Event Notification Report for April 28, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/27/2000 - 04/28/2000 ** EVENT NUMBERS ** 36809 36924 36934 36935 36936 36937 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36809 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. ARMY |NOTIFICATION DATE: 03/17/2000| |LICENSEE: U.S. ARMY |NOTIFICATION TIME: 15:53[EST]| | CITY: ROCK ISLAND REGION: 3 |EVENT DATE: 03/17/2000| | COUNTY: STATE: IL |EVENT TIME: 12:00[CST]| |LICENSE#: 12-00722-06 AGREEMENT: Y |LAST UPDATE DATE: 04/27/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN JACOBSON R3 | | |AL BELISLE R2 | +------------------------------------------------+DON COOL NMSS | | NRC NOTIFIED BY: JEFF HAVENNER |CHARLES MILLER IRO | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT AN M43A1 CHEMICAL AGENT DETECTOR CELL MODULE CONTAINING 250 | | �Ci OF AMERICIUM-241 HAD BEEN MISSING FROM FT. BRAGG (NORTH CAROLINA) SINCE | | APRIL 1996 | | | | Late yesterday afternoon (03/16/00), representatives from Ft. Bragg, North | | Carolina, requested the U.S. Army in Rock Island, Illinois, to help trace | | files for documentation regarding a cell module that was discovered to be | | missing from an M43A1 chemical agent detector. (The cell module contained | | 250 �Ci of americium-241.) The most recent documentation found related to | | the missing cell module indicated that it was last seen at Ft. Bragg in | | April of 1996. More recent paperwork has not yet been found. The licensee | | determined this event to reportable at approximately 1200 CST today | | (03/17/00). | | | | The licensee hypothesized that the M43A1 chemical agent detector may have | | been turned into a maintenance unit at some point. If the device tested | | with bad air flow, the maintenance unit could have replaced several items | | including the cell module. At this time, it is believed that the cell | | module in question may have been removed (without any paperwork) and that | | the device may have been returned without a replacement cell module | | installed. | | | | The licensee stated that there does not appear to be any likelihood that the | | general public will get involved with this issue. The licensee plans to | | submit a 30-day written report to the NRC Region 3 office. (Call the NRC | | operations officer for licensee contact information.) | | | | * * * UPDATE AT 1420 ON 03/30/00 BY MOHS RECEIVED BY WEAVER * * * | | | | The module was found on March 23, 2000. The Operations Center notified the | | R3DO (Gardner) and R2DO (Caudle) and NMSS (Sherbini). | | | | ***** UPDATE AT 1631 ON 04/27/00 FROM JEFF HAVENNER TO LEIGH TROCINE ***** | | | | Based on a paper trail, the missing item was located at a Defense Logistics | | Agency (DLA) facility in Anniston, Alabama. The M43A1 chemical agent | | detector cell module was non-functional and had been removed during | | maintenance. It was then turned in through channels and sent to this depot | | facility. | | | | The NRC operations officer notified the R3DO (Shear), R2DO (Fredrickson), | | and NMSS EO (Cool). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36924 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 04/24/2000| | UNIT: [1] [] [] STATE: AL |NOTIFICATION TIME: 16:26[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/24/2000| +------------------------------------------------+EVENT TIME: 12:53[CDT]| | NRC NOTIFIED BY: WES CUMBEE |LAST UPDATE DATE: 04/27/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC START OF THE PENETRATION ROOM FILTRATION SYSTEM DURING MAINTENANCE | | ACTIVITIES. | | | | Maintenance investigation of a high vibration on "1B" Spent Fuel Pool | | Exhaust fan resulted in the trip of the Spent Fuel Pool ventilation and | | subsequent autostart of the Penetration Room Filtration System. All systems | | operated as required. | | | | Operations restarted the Spent Fuel Pool ventilation and secured the | | Penetration Room Filtration System. | | | | An investigation into this event is in progress. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | ***** UPDATE AT 1357 EDT ON 04/27/00 FROM VAUDY HOLLY, JR. TO LEIGH TROCINE | | ***** | | | | The licensee is retracting this event notification. The following text is a | | portion of a facsimile received from the licensee: | | | | "This event has been evaluated further and determined to be an invalid | | actuation based on 10 CFR 50.72(b)(2)(ii)(B)(3)(iv) and (v). An invalid | | actuation of the fuel building ventilation system or auxiliary building | | ventilation system is not reportable." | | | | "The accident analysis for fuel handling accidents in the spent fuel pool | | (SFP) credits the high radiation signal initiation of SFP ventilation | | isolation and penetration room filtration (PRF) system start. The low | | differential pressure start of the PRF system is not credited; therefore, | | PRF system actuation in the absence of a high radiation signal is not an | | [engineered safety feature (ESF)] actuation. For the purposes of 10 CFR | | 50.72, this is an invalid actuation." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R2DO (Fredrickson). