Event Notification Report for April 11, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/10/2000 - 04/11/2000 ** EVENT NUMBERS ** 36872 36878 36879 36880 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Hospital |Event Number: 36872 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST LOUIS UNIVERSITY HOSPITAL |NOTIFICATION DATE: 04/07/2000| |LICENSEE: ST LOUIS UNIVERSITY HOSPITAL |NOTIFICATION TIME: 16:42[EDT]| | CITY: ST LOUIS REGION: 3 |EVENT DATE: 04/06/2000| | COUNTY: STATE: MO |EVENT TIME: 17:36[CDT]| |LICENSE#: 24-00196-07 AGREEMENT: N |LAST UPDATE DATE: 04/10/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS KOZAK R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MARK HAENCHEN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | A patient on a ventilator was being treated with a High Dose Radiation | | Remote Afterloader when the patient intervened causing a jarring motion | | which caused the patient's catheter to come part way out. The catheter came | | part way out after 13 of 14 dwell positions had been completed. Just before | | the commencement of the 14th dwell position the catheter was pulled out and | | the physicist immediately intervened and retracted the source such that the | | 14th dwell position was underdosed between 10 and 60%. The worst case is | | that the 14th dwell position, which was outside of the tumor volume, would | | have received as little as 40% of the original planned dose at that | | location. | | | | NRC Region 3 (Kevin Null) was notified of this event by the licensee. | | | | * * * UPDATE AT 1215 ON 04/10/00 BY DAWSON RECEIVED BY WEAVER * * * | | | | The licensee has requested that this event be retracted after discussions | | with NRC Region III. The dose did not deviate by greater than 20% from the | | intended dose and no dose was delivered to unintended sites. | | | | The NRC Operations Officer notified the R3DO (Hiland) and NMSS (Hickey). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36878 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 04/09/2000| | UNIT: [1] [] [] STATE: AL |NOTIFICATION TIME: 12:32[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/09/2000| +------------------------------------------------+EVENT TIME: 10:00[CDT]| | NRC NOTIFIED BY: BILL ARENS |LAST UPDATE DATE: 04/10/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |STEVE CAHILL R2 | |10 CFR SECTION: | | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF BOTH VITAL BUSES DURING 'B' TRAIN LOAD SHED TESTING | | | | At 1000 CDT, during Unit 1 'B' train load shed testing (performed every 18 | | months during a refueling outage), the 'A' startup transformer tripped, | | resulting in a loss of offsite power to both trains of Unit 1 vital buses, | | the autostart of 'A' train emergency diesel generators (EDGs) which | | reenergized the 'A' train buses, and the sustained deenergization of the 'B' | | train vital buses. | | | | At the time of this event, Unit 1 was defueled, with the 'B' train service | | water system out of service and the 'B' train EDG unavailable to Unit 1. | | Both trains of Unit 1 vital power were aligned to the '1A' startup | | transformer as part of the load shed test that was in progress. The loss of | | the '1A' startup transformer coincided with, and appears to be associated | | with, the removal of a jumper from a 'B' train sequencer relay. | | Investigation of this apparent cause is continuing. | | | | The 'A' train vital buses were immediately restored to service by the 'A' | | train EDGs. | | | | At 1018 CDT, spent fuel pool cooling was manually restored. Spent fuel pool | | temperature remained at 98�F throughout this event. | | | | At 1019 CDT. the 'B' train buses were manually reenergized from the '1B' | | startup transformer. | | | | At 1053 CDT, the 'A' train buses were transferred from the EDGs to offsite | | power. | | | | Unit 2 remains at 100% power and is unaffected by this event. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE AT 1615 ON 4/10/00, BY COLLINS RECEIVED BY WEAVER * * * | | | | The following is an update to the above non-emergency report: | | | | The purpose of this emergency notification is to retroactively declare and | | terminate a Notice of Unusual Event (NOUE) that occurred on April 9, 2000. | | As of 1000 CDT on April 9, 2000, a NOUE was declared due to a loss of | | offsite power to the Unit 1 vital buses. The emergency declaration was | | terminated at 1019 CDT on April 9, 2000 at which time one train of vital | | power was reestablished from offsite power supply. During this event, one | | train of vital power was automatically supplied from an EDG. | | | | At the time of the event, Unit 1 was defueled. The 'B' train EDG was not | | available due to routine outage activities and the Unit 1 'A' startup | | transformer was supplying both trains of vital buses from offsite power. | | | | At 1000 CDT on April 9, 2000, the Unit 1 'A' startup transformer tripped for | | unknown reason, resulting in a loss of power to both trains of vital | | electrical buses. Both 'A' train EDGs automatically started and reenergized | | the Unit 1 'A' train vital buses within seconds. The Unit 1 'B' train vital | | buses remained deenergized for about 19 minutes until the Unit 1 'B' startup | | transformer was