Event Notification Report for May 5, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/04/2000 - 05/05/2000 ** EVENT NUMBERS ** 36967 36969 36970 36971 36972 36973 36974 36975 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36967 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/03/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 22:27[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/03/2000| +------------------------------------------------+EVENT TIME: 22:15[EDT]| | NRC NOTIFIED BY: TONY PETRELLI |LAST UPDATE DATE: 05/04/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |96 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 TECH SPEC REQD SHUTDOWN DUE TO 2 CONTAINMENT PURGE VALVES FAILING | | THEIR LLRT- | | | | The licensee is shutting Unit 2 down from 100% power in accordance with Tech | | Spec 3.6.3.A, 12 Hour Shutdown LCO, due to containment purge valves | | #CPS*AOV-104 & 106 failing their local leak rate test #N2-ISP-CPS-Q001. | | | | The licensee notified the NRC Resident Inspector. | | | | * * *UPDATE ON 05/04/00 AT 0002 ET BY M. ERON TAKEN BY MACKINNON * * * | | | | Licensee exited Technical Specification 3.6.3.A at 2350 ET after manual | | Containment Purge Supply valve, 2CPS-V6, an upstream valve to #CPS*AOV-104 & | | 106 was leak tested and verified closed. Lowest reactor power level reached | | was 92%. R1DO (Della Greca) notified. | | | | The NRC Resident Inspector was notified of this update by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36969 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/04/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 05:46[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/03/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 08:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/04/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE BURGESS R3 | | DOCKET: 0707002 |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SISLER | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL FOR ACCUMULATION OF SLUDGE CONTAINING HEAVY METALS ON/IN THE LID | | OF TUB | | | | NRC BULLETIN 91-01 24 hour notification | | | | On 5/3/00 at 0800 hours it was discovered that a NCSA-0705_027.A003 control | | was not in place. The sludge tub used for accumulating heavy metal | | (including uranium) sludge had an unsafe/unfavorable geometry molded into | | the design. The unfavorable dimensions created by the raised lip is 7.75" by | | 37" by 2". This could have resulted in the potential accumulation, of an | | unsafe volume on the sludge tub lid had a leak developed In a nearby system | | containing uranium-bearing solution. | | | | NCSA-705_027.A003 requirement #17 states "Geometrically unfavorable | | containers shall not be left uncovered while unattended in the heavy metals | | precipitation process area or on the mezzanine in the area of the heavy | | metals precipitation raffinate storage (HMPRS)". This was a loss of one | | control (geometry/volume) in the double contingency principle for the afore | | mentioned NCSA. The second control (physical integrity of nearby | | uranium-bearing systems) was maintained throughout the event. | | | | At the direction of the Plant Shift Superintendent (PSS), the requirements | | for the NCS anomalous condition were initiated. At 1015 hours compliance was | | regained by covering the molded design | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | On May 3, 2000, it was discovered that the sludge tub used for accumulating | | sludge containing heavy metals (including uranium) contains an accumulation | | point on/in the lid. That accumulation point is created by a raised lip and | | has unfavorable geometric dimensions (7.75" by 37" by 2"). This is a | | violation of NCSA-0705_027 and NCSA-0705_076. This could have resulted in | | the potential accumulation of an unsafe volume of solution on/in the sludge | | tub lid had a leak developed in a nearby system which contain | | uranium-bearing solution. No uranium-bearing material was involved in the | | violation, since the remaining barrier to criticality (i.e., the physical | | integrity of nearby uranium-bearing systems) was maintained. Therefore, the | | safety significance of this event is low. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | If a leak had developed in a nearby uranium-bearing system such that the | | solution could have accumulated on/in the sludge tub lid, an unsafe geometry | | of solution could have resulted. If the leaking solution had contained a | | sufficient amount of uranium, the resulting configuration could have been | | sufficient for a criticality to occur. It should be noted that the allowed | | safe geometry and volume limits established In NCSA-0705_076 are based on | | potentially moderated, UO2F2 and water solution which contains uranium | | enriched to 100 wt%. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | The parameter which was violated during this upset was the geometry of | | potential accumulation present in the sludge tub lid (i.e., the volume in | | which uranium-bearing solution could have accumulated in the event of a | | leak). The physical integrity of the nearby systems containing | | uranium-bearing material was maintained. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | No uranium bearing material was actually introduced into the lid of the | | sludge tub. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES | | | | NCSA-0705_076.A00 and NCSA-0705_027 take credit for the physical integrity | | of Systems which contain uranium-bearing material and that unsafe | | volume/geometry containers are either modified, covered, or oriented to | | prevent an unsafe configuration from resulting In the event of a leak. The | | lid of the sludge tub observed was not protected from a potential | | accumulation and it had been left unattended. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | At 0800 hours, a NCS anomalous condition was initiated. | | | | At 1015 hours compliance was re-established | | | | The NRC Resident Inspector was notified of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36970 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TENNESSEE DIV OF RAD HEALTH |NOTIFICATION DATE: 05/04/2000| |LICENSEE: STUDSVICK PROCESSING FACILITY, LLC |NOTIFICATION TIME: 09:45[EDT]| | CITY: ERWIN REGION: 2 |EVENT DATE: 04/30/2000| | COUNTY: STATE: TN |EVENT TIME: 12:00[EDT]| |LICENSE#: R-S1001 AGREEMENT: Y |LAST UPDATE DATE: 05/04/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROBERT HAAG R2 | | |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DEBRA SHULTS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 5000 SQUARE FOOT AREA CONTAMINATED WITH AN ESTIMATED 0.49 MILLICURIES OF | | PRIMARILY COBALT-60. | | | | | | On 05/01/2000, the licensee called to report a spill of residue inside their | | processing building. A 5000 square foot area was affected/contaminated | | with an estimated 0.49 millicuries of mixed fission/activation products | | (primary Co-60) when the event occurred on 04/30/00. Gross maslin smears | | revealed 30,000 dpm with a maximum small area smear of 6,600 dpm/100 square | | centimeter. There was no release of radioactive material to the | | environment. There were two minor personnel contamination incidents: one | | involving an individual's shoes and one involving an individual's hair. | | Both were easily decontaminated and released. There was no damage to | | equipment. Decontamination had already begun when reported. This event | | does not pose a risk to public health and safety but is reportable under | | 1200-2-5-141 (2)(c)1 i, ii, and iii. It required restricted access for | | greater than 24 hours, 0.49 millicuries is greater than 5 times the lowest | | ALI for Co-60, and access was restricted to allow isotopes with less than 24 | | half-lives to decay. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36971 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 05/04/2000| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 16:36[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 05/04/2000| +------------------------------------------------+EVENT TIME: 13:24[EDT]| | NRC NOTIFIED BY: CASPER JERNIGAN |LAST UPDATE DATE: 05/04/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INADVERTENT SAFETY INJECTION ACTUATION | | | | "Harris Nuclear Plant was in Mode-5 with Reactor Vessel level at -12 inches | | following Mid-Loop operations. A Safety Injection Signal was actuated when | | Instrument Bus S-III was de-energized to return it to its normal power | | supply. Plant procedure MST-I0604 (Time Response Test for Channel 1 | | Pressurizer Pressure) was in progress. This procedure had channel 1 | | Pressurizer Pressure in test. When S-III was de-energized, the Low | | Pressurizer Pressure SI and Low Steam Generator Pressure SI Block signal | | (P-11) were unblocked due to Pressurizer channel III being de-energized | | concurrent with Pressurizer channel 1 in test. The plant was in Mode-5 with | | Pressurizer Pressure and Steam Generator Pressure at approximately 0 psig. | | Pressurizer Low Pressure SI and Low Steam Generator Pressure SI actuated the | | SI signal after P-11 was unblocked. Preparations to perform OST 1826 "Safety | | Injection: ESF Response Time, Train B 18 Month Interval test" were in | | progress. This test had the BIT injection valves closed with power off, | | which prevented ECCS discharge to the RCS. Other equipment operated as | | required in response to the Safety Injection Signal in these plant | | conditions. This actuation did not have any negative impact on RCS | | temperature or inventory control. The plant is currently stable in Mode-5." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36972 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. ARMY |NOTIFICATION DATE: 05/04/2000| |LICENSEE: U.S. ARMY |NOTIFICATION TIME: 16:54[EDT]| | CITY: REDSTONE ARSENAL REGION: 2 |EVENT DATE: 05/04/2000| | COUNTY: STATE: AL |EVENT TIME: [CDT]| |LICENSE#: SNM1998 AGREEMENT: Y |LAST UPDATE DATE: 05/04/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROBERT HAAG R2 | | |JOSEPHINE PICCONE NMSS | +------------------------------------------------+NIEL DELLA GRECA R1 | | NRC NOTIFIED BY: JERRY GRAY |BRUCE BURGESS R3 | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SOURCE SET LOST DURING SHIPPING | | | | Operations for US Army Communications Electronics Command at Fort Monmouth, | | New Jersey shipped, via FedEx, an Amersham large area alpha calibration | | source to US Army at Redstone Arsenal, Alabama on 3/15/2000. The | | calibration set (serial # LAAS-003) contains 3 sources (serial #'s ES-927, | | 928 and 929) with a total of about 18 microcuries of Pu-238. On 4/18/2000, | | Redstone Arsenal contacted US Army Communications Electronics Command in New | | Jersey to inquire about a leak test that was due on the calibration source, | | who in turn informed them that it had been shipped to them in March. A | | search was conducted at Redstone Arsenal without the calibration source set | | being found. FedEx was contacted and a search of the sort center in New | | Jersey, to which the shipment was traced, failed to locate the shipment. | | The US Army is reporting that the source set is missing, assumed lost or | | stolen. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36973 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 05/04/2000| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 18:00[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 05/04/2000| +------------------------------------------------+EVENT TIME: 14:41[EDT]| | NRC NOTIFIED BY: RUSSELL LONG |LAST UPDATE DATE: 05/04/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ABOUT 25 DEAD FISH DISCOVERED IN DISCHARGE CANAL | | | | "On May 4, 2000, at approximately 1441 hours, plant personnel discovered | | dead fish in the discharge canal. There were no plant events or occurrences | | that appear to be causally related. The fish numbered about 25, had an | | average length of about one foot and consisted of gizzard shad, not an | | endangered species. The water in the discharge canal is river water used for | | cooling plant equipment in both Indian Point 2 and 3 during plant operation. | | The fish could not have traveled through the plant to the discharge canal | | since the river water intake has screens to prevent this type of fish | | intrusion. | | | | "This event is reported, within 24 hours, pursuant to Non-radiological | | Environmental Technical Specification 4.1 as an unusual event, a fish kill. | | The cause is being evaluated." | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36974 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 05/04/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 19:02[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 05/04/2000| +------------------------------------------------+EVENT TIME: 13:18[CDT]| | NRC NOTIFIED BY: RICHARD CALVIN |LAST UPDATE DATE: 05/04/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WATER CLEANUP SYSTEM AUTOMATICALLY ISOLATED | | | | The reactor water cleanup system (RWCU) isolated due to ESF signal "high | | flow isolation signal". Originally it was determined to be an invalid | | signal caused by a pressure pulse induced by human error. Additional | | information indicates that it cannot be proven that the isolation was not | | caused by system flow, therefore it has been determined that the event is | | reportable. The system isolated as designed and has been restored. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36975 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 05/04/2000| | UNIT: [] [] [3] STATE: IL |NOTIFICATION TIME: 22:09[EDT]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 05/04/2000| +------------------------------------------------+EVENT TIME: 20:18[CDT]| | NRC NOTIFIED BY: DAVID SLAGER |LAST UPDATE DATE: 05/04/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE BURGESS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 M/R Y 44 Power Operation |0 Hot Standby | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DECREASING CONDENSER VACUUM REQUIRED MANUAL REACTOR SCRAM | | | | "During unit startup from D3F30 forced outage, condenser vacuum was reducing | | on 2 of 3 condenser hoods and condensate demin inlet temperatures were | | rising. The abnormal operating procedure for loss of condenser vacuum was | | entered and actions followed to scram at 135 �F condensate temp. All | | systems responded as designed with no abnormalities noted. Investigation | | into cause in progress." | | | | All rods fully inserted following the manual reactor scram. Group 2 and 3 | | isolations were received as expected on reduced reactor vessel level. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021