Event Notification Report for April 21, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/20/2000 - 04/21/2000 ** EVENT NUMBERS ** 36908 36909 36910 36911 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36908 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 04/20/2000| | UNIT: [] [2] [3] STATE: CA |NOTIFICATION TIME: 11:43[EDT]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 04/20/2000| +------------------------------------------------+EVENT TIME: 07:45[PDT]| | NRC NOTIFIED BY: CLAY WILLIAMS |LAST UPDATE DATE: 04/20/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DALE POWERS R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HPSI, LPSI & CS SYSTEMS OUTSIDE THEIR DESIGN BASIS DUE TO LACK OF | | INSTALLED INSULATION - | | | | The following is the text of a fax received from San Onofre: | | | | This notification from San Onofre Units 2 and 3 is being made in accordance | | with 10CFR50.72(b)(1)(ii)(B) for the condition of the High Pressure Safety | | Injection (HPSI), Low Pressure Safety Injection (LPSI) and Containment Spray | | (CS) Systems being outside their design basis. This condition exists for | | both Units 2 and 3. | | | | On 04/19/00, during an NRC inspection, it was discovered that portions of | | the ECCS piping were not insulated as assumed in design calculations. | | Affected lines are the suction and discharge piping for the HPSI Pumps | | #P017, P018 & P019, LPSI Pumps #P015 & P016, and CS Pumps #P013 & P014. The | | consequence of the missing insulation is that the heat loads in the ECCS | | pump rooms will be higher than assumed in the plant accident analyses. | | | | At 0745 PDT on 04/20/00, SCE concluded that ECCS pump room temperatures | | during certain accident scenarios may not remain below their design basis | | room temperatures of 104�F. However, the equipment in the pump rooms | | continues to be operable at the calculated higher post-accident | | temperatures. That is, even with the higher than expected ECCS pump room | | temperatures, the affected equipment would continue to be able to perform | | its intended safety function. | | | | SCE has installed some temporary insulation and will take actions to install | | permanent insulation on the affected piping. SCE's investigation of this | | occurrence is ongoing; the cause of this condition will be reported in the | | followup 30 day licensee event report. | | | | At the time of this discovery, both Units 2 and 3 were operating at about | | 100% power: Unit 1 remains permanently defueled. SCE plans to notify the | | NRC Resident Inspectors about this issue and will provide them with a copy | | of this event report. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36909 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 04/20/2000| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 14:02[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 04/20/2000| +------------------------------------------------+EVENT TIME: 09:30[EDT]| | NRC NOTIFIED BY: KEVIN DONNELLY |LAST UPDATE DATE: 04/20/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: |ED GOODWIN NRR | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - UNIT 2 S/Gs PRIMARY-TO-SECONDARY DESIGN DIFFERENTIAL PRESSURE OUTSIDE | | DESIGN BASIS - | | | | Indian Point Unit 2 received a letter from Westinghouse (the NSSS Supplier) | | which stated that Westinghouse is in the process of completing a Nuclear | | Safety Advisory Letter regarding the primary-to-secondary design pressure | | differential in the steam generators. The current design pressure listed in | | the equipment Specification is 1550 psid. With an anticipated steam | | generator outlet pressure in the 650 to 660 psia range, this design pressure | | will be exceeded. However, Indian Point Unit 2 has an analysis that | | determined that the limiting structure within the steam generator, the tube | | sheet, can withstand a pressure differential of 1750 psid. This issue may be | | addressed by updating the design pressure and stress reports demonstrating | | compliance with the ASME Code as governed by Section IWA-4312, Re-rating, of | | Section Xl of the ASME Code. | | | | The licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36910 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 04/20/2000| | UNIT: [] [2] [] STATE: FL |NOTIFICATION TIME: 17:38[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 04/17/2000| +------------------------------------------------+EVENT TIME: 10:20[EDT]| | NRC NOTIFIED BY: STEVE MERRILL |LAST UPDATE DATE: 04/20/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: |DAVID MATTHEWS NRR | |NINF INFORMATION ONLY |CHUCK DePUY FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Hot Shutdown |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - RCS LEAKAGE CRITERIA FOR DECLARING AN UNUSUAL EVENT EXISTED ON 04/17/00 - | | | | At 1020 on 04/17/00, St. Lucie Unit 2 was in Mode 4 in a refueling outage | | preparing to go on shutdown cooling. | | A pre-job brief was conducted and included a discussion of the potential for | | pressurizer level change, relief valve lifting and the need to monitor the | | telltale on containment spray isolation valve #MV-07-3 to determine valve | | leakage. The expectation was established