aligned by the operators to supply power to them. The cause | | of the Unit 1 ' A' startup transformer trip is unknown and being | | investigated. | | | | This event resulted in a brief loss of spent fuel pool cooling. Spent fuel | | pool cooling was restored by the operators at 1018 CDT on April 9, 2000 in | | accordance with plant procedures. The temperature of the spent fuel pool | | remained constant at 98�F throughout this event. Following a walkdown for | | faults, the Unit 1 'B' train vital buses were reenergized from offsite power | | at 1019 CDT from the Unit 1 'B' startup transformer. Offsite electrical | | power was restored to the 'A' train vital buses at 1053 CDT and the EDGs | | were secured and returned to normal standby alignment. The operations shift | | crew evaluated this event and reported it to the NRC as a four hour | | non-emergency report per 10CFR50.72. The operations shift crew recognized | | the momentary loss of power to the vital buses but after reviewing the | | emergency implementation procedures and Technical Specifications concluded | | that a loss of both trains of offsite power had not occurred. That was | | concluded since the operators were readily able to align the Unit 1 'B' | | startup transformer to supply the 'B' train vital buses. Further evaluation | | of the event on April 10, 2000, concluded that a NOUE was appropriate since | | offsite power was momentarily lost to the vital electrical buses. | | | | Unit 2 remained at 100% power during this event and was unaffected by this | | event. | | | | The licensee informed the NRC resident inspector of this notification. | | | | The NRC Operations Officer notified the R2DO (Cahill), NRR EO (Marsh), IRO | | (Giitter) and FEMA (Steindruff). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36879 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/10/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 20:57[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/10/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 14:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/10/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |PATRICK HILAND R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICK LARSON | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01, 24 HOUR REPORT | | | | "AT 1400 HOURS ON APRIL 10, 2000, X-710 LABORATORY PERSONNEL WERE CONDUCTING | | A SELF ASSESSMENT REVIEW OF NCSA-710-025.A00 (HANDLING AND STORAGE OF | | SAMPLES FROM ES&H ANALYTICAL LABS) WHEN THEY DISCOVERED THAT REQUIREMENT #4 | | (SPACING) WAS NOT BEING MAINTAINED IN A SPECIFIED STORAGE AREA WITHIN THE | | FACILITY. REQUIREMENT #4 STATES: 'A | | MINIMUM SPACING OF TWO FEET SHALL BE MAINTAINED BETWEEN GROUPS OF SAMPLES, | | EXCLUDING EXEMPTED SAMPLES.' THE FACT THAT THIS REQUIREMENT WAS NOT BEING | | MAINTAINED RESULTED IN A LOSS OF ONE CONTROL (SPACING). THIS CONSTITUTES A | | LOSS OF CONTROL 'A' (SPACING) AS IDENTIFIED IN THE DOUBLE CONTINGENCY MATRIX | | A/B.7.1. CONTROL 'B' (MASS + VOLUME + ENRICHMENT) WAS MAINTAINED THROUGHOUT | | THIS EVENT. | | | | "AT THE DIRECTION OF THE PLANT SHIFT SUPERINTENDENT, THE REQUIREMENTS FOR AN | | ANOMALOUS CONDITION WERE ESTABLISHED PER PLANT PROCEDURES. AT 1630 HOURS ON | | 04/10/2000, DOUBLE CONTINGENCY CONTROLS WERE REESTABLISHED (SPACING) UNDER | | THE DIRECTION OF ONSCENE NUCLEAR CRITICALITY SAFETY PERSONNEL. | | | | "AT THE DIRECTION OF THE PLANT SHIFT SUPERINTENDENT, THE X-710 MANAGEMENT | | STAFF WILL CONDUCT BRIEFINGS WITH THE RESPECTIVE PERSONNEL TO PREVENT | | RECURRENCE." | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36880 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/10/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 21:03[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/10/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 09:47[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/10/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |PATRICK HILAND R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CALVIN PITTMAN | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY EQUIPMENT FAILURE (CRITICALITY ALARM SYSTEM TROUBLE) | | | | "At 0947 CDT on 04/10/00, the Plant Shift Superintendent was informed of a | | trouble alarm on the C-337A Criticality Accident Alarm System (CAAS) | | cluster. Investigation of trouble alarm revealed that all three modules on | | the 'N' CAAS cluster were in a 'Fault' condition. With all three modules in | | this condition, the system was unable to perform its intended safety | | function, rendering the system inoperable. The system is required to be | | operable according to TSR 2.2.4.3 for the current mode of operation in | | twelve rad areas covered by CAAS systems. Overlapping coverage for the | | C-337A facility was provided by the C-337 'X' and 'V' CAAS clusters. | | However, the C-360/C-337 tie line CAAS coverage is provided by the 'N' | | cluster. The system was inoperable for approximately seven minutes until it | | could be reset per procedure. A portion of the C-337/C-360 tie line was | | without CAAS coverage as required by TSR 2.2.4.3 during the time of cluster | | inoperability." | | | | The NRC Senior Resident Inspector has been notified of this event, | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021