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36934 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/27/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 12:45[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/23/1998| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 06:13[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/27/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |GARY SHEAR R3 | | DOCKET: 0707001 |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: THOMAS WHITE | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HISTORICAL REPORT OF THE DISCOVERY OF A FAULT CONDITION ON THREE MODULES ON | | THE 'X' CRITICALITY ACCIDENT ALARM SYSTEM CLUSTER DURING 1998 (24-HOUR | | REPORT) | | | | The following text is a portion of a facsimile received from Paducah: | | | | "At 0613 [CDT] on 05/23/98, the PSS was informed of a trouble alarm on C-337 | | Criticality Accident Alarm System (CAAS) 'X' cluster. Investigation of | | trouble alarm revealed that all three modules on [the] 'X' CAAS cluster were | | in a 'Fault' condition. The cluster was reset, and the Fault condition | | cleared. This condition was not reported as an event in which equipment | | required by the [Technical Safety Requirement (TSR)] is disabled or fails to | | function as designed as required by 10 CFR 76.120(c)(2). This event was | | found during the investigation of Notification Worksheet No. 36880, which | | occurred on 04/12/00. [The] 'X' CAAS cluster was in this 'Fault' condition | | from 0613 [CDT] until 0722 [CDT on 05/23/98]. During this time, an area in | | the Southeast corner of C-337, which contains a [Department of Energy (DOE)] | | Material Storage Area (DMSA) that holds 55-gallon drums of potentially | | fissile material, was without operable CAAS coverage." | | | | "This event should have been reported under 10 CFR 76.120(c)(2) as an event | | in which equipment required by the TSR is disabled or fails to function as | | designed." | | | | This issue was determined to be reportable yesterday afternoon. | | | | Paducah personnel notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36935 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NRC REGION 1 OFFICE |NOTIFICATION DATE: 04/27/2000| |LICENSEE: DAVID BLACKMORE & ASSOCIATES |NOTIFICATION TIME: 13:48[EDT]| | CITY: POTTSTOWN REGION: 1 |EVENT DATE: 04/27/2000| | COUNTY: STATE: PA |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 04/27/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JAMES NOGGLE R1 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES NOGGLE (R1DO) | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DAVID BLACKMORE & ASSOCIATES REPORT TO NRC REGION 1 REGARDING A CRUSHED SOIL | | DENSITY GAUGE IN POTTSTOWN, PENNSYLVANIA | | | | At 1345 on 04/27/00, Joe Hughes (the radiation safety officer at David | | Blackmore & Associates) notified the NRC Region 1 office that a soil density | | gauge was crushed at a construction site in Pottstown, Pennsylvania, near | | Porter Road. Mr. Hughes was informed of the event and was en route to the | | job site at the time of this notification to the NRC Region 1 office. Mr. | | Hughes called the NRC Region 1 Office to ask advice and was not aware of the | | event specifics. The NRC Region 1 office (Noggle) subsequently notified the | | NRC operations center. | | | | The R1DO (James Noggle) stated that the NRC Office of Nuclear Materials | | Safety and Safeguards (George Pangburn and Judith Joustra) had been | | informed. | | | | (Call the NRC operations office for licensee contact information.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36936 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 04/27/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 14:42[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 04/27/2000| +------------------------------------------------+EVENT TIME: 10:50[EDT]| | NRC NOTIFIED BY: BOB STEIGERWALD |LAST UPDATE DATE: 04/27/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: |FEMA, DOE, USDA, HHS FAX | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |EPA, DOT (via NRC) FAX | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |90 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - STATE DEC AND U.S. COAST GUARD NOTIFIED OF SMALL OIL DISCHARGE INTO LAKE | | ONTARIO - | | | | The licensee notified the New York State Department of Environmental | | Conservation (DEC), the U.S. Coast Guard, and the NRC Resident Inspector | | that approximately two ounces of oil had discharged from the plant storm | | drains into Lake Ontario. The oil has dispersed. The cause is unknown and | | being investigated by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36937 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 04/27/2000| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 17:03[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 04/27/2000| +------------------------------------------------+EVENT TIME: 16:05[EDT]| | NRC NOTIFIED BY: JIM KOVALCHICK |LAST UPDATE DATE: 04/27/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF POWER TO THE TECHNICAL SUPPORT CENTER | | | | At 1505 on 04/27/00, power was lost to the Peach Bottom Technical Support | | Center (TSC) as a result of breaker malfunctions during planned electrical | | switching. As of 1605, power had been out for greater than 1 hour | | constituting a loss of emergency assessment capability at the TSC. | | | | Assessment capability remains in the main control room and the Emergency | | Operations Facilities, and communication is still in tact between the | | control room and the TSC. Troubleshooting and restoration activities by | | maintenance and operations personnel are currently in progress, and this | | condition does not affect either of the operating plants. | | | | The licensee stated that power to the TSC was lost when two breakers failed | | to operate during performance of activities to restore power to a normal | | lineup following maintenance work on lines that do not normally affect the | | TSC. (However, when this particular lineup change is made, it realigns the | | power going to the TSC.) When the two breakers failed to operate, power at | | the TSC was lost. The licensee stated that the loss of power affected the | | TSC only and that no other systems of facilities were affected. | | | | The licensee plans to notify the NRC resident inspector. | | | | ***** UPDATE AT 1729 ON 04/27/00 FROM JIM KOVALCHICK TO LEIGH TROCINE ***** | | | | Power was restored to the TSC at 1710 on 04/27/00. | | | | The licensee notified the NRC resident inspector. The NRC operations center | | notified the R1DO (Noggle). | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021