that the operating crew would | | terminate the evolution if unexpected leakage was observed with the primary | | focus on the telltale tubing monitoring containment spray isolation valve | | #MV-07-3. | | | | The control room operator observed a sudden drop in pressurizer level once | | the last shutdown cooling isolation valve was opened (6% drop on the hot | | calibration indication). The valve was immediately closed and pressurizer | | level stabilized; the evolution duration was approximately 3 minutes. As | | the valve was closing, the field operator stated he was seeing leakage | | through the tygon tubing, which he estimated to be about 1 to 2 gpm. There | | was no increase in sump level and no abnormal interfacing system behavior. | | Operations department personnel believed the behavior observed was | | consistent with filling shutdown cooling lines. | | | | Subsequently, the on-shift engineer performed an inventory balance and, | | without adjusting for changing temperatures and pressures, estimated a 100 | | gpm leak had occurred. The Nuclear Plant Supervisor (NPS) did not feel the | | inventory balance was valid in that he knew the accuracy of the calculation | | was biased because of the effect of temperature and pressure and the short | | duration of the event. Based on the discrepancy between the calculation and | | field observation, the NPS had a condition report issued to determine the | | RCS leak rate. | | | | The NPS rationale for not entering the Emergency Plan and that RCS leakage | | was not greater than 10 gpm was based on the following: | | | | - his field operator's observations showed a 1-2 gpm leak, | | - a lack of any increase in sump level, | | - a lack of any abnormal plant interfacing systems behavior, and | | - the evolution was consistent with his understanding of the pressurizer | | level behavior when filling shutdown cooling piping based on his observation | | in the past. | | | | A subsequent activity of placing shutdown cooling on line later that same | | day resulted in a similar event, | | with significantly less inventory loss. Shutdown cooling train A was placed | | on line the afternoon of 04/17/00. | | | | However, based on the results of the engineering review, the pressurizer | | level drop was not solely due to the fill and vent evolution of the shutdown | | cooling system, as originally concluded. Two hundred (200) gallons of RCS | | inventory was transferred inter-system during this event. FPL has concluded | | that this short duration, operator-terminated event met the procedural | | requirements for entering the emergency plan. However, it is clear upon | | review of the context and intent of the emergency plan that at no time did | | an actual emergency or threat thereof exist. | | | | As provided for in NUREG 1022, "a licensee may discover that an event or | | condition had existed which met the emergency plan criteria, but that no | | emergency had been declared and the basis for the emergency class no longer | | exists at the time of discovery". Based on an engineering review, FPL | | concludes that while initiating shutdown cooling on the A train on 04/17/00, | | an RCS inventory transfer occurred to interfacing systems in the 2-3 minute | | periods associated with starting shutdown cooling. The initial attempt to | | place shutdown cooling on line, and possibly a second attempt later the same | | day, resulted in leakage exceeding the Technical Specification threshold and | | would constitute entry into a Notification of Unusual Event. Although the | | criteria was met, FPL is not declaring an emergency for the following | | reasons: | | | | 1. The event was the result of a planned activity and the greater than | | expected pressurizer level drop was quickly compensated for by operator | | actions. | | | | 2. The event was of very short duration and at no time challenged the | | ability for decay heat removal or posed a threat to the health and safety of | | the public or plant personnel. | | | | 3. The circumstances associated with determining the appropriate | | classification of the event required three days of engineering evaluation. | | | | State and local county officials and the Senior NRC Resident Inspector are | | being informed of the event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36911 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 04/20/2000| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 20:29[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/20/2000| +------------------------------------------------+EVENT TIME: 19:30[EDT]| | NRC NOTIFIED BY: DOUG AMTHFIELD |LAST UPDATE DATE: 04/20/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - LICENSEE NOTIFIED NATIONAL RESPONSE CENTER AND STATE DEP OF A CHEMICAL | | SPILL ONSITE - | | | | The licensee notified the National Response Center and the State Department | | of Environmental Protection (DEP) that approximately 5 gallons of a mixture | | of sulfuric acid and sodium hydroxide spilled from a tank truck onto the | | ground after a chemical reaction took place. The spill was contained within | | a portable dike area onsite and is being cleaned up. | | | | The licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021