-High Weight Trip System. The | | Freezer/Sublimer was unable to enter Mode F/S 2 due to inability to open | | A-valve because of mechanical failure. Actuation of High- High Weight Trip | | system did not occur. However, had it been required to do so while in mode | | F/S 3, there is potential that the A-valve would not have opened as required | | if actuation of system occurred. Upon discovery of valve failure, | | Freezer/Sublimer was placed in mode F/S 4 which does not require operability | | of the High-High Weight Trip system. | | | | The valve failure was caused by a failure of the motor operator in this six | | inch valve. | | | | The NRC Senior Resident Inspector has been notified of this event. See | | related event 36985. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36985 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/08/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:22[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/05/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 21:30[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/08/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRENT CLAYTON R3 | | DOCKET: 0707001 | | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC WALKER | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF A SAFETY SYSTEM | | | | | | At 2130 CDT on 5/05/2000, the C-337 Unit 3 Cell 8 Freezer/Sublimer A-valve | | failed to open while in TSR mode F/S 3 which requires operability of the | | A-valve in order for the valve to open if required to do so upon actuation | | of the Freezer/Sublimer High-High Weight Trip System. An operator was | | attempting to place the Freezer/Sublimer into mode F/S 2 which does not | | require operability of the High-High Weight Trip System. The | | Freezer/Sublimer was unable to enter Mode F/S 2 due to inability to open | | A-valve because of mechanical failure. Actuation of High-High Weight Trip | | system did not occur. However, had it been required to do so while in mode | | F/S 3, there is potential that the A-valve would not have opened as required | | if actuation of system occurred. Upon discovery of valve failure, | | Freezer/Sublimer was placed in mode F/S 4 which does not require operability | | of the High-High Weight Trip system. | | | | The valve failure was caused by a failure of limit switch on the valve. | | | | The NRC Senior Resident Inspector has been notified of this event. See | | related event 36984. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36986 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/08/2000| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 20:56[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/08/2000| +------------------------------------------------+EVENT TIME: 20:25[EDT]| | NRC NOTIFIED BY: JOSEPH GIAR |LAST UPDATE DATE: 05/08/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OUTSIDE DESIGN BASIS - FOULING OF THE REACTOR BUILDING CLOSED COOLING WATER | | HEAT EXCHANGER (RBCCW HX). | | | | Surveillance testing has identified fouling of the Salt Service Water (SSW) | | side of the RBCCW HX. The extent of the fouling on one of the two heat | | exchangers would prevent design basis containment heat removal post-accident | | at maximum design basis ultimate heat sink (UHS) temperature (75�F). | | Engineering evaluation has determined that design basis heat removal can be | | achieved with UHS temperature less than 70�F. Periodic evaluation will be | | performed to ensure that additional fouling has not further degraded the | | heat exchangers heat transfer capability. | | | | The licensee will inform the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021